HL incident on 2017-04-21 — TX

Operator
Plains Pipeline, L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,000
Incident datetime
2017-04-21 21:19
Report number
Location
TX
Narrative
Approximately 347 bbls of crude oil were released from dead leg piping, which was scheduled to be removed 5/1/2017. The crude was observed leaking from the 6 o'clock position as a result of internal corrosion. The pipe has since been replaced. Some crude flowed into a retention pond, but was contained within plains' property. The facility response plan actions were implemented immediately. The national response center was notified and assigned report #1176338. The second nrc notification assigned report #1176384.
Detailed record list
Report Received Date
2017-05-19 00:00:00
Iyear
2017
Report Number
20170168
Supplemental Number
22346
Report Type
Original Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-04-21 21:19:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
347
Recovered Bbls
347
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2017-04-21 21:19:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Line Had Already Been Shut Down.
On Site Datetime
2017-04-21 21:19:00
Nrc Rpt Datetime
2017-04-21 21:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lumberton Station
Segment Name
Station Piping
Onshore State Abbreviation
Ms
Onshore Postal Code
39455
Onshore City Name
Lumberton
Onshore County Name
Lamar
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.322
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Other
Pipe Seam Details
Not Applicable As This Was In A Pipe Fitting T.
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
341
Rel Water Name
Containment Pond On Company Facility
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
250
Est Cost Prop Damage
3000
Est Cost Emergency
65000
Est Cost Environmental
0
Est Cost Other
0
Prpty
68250
Accident Psig
606
Mop Psig
883
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C******* C*****
Preparer Title
Compliance Specialist
Preparer Email
C*******@p****.com
Preparer Telephone
713-993-5080
Prepared Date
2017-05-19 00:00:00
Authorizer Name
T***** M*****
Authorizer Telephone
713-646-4109
Authorizer Title
Sr Dir Environmental And Regulatory Compliance
Authorizer Email
T*******@p****.com
Narrative
Approximately 347 bbls of crude oil were released from dead leg piping, which was scheduled to be removed 5/1/2017. The crude was observed leaking from the 6 o'clock position as a result of internal corrosion. The pipe has since been replaced. Some crude flowed into a retention pond, but was contained within plains' property. The facility response plan actions were implemented immediately. The national response center was notified and assigned report #1176338. The second nrc notification assigned report #1176384.
Report Received Date 2017-05-19 00:00:00
Iyear 2017
Report Number 20170168
Supplemental Number 22346
Report Type Original Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-04-21 21:19:00
Location Latitude 31.03428 Google Maps OpenStreetMap
Location Longitude -89.44975 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 347
Recovered Bbls 347
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2017-04-21 21:19:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Line Had Already Been Shut Down.
On Site Datetime 2017-04-21 21:19:00
Nrc Rpt Datetime 2017-04-21 21:30:00
Nrc Rpt Num 1176338 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lumberton Station
Segment Name Station Piping
Onshore State Abbreviation Ms
Onshore Postal Code 39455
Onshore City Name Lumberton
Onshore County Name Lamar
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.322
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Other
Pipe Seam Details Not Applicable As This Was In A Pipe Fitting T.
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 341
Rel Water Name Containment Pond On Company Facility
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 250
Est Cost Prop Damage 3000
Est Cost Emergency 65000
Est Cost Environmental 0
Est Cost Other 0
Prpty 68250
Accident Psig 606
Mop Psig 883
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C******* C*****
Preparer Title Compliance Specialist
Preparer Email C*******@p****.com
Preparer Telephone 713-993-5080
Prepared Date 2017-05-19 00:00:00
Authorizer Name T***** M*****
Authorizer Telephone 713-646-4109
Authorizer Title Sr Dir Environmental And Regulatory Compliance
Authorizer Email T*******@p****.com
Narrative Approximately 347 bbls of crude oil were released from dead leg piping, which was scheduled to be removed 5/1/2017. The crude was observed leaking from the 6 o'clock position as a result of internal corrosion. The pipe has since been replaced. Some crude flowed into a retention pond, but was contained within plains' property. The facility response plan actions were implemented immediately. The national response center was notified and assigned report #1176338. The second nrc notification assigned report #1176384.

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