HL incident on 2017-07-19 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25
Incident datetime
2017-07-19 03:26
Report number
Location
OK
Narrative
At approximately 03:26 am on july 19th 2017, oneok pipeline control center received a hazardous atmospheric lock-out and station shutdown at oneok's midland pump station located near midland, texas. Local field operations employees were notified and dispatched to the location. Field employees arrived at the station at approximately 04:27 am and identified a "hissing" sound coming from the door on the scraper trap. Employees isolated the trap and relieved the residual product to the flare system. Upon opening the scraper trap door, it was determined the o-ring in the closure had failed causing the release. A new o-ring was installed and the scraper trap was returned to service at approximately 05:57 am.
Detailed record list
Report Received Date
2017-08-07 00:00:00
Iyear
2017
Report Number
20170239
Supplemental Number
22528
Report Type
Original Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2017-07-19 03:26:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.2
Intentional Release Bbls
2.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2017-07-19 03:26:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Station Was Isolated And Pipeline Continued To Flow By Station
On Site Datetime
2017-07-19 04:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Midland Pump Station
Segment Name
Oneok Txl0373a 8" North Lateral (Index 21373)
Onshore State Abbreviation
Tx
Onshore Postal Code
79782
Onshore City Name
Not Within A Municipality
Onshore County Name
Midland
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2016
Material Involved
Material Other Than Carbon Steel
Material Details
O-Ring
Release Type
Leak
Leak Type
Other
Leak Type Other
O-Ring Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
8
Est Cost Prop Damage
25
Est Cost Emergency
150
Est Cost Environmental
0
Est Cost Other
0
Prpty
183
Accident Psig
500
Mop Psig
1250
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
6
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place prior to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear And Tear
Preparer Name
N*** J****
Preparer Title
Requlatory Compliance Manager
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2017-08-07 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
N*********@o****.com
Narrative
At approximately 03:26 am on july 19th 2017, oneok pipeline control center received a hazardous atmospheric lock-out and station shutdown at oneok's midland pump station located near midland, texas. Local field operations employees were notified and dispatched to the location. Field employees arrived at the station at approximately 04:27 am and identified a "hissing" sound coming from the door on the scraper trap. Employees isolated the trap and relieved the residual product to the flare system. Upon opening the scraper trap door, it was determined the o-ring in the closure had failed causing the release. A new o-ring was installed and the scraper trap was returned to service at approximately 05:57 am.
Report Received Date 2017-08-07 00:00:00
Iyear 2017
Report Number 20170239
Supplemental Number 22528
Report Type Original Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2017-07-19 03:26:00
Location Latitude 32.019869 Google Maps OpenStreetMap
Location Longitude -102.022412 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.2
Intentional Release Bbls 2.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2017-07-19 03:26:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Station Was Isolated And Pipeline Continued To Flow By Station
On Site Datetime 2017-07-19 04:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Midland Pump Station
Segment Name Oneok Txl0373a 8" North Lateral (Index 21373)
Onshore State Abbreviation Tx
Onshore Postal Code 79782
Onshore City Name Not Within A Municipality
Onshore County Name Midland
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 2016
Material Involved Material Other Than Carbon Steel
Material Details O-Ring
Release Type Leak
Leak Type Other
Leak Type Other O-Ring Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 8
Est Cost Prop Damage 25
Est Cost Emergency 150
Est Cost Environmental 0
Est Cost Other 0
Prpty 183
Accident Psig 500
Mop Psig 1250
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 6
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had taken place prior to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear And Tear
Preparer Name N*** J****
Preparer Title Requlatory Compliance Manager
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2017-08-07 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Manager
Authorizer Email N*********@o****.com
Narrative At approximately 03:26 am on july 19th 2017, oneok pipeline control center received a hazardous atmospheric lock-out and station shutdown at oneok's midland pump station located near midland, texas. Local field operations employees were notified and dispatched to the location. Field employees arrived at the station at approximately 04:27 am and identified a "hissing" sound coming from the door on the scraper trap. Employees isolated the trap and relieved the residual product to the flare system. Upon opening the scraper trap door, it was determined the o-ring in the closure had failed causing the release. A new o-ring was installed and the scraper trap was returned to service at approximately 05:57 am.

All rights reserved. Copyright © by ClearPHMSA