HL incident on 2017-07-07 — TX

Operator
Exxonmobil Pipeline Co
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40,000
Incident datetime
2017-07-07 09:15
Report number
Location
TX
Narrative
On 7/7/2017 a small pinhole was discovered on the bottom of a pipe girth weld connected to a 4" tee located on the sorrento dome propane pipeline manifold between the meters and the storage well. The manifold and associated pipeline was bypassed until repairs were made. Non-destructive x-ray tests determined a faulty weld was the cause of the release. Upon inspection, the cause of the leak was visually verified to be a pinhole due to an incomplete final pass at a girth weld at the 6 o'clock position of a welded tee. Nde found the base pipe material to be competent. Hc manifold is estimated to have been fabricated in the 1950s
Detailed record list
Report Received Date
2017-08-04 00:00:00
Iyear
2017
Report Number
20170237
Supplemental Number
30043
Report Type
Supplemental Final
Operator Id
Name
Exxonmobil Pipeline Co
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2017-07-07 09:15:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
1.88
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-07-07 09:15:00
System Part Involved
Onshore Equipment And Piping Associated With Belowground Storage
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Affected Manifold Pipeline Was Bypassed.
On Site Datetime
2017-07-07 09:15:00
Nrc Rpt Datetime
2017-07-07 12:18:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Sorrento Dome
Segment Name
Sorrento Dome Propane Manifold
Onshore State Abbreviation
La
Onshore Postal Code
70778
Onshore City Name
Not Within A Municipality
Onshore County Name
Ascension
Designated Location
Milepost/valve Station
Designated Name
Sorrento Dome
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
4.5
Pipe Wall Thickness
0.366
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Weld Subtype
Pipe Girth Weld
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
190
Est Cost Prop Damage
40000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
40190
Accident Psig
1057
Mop Psig
1450
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Weld failure was determined to be the cause of the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Other Analysis Ind
Yes
Other Analysis Details
Xray Of The Affected Weld
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Unknown
Pwf Additional Other Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K***** L Y****
Preparer Title
Pipeline Safety Compliance Advisor
Preparer Email
K*************@e*********.com
Preparer Telephone
225-324-3055
Prepared Date
2018-03-14 00:00:00
Authorizer Name
C******* B H********
Authorizer Telephone
832-624-7920
Authorizer Title
Empco And Amfo Sshe Manager
Authorizer Email
C*******************@e*********.com
Narrative
On 7/7/2017 a small pinhole was discovered on the bottom of a pipe girth weld connected to a 4" tee located on the sorrento dome propane pipeline manifold between the meters and the storage well. The manifold and associated pipeline was bypassed until repairs were made. Non-destructive x-ray tests determined a faulty weld was the cause of the release. Upon inspection, the cause of the leak was visually verified to be a pinhole due to an incomplete final pass at a girth weld at the 6 o'clock position of a welded tee. Nde found the base pipe material to be competent. Hc manifold is estimated to have been fabricated in the 1950s
Report Received Date 2017-08-04 00:00:00
Iyear 2017
Report Number 20170237
Supplemental Number 30043
Report Type Supplemental Final
Operator Id 4906 PHMSA Enforcement
Name Exxonmobil Pipeline Co
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2017-07-07 09:15:00
Location Latitude 30.173127 Google Maps OpenStreetMap
Location Longitude -90.787278 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 1.88
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2017-07-07 09:15:00
System Part Involved Onshore Equipment And Piping Associated With Belowground Storage
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Affected Manifold Pipeline Was Bypassed.
On Site Datetime 2017-07-07 09:15:00
Nrc Rpt Datetime 2017-07-07 12:18:00
Nrc Rpt Num 1183371 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Sorrento Dome
Segment Name Sorrento Dome Propane Manifold
Onshore State Abbreviation La
Onshore Postal Code 70778
Onshore City Name Not Within A Municipality
Onshore County Name Ascension
Designated Location Milepost/valve Station
Designated Name Sorrento Dome
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 4.5
Pipe Wall Thickness 0.366
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Weld Subtype Pipe Girth Weld
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 190
Est Cost Prop Damage 40000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 40190
Accident Psig 1057
Mop Psig 1450
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Weld failure was determined to be the cause of the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Other Analysis Ind Yes
Other Analysis Details Xray Of The Affected Weld
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Unknown
Pwf Additional Other Ind Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K***** L Y****
Preparer Title Pipeline Safety Compliance Advisor
Preparer Email K*************@e*********.com
Preparer Telephone 225-324-3055
Prepared Date 2018-03-14 00:00:00
Authorizer Name C******* B H********
Authorizer Telephone 832-624-7920
Authorizer Title Empco And Amfo Sshe Manager
Authorizer Email C*******************@e*********.com
Narrative On 7/7/2017 a small pinhole was discovered on the bottom of a pipe girth weld connected to a 4" tee located on the sorrento dome propane pipeline manifold between the meters and the storage well. The manifold and associated pipeline was bypassed until repairs were made. Non-destructive x-ray tests determined a faulty weld was the cause of the release. Upon inspection, the cause of the leak was visually verified to be a pinhole due to an incomplete final pass at a girth weld at the 6 o'clock position of a welded tee. Nde found the base pipe material to be competent. Hc manifold is estimated to have been fabricated in the 1950s

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