HL incident on 2017-06-28 — TX

Operator
Plains Pipeline, L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2017-06-28 13:46
Report number
Location
TX
Narrative
Approximately 740 bbls of crude oil were released as a result of internal corrosion. The failed segment of pipe has been sent to a lab to undergo metallurgical analysis; therefore, a supplemental report will be submitted once the cause is confirmed. The national response center (nrc) was notified and assigned initial report #1182539. A follow-up call to the nrc, assigned report #1182742. Supplemental narrative: the results of the metallurgical analysis indicate the leak occurred due to internal corrosion, associated with a pit and primarily due to the presences of dissolved CO2. The microbiological data obtained did not support mic as a contributing mechanism. The line remains purged at this time.
Detailed record list
Report Received Date
2017-07-28 00:00:00
Iyear
2017
Report Number
20170232
Supplemental Number
22815
Report Type
Supplemental Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-06-28 13:46:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
740
Recovered Bbls
306
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-06-28 13:46:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-06-28 13:48:00
Still Shutdown Ind
Yes
On Site Datetime
2017-06-28 15:05:00
Nrc Rpt Datetime
2017-06-28 14:25:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Buffalo Cashion
Segment Name
Blaine To Highway 33 Jct 8-Inch
Onshore State Abbreviation
Ok
Onshore Postal Code
73756
Onshore City Name
Dover
Onshore County Name
Kingfisher
Designated Location
Milepost/valve Station
Designated Name
27.16
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
64
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
X-52
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1960
Manufactured Year
1960
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0
Rel Water Name
Oil Collected In An Unnamed, Dry Pond. 267 Barrels Were Picked Up From This Dry Pond.
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
150000
Est Cost Gas Released
33300
Est Cost Prop Damage
10000
Est Cost Emergency
255000
Est Cost Environmental
199050
Est Cost Other
0
Prpty
647350
Accident Psig
87.99
Mop Psig
1040
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
109824
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2017
Geometry Recent Year
2017
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2017
Hydrtst Most Rcnt Pressure
1404
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C******* C*****
Preparer Title
Compliance Specialist
Preparer Email
C*******@p****.com
Preparer Telephone
713-993-5080
Preparer Fax
713-646-4310
Prepared Date
2017-11-15 00:00:00
Authorizer Name
N***** G*****
Authorizer Telephone
713-646-4336
Authorizer Title
Dir Environmental And Regulatory Compliance
Authorizer Email
N******@p****.com
Narrative
Approximately 740 bbls of crude oil were released as a result of internal corrosion. The failed segment of pipe has been sent to a lab to undergo metallurgical analysis; therefore, a supplemental report will be submitted once the cause is confirmed. The national response center (nrc) was notified and assigned initial report #1182539. A follow-up call to the nrc, assigned report #1182742. Supplemental narrative: the results of the metallurgical analysis indicate the leak occurred due to internal corrosion, associated with a pit and primarily due to the presences of dissolved CO2. The microbiological data obtained did not support mic as a contributing mechanism. The line remains purged at this time.
Report Received Date 2017-07-28 00:00:00
Iyear 2017
Report Number 20170232
Supplemental Number 22815
Report Type Supplemental Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-06-28 13:46:00
Location Latitude 35.938783 Google Maps OpenStreetMap
Location Longitude -97.994858 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 740
Recovered Bbls 306
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2017-06-28 13:46:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-06-28 13:48:00
Still Shutdown Ind Yes
On Site Datetime 2017-06-28 15:05:00
Nrc Rpt Datetime 2017-06-28 14:25:00
Nrc Rpt Num 1182539 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Buffalo Cashion
Segment Name Blaine To Highway 33 Jct 8-Inch
Onshore State Abbreviation Ok
Onshore Postal Code 73756
Onshore City Name Dover
Onshore County Name Kingfisher
Designated Location Milepost/valve Station
Designated Name 27.16
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 64
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification X-52
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1960
Manufactured Year 1960
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 0
Rel Water Name Oil Collected In An Unnamed, Dry Pond. 267 Barrels Were Picked Up From This Dry Pond.
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 150000
Est Cost Gas Released 33300
Est Cost Prop Damage 10000
Est Cost Emergency 255000
Est Cost Environmental 199050
Est Cost Other 0
Prpty 647350
Accident Psig 87.99
Mop Psig 1040
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 109824
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2017
Geometry Recent Year 2017
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2017
Hydrtst Most Rcnt Pressure 1404
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C******* C*****
Preparer Title Compliance Specialist
Preparer Email C*******@p****.com
Preparer Telephone 713-993-5080
Preparer Fax 713-646-4310
Prepared Date 2017-11-15 00:00:00
Authorizer Name N***** G*****
Authorizer Telephone 713-646-4336
Authorizer Title Dir Environmental And Regulatory Compliance
Authorizer Email N******@p****.com
Narrative Approximately 740 bbls of crude oil were released as a result of internal corrosion. The failed segment of pipe has been sent to a lab to undergo metallurgical analysis; therefore, a supplemental report will be submitted once the cause is confirmed. The national response center (nrc) was notified and assigned initial report #1182539. A follow-up call to the nrc, assigned report #1182742. Supplemental narrative: the results of the metallurgical analysis indicate the leak occurred due to internal corrosion, associated with a pit and primarily due to the presences of dissolved CO2. The microbiological data obtained did not support mic as a contributing mechanism. The line remains purged at this time.

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