HL incident on 2017-06-18 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$54,200
Incident datetime
2017-06-18 14:35
Report number
Location
TX
Narrative
The ndt level ii technician characterized the defect with ut & mt. The ut response indicated ~1" length at the id and mt confirmed an ~ 6" long defect on the od surface. Location of the crack was at the toe of the dsaw long seam of the pipe. A full encirclement type "b" steel steel was welded over the cracked area. 3/1/18 - corrected part a time land owner called in stain on ground, shut down time following notification by land owner.
Detailed record list
Report Received Date
2017-07-13 00:00:00
Iyear
2017
Report Number
20170215
Supplemental Number
36766
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2017-06-18 14:35:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.55
Recovered Bbls
0.55
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2017-06-18 14:35:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-06-18 14:47:00
Restart Datetime
2017-06-20 18:45:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2017-06-18 16:40:00
On Site Datetime
2017-06-18 15:10:00
Confirmed Discovery Datetime
2017-06-18 16:00:00
Nrc Rpt Datetime
2017-06-18 17:00:00
Nrc Rpt Num
Additional Nrc Report Numbers
1181753
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2017-06-18 14:47:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2017-06-18 14:47:00
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2017-06-18 14:50:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2017-06-19 17:30:00
Osro Arrived On Site Dt
6/19/2017 8:00
Num Pub Evacuated
0
Pipe Fac Name
Erath Ps To Pt. Neches 22"
Segment Name
Erath Ps To Lake Arthur Ps 22"
Onshore State Abbreviation
La
Onshore Postal Code
70528
Onshore City Name
Delcambre
Onshore County Name
Vermillion
Designated Location
Survey Station No.
Designated Name
6662+53
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
45
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
22
Pipe Wall Thickness
0.312
Pipe Smys
52000
Pipe Specification
5l-X52
Pipe Seam Type
Dsaw
Pipe Manufacturer
Kaiser Steel Corp
Pipe Coating Type
Coal Tar
Coating Applied Ind
Yes
Installation Year
1953
Manufactured Year
1953
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
54200
Est Cost Emergency
10000
Est Cost Environmental
0
Est Cost Other
0
Prpty
64200
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
765
Mop Psig
849
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2013-09-16 00:00:00
Maop Reversal Flow Ind
Yes
Surge Analysis Date
2013-01-30 00:00:00
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
142822
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controllers actions following a phone call from the public, land owner, were to shut down the pipeline and isolate that section of pipeline. Contacted supervisor and field personnel to investigate situation and make determination.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Field Exam Ind
Yes
Failure Type
Environmental Cracking-Related
Stress Subtype
Other
Stress Details
Fatigue Located At The Toe Of The Dsaw Long Seam. Crack At Od 6" Long, Id 1" Long.
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Ultrasonic Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2015
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Previous Year
2013
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Circ Wave Recent Year
2011
Circ Wv Rcnt Propul Method
Free Swimming
Circ Wv Rcnt Resolution
High Resolution
Ultrasonic Recent Year
2013
Ultrasonic Rcnt Propul Method
Free Swimming
Ultrasonic Rcnt Attuned
Crack
Geometry Recent Year
2015
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
Inside Ili Cups
Geometry Previous Year
2011
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
Inside Ili Cups
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2013
Hydrtst Most Rcnt Pressure
1126
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R****** K*****
Preparer Title
Operations Support Coordinator
Preparer Email
R*************@s****.com
Preparer Telephone
832 762 2682
Prepared Date
2022-06-16 00:00:00
Local Contact Name
J***** H*****
Local Contact Email
J************@s****.com
Local Contact Telephone
4095402781
Authorizer Name
D****** P****
Authorizer Telephone
832 762 2553
Authorizer Title
Integrity Regulatory Mngr.
