HL incident on 2017-05-06 — MO

Operator
Laclede Gas Co
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$60,000
Incident datetime
2017-05-06 06:30
Report number
Location
MO
Narrative
Leak on hvl line called in by an outside party at approximately 6:30am on saturday, may 6, 2017. Laclede pipeline personnel on site at approximately 7:30 am; immediately started notification and shutdown procedures. The leak was isolated as soon as possible by closing the nearest upstream and downstream block valves. Discussions between pipeline personnel on site and management determined that this could be a federal reportable accident because potential repair costs could exceed $50,000 at approximately 11:08 am cdt. The nrc was called at 11:39am cdt, nrc incident report #1177602. The nrc was notified that the line had been shut in and the release secured. Also, that the leak site had been cordoned off and would be monitored by pipeline personnel until the line could be isolated and repaired. The 48 hour renotification was made on monday, may 8, 2017 at 11:24 cdt; nrc incident report #1177752. A no change in status was reported. A line purge and repair plan was developed and set into motion on tuesday, may 9, 2017. The leak site was excavated on wednesday, may 10 and the source of the leak was found to be a leaking insulated flange. The leaking flange was cut out on thursday, may 11 and a new spool piece welded in its place. A line refill plan was formalized over the weekend and the line was refilled and returned to service tuesday, may 16. The other eleven (11) buried flanges along the line will be located and a complete evaluation made of their integrity. Mitigative actions will be taken if necessary.
Detailed record list
Report Received Date
2017-06-05 00:00:00
Iyear
2017
Report Number
20170180
Supplemental Number
22441
Report Type
Supplemental Final
Operator Id
Name
Laclede Gas Co
Operator Street Address
700 Market Street
Operator City Name
Saint Louis
Operator State Abbreviation
MO
Operator Postal Code
63101
Local Datetime
2017-05-06 06:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Liquid Propane
Unintentional Release Bbls
1519
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2017-05-06 06:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-05-06 08:00:00
Restart Datetime
2017-05-16 17:17:00
On Site Datetime
2017-05-06 07:30:00
Nrc Rpt Datetime
2017-05-06 11:51:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Laclede Pipeline
Segment Name
Main Line
Onshore State Abbreviation
Il
Onshore Postal Code
62206
Onshore City Name
Sauget
Onshore County Name
St. Clair
Designated Location
Milepost/valve Station
Designated Name
Am 374
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1964
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
26163
Est Cost Prop Damage
60000
Est Cost Emergency
3000
Est Cost Environmental
0
Est Cost Other
0
Prpty
89163
Accident Psig
191
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
16054
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No operational parameters were exceeded
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Preparer Name
K*** A* A***
Preparer Title
Compliance Engineer Iii
Preparer Email
K********@s**********.com
Preparer Telephone
314-349-2925
Prepared Date
2017-06-26 00:00:00
Authorizer Name
C**** R* H********
Authorizer Telephone
314-349-2972
Authorizer Title
Vice President Operations Services
Authorizer Email
C**************@s**********.com
Narrative
Leak on hvl line called in by an outside party at approximately 6:30am on saturday, may 6, 2017. Laclede pipeline personnel on site at approximately 7:30 am; immediately started notification and shutdown procedures. The leak was isolated as soon as possible by closing the nearest upstream and downstream block valves. Discussions between pipeline personnel on site and management determined that this could be a federal reportable accident because potential repair costs could exceed $50,000 at approximately 11:08 am cdt. The nrc was called at 11:39am cdt, nrc incident report #1177602. The nrc was notified that the line had been shut in and the release secured. Also, that the leak site had been cordoned off and would be monitored by pipeline personnel until the line could be isolated and repaired. The 48 hour renotification was made on monday, may 8, 2017 at 11:24 cdt; nrc incident report #1177752. A no change in status was reported. A line purge and repair plan was developed and set into motion on tuesday, may 9, 2017. The leak site was excavated on wednesday, may 10 and the source of the leak was found to be a leaking insulated flange. The leaking flange was cut out on thursday, may 11 and a new spool piece welded in its place. A line refill plan was formalized over the weekend and the line was refilled and returned to service tuesday, may 16. The other eleven (11) buried flanges along the line will be located and a complete evaluation made of their integrity. Mitigative actions will be taken if necessary.
Report Received Date 2017-06-05 00:00:00
Iyear 2017
Report Number 20170180
Supplemental Number 22441
Report Type Supplemental Final
Operator Id 11032 PHMSA Enforcement
Name Laclede Gas Co
Operator Street Address 700 Market Street
Operator City Name Saint Louis
Operator State Abbreviation MO
Operator Postal Code 63101
Local Datetime 2017-05-06 06:30:00
Location Latitude 38.587043 Google Maps OpenStreetMap
Location Longitude -90.18232 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Liquid Propane
Unintentional Release Bbls 1519
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2017-05-06 06:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-05-06 08:00:00
Restart Datetime 2017-05-16 17:17:00
On Site Datetime 2017-05-06 07:30:00
Nrc Rpt Datetime 2017-05-06 11:51:00
Nrc Rpt Num 1177602 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Laclede Pipeline
Segment Name Main Line
Onshore State Abbreviation Il
Onshore Postal Code 62206
Onshore City Name Sauget
Onshore County Name St. Clair
Designated Location Milepost/valve Station
Designated Name Am 374
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1964
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 26163
Est Cost Prop Damage 60000
Est Cost Emergency 3000
Est Cost Environmental 0
Est Cost Other 0
Prpty 89163
Accident Psig 191
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 16054
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No operational parameters were exceeded
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Installation Ind Yes
Preparer Name K*** A* A***
Preparer Title Compliance Engineer Iii
Preparer Email K********@s**********.com
Preparer Telephone 314-349-2925
Prepared Date 2017-06-26 00:00:00
Authorizer Name C**** R* H********
Authorizer Telephone 314-349-2972
Authorizer Title Vice President Operations Services
Authorizer Email C**************@s**********.com
Narrative Leak on hvl line called in by an outside party at approximately 6:30am on saturday, may 6, 2017. Laclede pipeline personnel on site at approximately 7:30 am; immediately started notification and shutdown procedures. The leak was isolated as soon as possible by closing the nearest upstream and downstream block valves. Discussions between pipeline personnel on site and management determined that this could be a federal reportable accident because potential repair costs could exceed $50,000 at approximately 11:08 am cdt. The nrc was called at 11:39am cdt, nrc incident report #1177602. The nrc was notified that the line had been shut in and the release secured. Also, that the leak site had been cordoned off and would be monitored by pipeline personnel until the line could be isolated and repaired. The 48 hour renotification was made on monday, may 8, 2017 at 11:24 cdt; nrc incident report #1177752. A no change in status was reported. A line purge and repair plan was developed and set into motion on tuesday, may 9, 2017. The leak site was excavated on wednesday, may 10 and the source of the leak was found to be a leaking insulated flange. The leaking flange was cut out on thursday, may 11 and a new spool piece welded in its place. A line refill plan was formalized over the weekend and the line was refilled and returned to service tuesday, may 16. The other eleven (11) buried flanges along the line will be located and a complete evaluation made of their integrity. Mitigative actions will be taken if necessary.

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