HL incident on 2017-07-22 — OK

Operator
Explorer Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15
Incident datetime
2017-07-22 16:32
Report number
Location
OK
Narrative
On saturday, july 22, 2017 at 16:32 cst a release of 2.50 barrels, or 105 gallons of transmix occurred. The source of the release was from a crack on a 0.75 inch threaded nipple associated with a pd transfer pump at the greenville, texas tank farm. The release was totally contained on the property, immediately addressed and the impacted soil was properly managed.
Detailed record list
Report Received Date
2017-08-21 00:00:00
Iyear
2017
Report Number
20170259
Supplemental Number
23094
Report Type
Supplemental Final
Operator Id
Name
Explorer Pipeline Co
Operator Street Address
Po Box 2650
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74101
Local Datetime
2017-07-22 16:32:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
2.5
Recovered Bbls
2.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-07-22 16:32:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Affected Area Isolated From Mainline.
On Site Datetime
2017-07-22 16:32:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Greenville Tank Farm
Segment Name
Greenville Tank Farm
Onshore State Abbreviation
Tx
Onshore Postal Code
75135-0354
Onshore City Name
Caddo Mills
Onshore County Name
Hunt
Designated Location
Milepost/valve Station
Designated Name
310.7
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
1971
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
15
Est Cost Emergency
5000
Est Cost Environmental
17000
Est Cost Other
0
Prpty
22215
Accident Psig
67.9
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controllers actions or inactions did not cause or contribute to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Pipe Nipple
Additional Vibration Ind
Yes
Preparer Name
K**** B****
Preparer Title
Manager Dot And Regulatory Compliance
Preparer Email
K*****@e***.com
Preparer Telephone
9184935104
Prepared Date
2018-02-02 00:00:00
Authorizer Name
J** S****
Authorizer Telephone
9184935143
Authorizer Title
Director Hsse And Engineering
Authorizer Email
J*****@e***.com
Narrative
On saturday, july 22, 2017 at 16:32 cst a release of 2.50 barrels, or 105 gallons of transmix occurred. The source of the release was from a crack on a 0.75 inch threaded nipple associated with a pd transfer pump at the greenville, texas tank farm. The release was totally contained on the property, immediately addressed and the impacted soil was properly managed.
Report Received Date 2017-08-21 00:00:00
Iyear 2017
Report Number 20170259
Supplemental Number 23094
Report Type Supplemental Final
Operator Id 4805 PHMSA Enforcement
Name Explorer Pipeline Co
Operator Street Address Po Box 2650
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74101
Local Datetime 2017-07-22 16:32:00
Location Latitude 33.035685 Google Maps OpenStreetMap
Location Longitude -96.200798 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 2.5
Recovered Bbls 2.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-07-22 16:32:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Affected Area Isolated From Mainline.
On Site Datetime 2017-07-22 16:32:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Greenville Tank Farm
Segment Name Greenville Tank Farm
Onshore State Abbreviation Tx
Onshore Postal Code 75135-0354
Onshore City Name Caddo Mills
Onshore County Name Hunt
Designated Location Milepost/valve Station
Designated Name 310.7
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 1971
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 15
Est Cost Emergency 5000
Est Cost Environmental 17000
Est Cost Other 0
Prpty 22215
Accident Psig 67.9
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controllers actions or inactions did not cause or contribute to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Pipe Nipple
Additional Vibration Ind Yes
Preparer Name K**** B****
Preparer Title Manager Dot And Regulatory Compliance
Preparer Email K*****@e***.com
Preparer Telephone 9184935104
Prepared Date 2018-02-02 00:00:00
Authorizer Name J** S****
Authorizer Telephone 9184935143
Authorizer Title Director Hsse And Engineering
Authorizer Email J*****@e***.com
Narrative On saturday, july 22, 2017 at 16:32 cst a release of 2.50 barrels, or 105 gallons of transmix occurred. The source of the release was from a crack on a 0.75 inch threaded nipple associated with a pd transfer pump at the greenville, texas tank farm. The release was totally contained on the property, immediately addressed and the impacted soil was properly managed.

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