Authorizer Email
D************@s****.com
Narrative
The ndt level ii technician characterized the defect with ut & mt. The ut response indicated ~1" length at the id and mt confirmed an ~ 6" long defect on the od surface. Location of the crack was at the toe of the dsaw long seam of the pipe. A full encirclement type "b" steel steel was welded over the cracked area. 3/1/18 - corrected part a time land owner called in stain on ground, shut down time following notification by land owner.
Report Received Date 2017-07-13 00:00:00
Iyear 2017
Report Number 20170215
Supplemental Number 36766
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2017-06-18 14:35:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.928433 Google Maps OpenStreetMap
Location Longitude -91.9924 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.55
Recovered Bbls 0.55
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2017-06-18 14:35:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-06-18 14:47:00
Restart Datetime 2017-06-20 18:45:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2017-06-18 16:40:00
On Site Datetime 2017-06-18 15:10:00
Confirmed Discovery Datetime 2017-06-18 16:00:00
Nrc Rpt Datetime 2017-06-18 17:00:00
Nrc Rpt Num 1181516 NRC Report How to search
Additional Nrc Report Numbers 1181753
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2017-06-18 14:47:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2017-06-18 14:47:00
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2017-06-18 14:50:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2017-06-19 17:30:00
Osro Arrived On Site Dt 6/19/2017 8:00
Num Pub Evacuated 0
Pipe Fac Name Erath Ps To Pt. Neches 22"
Segment Name Erath Ps To Lake Arthur Ps 22"
Onshore State Abbreviation La
Onshore Postal Code 70528
Onshore City Name Delcambre
Onshore County Name Vermillion
Designated Location Survey Station No.
Designated Name 6662+53
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 45
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 22
Pipe Wall Thickness 0.312
Pipe Smys 52000
Pipe Specification 5l-X52
Pipe Seam Type Dsaw
Pipe Manufacturer Kaiser Steel Corp
Pipe Coating Type Coal Tar
Coating Applied Ind Yes
Installation Year 1953
Manufactured Year 1953
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 54200
Est Cost Emergency 10000
Est Cost Environmental 0
Est Cost Other 0
Prpty 64200
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 765
Mop Psig 849
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2013-09-16 00:00:00
Maop Reversal Flow Ind Yes
Surge Analysis Date 2013-01-30 00:00:00
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 142822
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controllers actions following a phone call from the public, land owner, were to shut down the pipeline and isolate that section of pipeline. Contacted supervisor and field personnel to investigate situation and make determination.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Field Exam Ind Yes
Failure Type Environmental Cracking-Related
Stress Subtype Other
Stress Details Fatigue Located At The Toe Of The Dsaw Long Seam. Crack At Od 6" Long, Id 1" Long.
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Ultrasonic Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2015
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Previous Year 2013
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Circ Wave Recent Year 2011
Circ Wv Rcnt Propul Method Free Swimming
Circ Wv Rcnt Resolution High Resolution
Ultrasonic Recent Year 2013
Ultrasonic Rcnt Propul Method Free Swimming
Ultrasonic Rcnt Attuned Crack
Geometry Recent Year 2015
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups Inside Ili Cups
Geometry Previous Year 2011
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups Inside Ili Cups
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2013
Hydrtst Most Rcnt Pressure 1126
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R****** K*****
Preparer Title Operations Support Coordinator
Preparer Email R*************@s****.com
Preparer Telephone 832 762 2682
Prepared Date 2022-06-16 00:00:00
Local Contact Name J***** H*****
Local Contact Email J************@s****.com
Local Contact Telephone 4095402781
Authorizer Name D****** P****
Authorizer Telephone 832 762 2553
Authorizer Title Integrity Regulatory Mngr.
Authorizer Email D************@s****.com
Narrative The ndt level ii technician characterized the defect with ut & mt. The ut response indicated ~1" length at the id and mt confirmed an ~ 6" long defect on the od surface. Location of the crack was at the toe of the dsaw long seam of the pipe. A full encirclement type "b" steel steel was welded over the cracked area. 3/1/18 - corrected part a time land owner called in stain on ground, shut down time following notification by land owner.

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