HL incident on 2017-06-17 — PA

Operator
Buckeye Partners, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-06-17 01:30
Report number
Location
PA
Narrative
On the morning of june 17th, 2017, 0130 a release of gasoline occurred at the east chicago tank farm. The release occurred inside the east chicago junction as a result of a bleeder valve being left open. This valve was being used to refill the line after a hydrotest, and was left unattended while crews monitored other area of the refill operation. This resulted in a release of approximately 8 barrels of gasoline. All product was contained on buckeye property. A vac truck and crew were on site already and quickly mobilized, isolated the line and stopped all work. All free product was picked up and contaminated soil was removed. All required notifications were made. The city of east chicago and 911 dispatch center was also notified per requirements. Update 2-20-2018: internal investigation determined that the spill was caused by failure to follow lock out/ tag out (loto) procedures. Additional training was mandated for all personnel involved in the event.
Detailed record list
Report Received Date
2017-07-17 00:00:00
Iyear
2017
Report Number
20170217
Supplemental Number
23166
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2017-06-17 01:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
8
Recovered Bbls
8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-06-17 01:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-06-17 01:30:00
Restart Datetime
2017-06-20 07:30:00
On Site Datetime
2017-06-17 01:30:00
Nrc Rpt Datetime
2017-06-17 02:29:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
East Chicago
Segment Name
Eg
Onshore State Abbreviation
In
Onshore Postal Code
46312
Onshore City Name
East Chicago
Onshore County Name
Lake
Designated Location
Milepost/valve Station
Designated Name
East Chicago
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Valve Was Left Open
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
675
Est Cost Prop Damage
0
Est Cost Emergency
15000
Est Cost Environmental
47000
Est Cost Other
0
Prpty
62675
Accident Psig
1
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control center had no control over the activity being completed.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
1
Num Employees Failed
0
Num Contractors Tested
3
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
G***** G*****
Preparer Title
Compliance Specialist
Preparer Email
G******@b******.com
Preparer Telephone
412-716-8250
Preparer Fax
412-264-1433
Prepared Date
2018-02-20 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
6109044113
Authorizer Title
Director Regulatory Compliane
Authorizer Email
C*********@b******.com
Narrative
On the morning of june 17th, 2017, 0130 a release of gasoline occurred at the east chicago tank farm. The release occurred inside the east chicago junction as a result of a bleeder valve being left open. This valve was being used to refill the line after a hydrotest, and was left unattended while crews monitored other area of the refill operation. This resulted in a release of approximately 8 barrels of gasoline. All product was contained on buckeye property. A vac truck and crew were on site already and quickly mobilized, isolated the line and stopped all work. All free product was picked up and contaminated soil was removed. All required notifications were made. The city of east chicago and 911 dispatch center was also notified per requirements. Update 2-20-2018: internal investigation determined that the spill was caused by failure to follow lock out/ tag out (loto) procedures. Additional training was mandated for all personnel involved in the event.
Report Received Date 2017-07-17 00:00:00
Iyear 2017
Report Number 20170217
Supplemental Number 23166
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2017-06-17 01:30:00
Location Latitude 41.639527 Google Maps OpenStreetMap
Location Longitude -87.472417 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 8
Recovered Bbls 8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2017-06-17 01:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-06-17 01:30:00
Restart Datetime 2017-06-20 07:30:00
On Site Datetime 2017-06-17 01:30:00
Nrc Rpt Datetime 2017-06-17 02:29:00
Nrc Rpt Num 1181410 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name East Chicago
Segment Name Eg
Onshore State Abbreviation In
Onshore Postal Code 46312
Onshore City Name East Chicago
Onshore County Name Lake
Designated Location Milepost/valve Station
Designated Name East Chicago
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Valve Was Left Open
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 675
Est Cost Prop Damage 0
Est Cost Emergency 15000
Est Cost Environmental 47000
Est Cost Other 0
Prpty 62675
Accident Psig 1
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control center had no control over the activity being completed.
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 1
Num Employees Failed 0
Num Contractors Tested 3
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name G***** G*****
Preparer Title Compliance Specialist
Preparer Email G******@b******.com
Preparer Telephone 412-716-8250
Preparer Fax 412-264-1433
Prepared Date 2018-02-20 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 6109044113
Authorizer Title Director Regulatory Compliane
Authorizer Email C*********@b******.com
Narrative On the morning of june 17th, 2017, 0130 a release of gasoline occurred at the east chicago tank farm. The release occurred inside the east chicago junction as a result of a bleeder valve being left open. This valve was being used to refill the line after a hydrotest, and was left unattended while crews monitored other area of the refill operation. This resulted in a release of approximately 8 barrels of gasoline. All product was contained on buckeye property. A vac truck and crew were on site already and quickly mobilized, isolated the line and stopped all work. All free product was picked up and contaminated soil was removed. All required notifications were made. The city of east chicago and 911 dispatch center was also notified per requirements. Update 2-20-2018: internal investigation determined that the spill was caused by failure to follow lock out/ tag out (loto) procedures. Additional training was mandated for all personnel involved in the event.

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