HL incident on 2017-05-08 — PA

Operator
Buckeye Partners, Lp
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$452,000
Incident datetime
2017-05-08 10:25
Report number
Location
PA
Narrative
On may 8th, 2017 at 10:00 a.M., buckeye's control center received a phone call from a property owner to report an oil sheen in a drainage ditch. Local operations personnel responded to investigate the report and confirmed a release in a casing running under a roadway. All required notifications were made and the pipeline was shut down and isolated. It was determined that the pipeline release entered a field drain tile which led to the drainage ditch. The pipeline was purged of product and the section of pipe was replaced. The removed portion of pipe was sent for metallurgical analysis. Update: february 27th, 2017, the results from the metallurgical testing indicate that the leak was associated with external pitting corrosion that thinned the wall of the pipe sufficiently allowing for in-service growth of a crack until overload failure of the remaining wall thickness occurred.
Detailed record list
Report Received Date
2017-06-07 00:00:00
Iyear
2017
Report Number
20170184
Supplemental Number
23187
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2017-05-08 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
13
Recovered Bbls
11.8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2017-05-08 10:25:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-05-08 10:31:00
Restart Datetime
2017-05-15 20:49:00
On Site Datetime
2017-05-08 10:25:00
Nrc Rpt Datetime
2017-05-08 11:37:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Wo160eh
Segment Name
Ht160dq
Onshore State Abbreviation
Il
Onshore Postal Code
62573
Onshore City Name
Not Within A Municipality
Onshore County Name
Macon
Designated Location
Survey Station No.
Designated Name
5060+78
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Cased
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
14
Pipe Wall Thickness
0.312
Pipe Smys
42000
Pipe Specification
X42
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
None
Installation Year
1953
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0.5
Rel Water Name
Unnamed Ditch
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
31000
Est Cost Gas Released
1365
Est Cost Prop Damage
452000
Est Cost Emergency
1053000
Est Cost Environmental
185000
Est Cost Other
0
Prpty
1722365
Accident Psig
710
Mop Psig
1162
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
67375
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release volume was too small for the control center to see.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Atmosphere Corrosion Ind
Yes
Other Corrosion Ind
Yes
Corrosion Type Details
Near Neutral Ph Stress Corrosion Cracking
Field Exam Basis Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2016
Close Interval Survey Year
2014
Prior Damage
No
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2013
Geometry Recent Year
2013
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1991
Hydrtst Most Rcnt Pressure
1440
Direct Asmnt Conducted
Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr
2017
Non Destructive Exam Ind
No
Preparer Name
G***** G*****
Preparer Title
District Compliance Specialist
Preparer Email
G******@b******.com
Preparer Telephone
412-716-8250
Preparer Fax
412-264-1433
Prepared Date
2018-02-27 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
6109044113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On may 8th, 2017 at 10:00 a.M., buckeye's control center received a phone call from a property owner to report an oil sheen in a drainage ditch. Local operations personnel responded to investigate the report and confirmed a release in a casing running under a roadway. All required notifications were made and the pipeline was shut down and isolated. It was determined that the pipeline release entered a field drain tile which led to the drainage ditch. The pipeline was purged of product and the section of pipe was replaced. The removed portion of pipe was sent for metallurgical analysis. Update: february 27th, 2017, the results from the metallurgical testing indicate that the leak was associated with external pitting corrosion that thinned the wall of the pipe sufficiently allowing for in-service growth of a crack until overload failure of the remaining wall thickness occurred.
Report Received Date 2017-06-07 00:00:00
Iyear 2017
Report Number 20170184
Supplemental Number 23187
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2017-05-08 10:00:00
Location Latitude 39.918628 Google Maps OpenStreetMap
Location Longitude -89.061751 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 13
Recovered Bbls 11.8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2017-05-08 10:25:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-05-08 10:31:00
Restart Datetime 2017-05-15 20:49:00
On Site Datetime 2017-05-08 10:25:00
Nrc Rpt Datetime 2017-05-08 11:37:00
Nrc Rpt Num 1177755 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Wo160eh
Segment Name Ht160dq
Onshore State Abbreviation Il
Onshore Postal Code 62573
Onshore City Name Not Within A Municipality
Onshore County Name Macon
Designated Location Survey Station No.
Designated Name 5060+78
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing Yes
Road Crossing Ind Yes
Road Type Cased
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 14
Pipe Wall Thickness 0.312
Pipe Smys 42000
Pipe Specification X42
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type None
Installation Year 1953
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 0.5
Rel Water Name Unnamed Ditch
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 31000
Est Cost Gas Released 1365
Est Cost Prop Damage 452000
Est Cost Emergency 1053000
Est Cost Environmental 185000
Est Cost Other 0
Prpty 1722365
Accident Psig 710
Mop Psig 1162
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 67375
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release volume was too small for the control center to see.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Atmosphere Corrosion Ind Yes
Other Corrosion Ind Yes
Corrosion Type Details Near Neutral Ph Stress Corrosion Cracking
Field Exam Basis Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2016
Close Interval Survey Year 2014
Prior Damage No
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2013
Geometry Recent Year 2013
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1991
Hydrtst Most Rcnt Pressure 1440
Direct Asmnt Conducted Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr 2017
Non Destructive Exam Ind No
Preparer Name G***** G*****
Preparer Title District Compliance Specialist
Preparer Email G******@b******.com
Preparer Telephone 412-716-8250
Preparer Fax 412-264-1433
Prepared Date 2018-02-27 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 6109044113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On may 8th, 2017 at 10:00 a.M., buckeye's control center received a phone call from a property owner to report an oil sheen in a drainage ditch. Local operations personnel responded to investigate the report and confirmed a release in a casing running under a roadway. All required notifications were made and the pipeline was shut down and isolated. It was determined that the pipeline release entered a field drain tile which led to the drainage ditch. The pipeline was purged of product and the section of pipe was replaced. The removed portion of pipe was sent for metallurgical analysis. Update: february 27th, 2017, the results from the metallurgical testing indicate that the leak was associated with external pitting corrosion that thinned the wall of the pipe sufficiently allowing for in-service growth of a crack until overload failure of the remaining wall thickness occurred.

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