HL incident on 2017-06-01 — AL

Operator
Southern Company Pipelines
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2017-06-01 16:14
Report number
Location
AL
Narrative
Operator personnel was visiting rectifier and noticed small "hissing" sound, and then reported to other, local operating personnel who replaced the safety nut.
Detailed record list
Report Received Date
2017-06-30 00:00:00
Iyear
2017
Report Number
20170206
Supplemental Number
32727
Report Type
Supplemental Final
Operator Id
Name
Southern Company Pipelines
Operator Street Address
3535 Colonnade Parkway Bin S-675-Ec
Operator City Name
Birmingham
Operator State Abbreviation
AL
Operator Postal Code
35243
Local Datetime
2017-06-01 16:14:00
Location Latitude
Location Longitude
-88.77125492
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2017-06-01 16:14:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leaking Valve Was Isolated From Pipeline, Removed, And Replaced.
On Site Datetime
2017-06-01 16:14:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Kemper Co2
Segment Name
Segment 4
Onshore State Abbreviation
Ms
Onshore Postal Code
39307
Onshore City Name
Not Within A Municipality
Onshore County Name
Lauderdale
Designated Location
Milepost/valve Station
Designated Name
Mlv3
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Threaded Safety Nut For Yale Enclosure
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
3
Est Cost Prop Damage
50
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
53
Accident Psig
1900
Mop Psig
2875
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
10
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Very small leak of a threaded safety nut; was replaced soon thereafter.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Safety Nut Appeared To Be Jammed Or Locked In Place.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Safety Nut Appeared To Be Jammed Or Locked In Place.
Preparer Name
J** D*****
Preparer Title
Senior Operations-Compliance Engineer
Preparer Email
J*******@s*********.com
Preparer Telephone
2059926376
Prepared Date
2019-09-19 00:00:00
Authorizer Name
T**** C***
Authorizer Telephone
2059927883
Authorizer Title
Mechanical Support Gm
Authorizer Email
T******@s*********.com
Narrative
Operator personnel was visiting rectifier and noticed small "hissing" sound, and then reported to other, local operating personnel who replaced the safety nut.
Report Received Date 2017-06-30 00:00:00
Iyear 2017
Report Number 20170206
Supplemental Number 32727
Report Type Supplemental Final
Operator Id 31724 PHMSA Enforcement
Name Southern Company Pipelines
Operator Street Address 3535 Colonnade Parkway Bin S-675-Ec
Operator City Name Birmingham
Operator State Abbreviation AL
Operator Postal Code 35243
Local Datetime 2017-06-01 16:14:00
Location Latitude 32.34841735 Google Maps OpenStreetMap
Location Longitude -88.77125492 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 1
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2017-06-01 16:14:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Leaking Valve Was Isolated From Pipeline, Removed, And Replaced.
On Site Datetime 2017-06-01 16:14:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Kemper Co2
Segment Name Segment 4
Onshore State Abbreviation Ms
Onshore Postal Code 39307
Onshore City Name Not Within A Municipality
Onshore County Name Lauderdale
Designated Location Milepost/valve Station
Designated Name Mlv3
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Threaded Safety Nut For Yale Enclosure
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 3
Est Cost Prop Damage 50
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 53
Accident Psig 1900
Mop Psig 2875
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 10
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Very small leak of a threaded safety nut; was replaced soon thereafter.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Safety Nut Appeared To Be Jammed Or Locked In Place.
Eq Additional Other Ind Yes
Eq Additional Other Details Safety Nut Appeared To Be Jammed Or Locked In Place.
Preparer Name J** D*****
Preparer Title Senior Operations-Compliance Engineer
Preparer Email J*******@s*********.com
Preparer Telephone 2059926376
Prepared Date 2019-09-19 00:00:00
Authorizer Name T**** C***
Authorizer Telephone 2059927883
Authorizer Title Mechanical Support Gm
Authorizer Email T******@s*********.com
Narrative Operator personnel was visiting rectifier and noticed small "hissing" sound, and then reported to other, local operating personnel who replaced the safety nut.

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