HL incident on 2017-05-29 — TX

Operator
Enterprise Products Operating Llc
Cause
Other Outside Force Damage
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$600,000
Incident datetime
2017-05-29 15:22
Report number
Location
TX
Narrative
On monday 5/29/17, at 15:22, a contractor was using a track hoe to excavate the east red line at mp 69.6 near parkville, ks. For an integrity assessment (dig #37). The contractor repositioned the track hoe to continue the excavation. The rear of the track hoe sunk into mud that was saturated with water from recent rain.The track-hoe operator then noticed bubbling coming up through the mud and water and he suspected a leak. The operator immediately shut down the track-hoe and exited the equipment. Pipeline control was notified. The nrc was contacted and a 48-hour update was given. On 05/29/17, at 16:00, this pipeline incident was deemed to be reportable to the nrc because it was likely to exceed $50,000 and the call was made to the nrc at 16:35.
Detailed record list
Report Received Date
2017-06-28 00:00:00
Iyear
2017
Report Number
20170203
Supplemental Number
22445
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-05-29 15:22:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
E/p
Unintentional Release Bbls
0.1
Intentional Release Bbls
0
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-05-29 15:22:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-05-22 15:22:00
Restart Datetime
2017-06-07 09:41:00
On Site Datetime
2017-05-29 15:22:00
Nrc Rpt Datetime
2017-05-29 16:35:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
East Leg
Segment Name
Lid 603
Onshore State Abbreviation
Ks
Onshore Postal Code
66846
Onshore City Name
Not Within A Municipality
Onshore County Name
Morris
Designated Location
Milepost/valve Station
Designated Name
69
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10.75
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
X52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
Unknown
Manufactured Year
1970
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
5500
Est Cost Gas Released
3
Est Cost Prop Damage
600000
Est Cost Emergency
1500
Est Cost Environmental
0
Est Cost Other
0
Prpty
607003
Accident Psig
800
Mop Psig
1300
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
59000
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The actions of the control room did not cause this incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
6
Num Contractors Failed
0
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Operator's Contractor
Preparer Name
A***** A*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
A******@e****.com
Preparer Telephone
2818410713
Prepared Date
2017-06-28 00:00:00
Authorizer Name
A***** A*****
Authorizer Telephone
2818410713
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
A******@e****.com
Narrative
On monday 5/29/17, at 15:22, a contractor was using a track hoe to excavate the east red line at mp 69.6 near parkville, ks. For an integrity assessment (dig #37). The contractor repositioned the track hoe to continue the excavation. The rear of the track hoe sunk into mud that was saturated with water from recent rain.The track-hoe operator then noticed bubbling coming up through the mud and water and he suspected a leak. The operator immediately shut down the track-hoe and exited the equipment. Pipeline control was notified. The nrc was contacted and a 48-hour update was given. On 05/29/17, at 16:00, this pipeline incident was deemed to be reportable to the nrc because it was likely to exceed $50,000 and the call was made to the nrc at 16:35.
Report Received Date 2017-06-28 00:00:00
Iyear 2017
Report Number 20170203
Supplemental Number 22445
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-05-29 15:22:00
Location Latitude 38.739998 Google Maps OpenStreetMap
Location Longitude -96.6468 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details E/p
Unintentional Release Bbls 0.1
Intentional Release Bbls 0
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2017-05-29 15:22:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-05-22 15:22:00
Restart Datetime 2017-06-07 09:41:00
On Site Datetime 2017-05-29 15:22:00
Nrc Rpt Datetime 2017-05-29 16:35:00
Nrc Rpt Num 1179662 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name East Leg
Segment Name Lid 603
Onshore State Abbreviation Ks
Onshore Postal Code 66846
Onshore City Name Not Within A Municipality
Onshore County Name Morris
Designated Location Milepost/valve Station
Designated Name 69
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10.75
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification X52
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year Unknown
Manufactured Year 1970
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 5500
Est Cost Gas Released 3
Est Cost Prop Damage 600000
Est Cost Emergency 1500
Est Cost Environmental 0
Est Cost Other 0
Prpty 607003
Accident Psig 800
Mop Psig 1300
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 59000
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The actions of the control room did not cause this incident.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 6
Num Contractors Failed 0
Cause Other Outside Force Damage
Cause Details Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype Operator's Contractor
Preparer Name A***** A*****
Preparer Title Pipeline Compliance Engineer
Preparer Email A******@e****.com
Preparer Telephone 2818410713
Prepared Date 2017-06-28 00:00:00
Authorizer Name A***** A*****
Authorizer Telephone 2818410713
Authorizer Title Pipeline Compliance Engineer
Authorizer Email A******@e****.com
Narrative On monday 5/29/17, at 15:22, a contractor was using a track hoe to excavate the east red line at mp 69.6 near parkville, ks. For an integrity assessment (dig #37). The contractor repositioned the track hoe to continue the excavation. The rear of the track hoe sunk into mud that was saturated with water from recent rain.The track-hoe operator then noticed bubbling coming up through the mud and water and he suspected a leak. The operator immediately shut down the track-hoe and exited the equipment. Pipeline control was notified. The nrc was contacted and a 48-hour update was given. On 05/29/17, at 16:00, this pipeline incident was deemed to be reportable to the nrc because it was likely to exceed $50,000 and the call was made to the nrc at 16:35.

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