HL incident on 2017-04-21 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$7,500
Incident datetime
2017-04-21 13:00
Report number
Location
TX
Narrative
On 04/21/2017 at approximately 1300 a pipeline technician was completing work on the station sump for lawson jct. At that time a 1" nipple broke causing a release of 4 barrels. The line was immediately shutdown and the leak isolated. Clean-up is complete and a new nipple has been installed. A different style sump pump has been installed to reduce the potential for future vibration events.
Detailed record list
Report Received Date
2017-05-12 00:00:00
Iyear
2017
Report Number
20170160
Supplemental Number
22326
Report Type
Original Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-04-21 13:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-04-21 13:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-04-21 13:00:00
Restart Datetime
2017-04-21 14:30:00
On Site Datetime
2017-04-21 13:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lawson Jct
Segment Name
Lawson Jct
Onshore State Abbreviation
Tx
Onshore Postal Code
79741
Onshore City Name
Goldsmith
Onshore County Name
Ector
Designated Location
Milepost/valve Station
Designated Name
Lawson
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Nipple
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
7500
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
7650
Accident Psig
375
Mop Psig
1318
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Pipe Nipple
Additional Vibration Ind
Yes
Preparer Name
C**** A******
Preparer Email
C*******@e****.com
Preparer Telephone
713-381-6426
Prepared Date
2017-05-12 00:00:00
Authorizer Name
C**** A******
Authorizer Telephone
713-381-6426
Authorizer Title
Pipeline Compliance
Authorizer Email
C*******@e****.com
Narrative
On 04/21/2017 at approximately 1300 a pipeline technician was completing work on the station sump for lawson jct. At that time a 1" nipple broke causing a release of 4 barrels. The line was immediately shutdown and the leak isolated. Clean-up is complete and a new nipple has been installed. A different style sump pump has been installed to reduce the potential for future vibration events.
Report Received Date 2017-05-12 00:00:00
Iyear 2017
Report Number 20170160
Supplemental Number 22326
Report Type Original Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-04-21 13:00:00
Location Latitude 31.8998 Google Maps OpenStreetMap
Location Longitude -102.6292 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3
Recovered Bbls 3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-04-21 13:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-04-21 13:00:00
Restart Datetime 2017-04-21 14:30:00
On Site Datetime 2017-04-21 13:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lawson Jct
Segment Name Lawson Jct
Onshore State Abbreviation Tx
Onshore Postal Code 79741
Onshore City Name Goldsmith
Onshore County Name Ector
Designated Location Milepost/valve Station
Designated Name Lawson
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Nipple
Installation Year 2015
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 150
Est Cost Prop Damage 7500
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 7650
Accident Psig 375
Mop Psig 1318
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Pipe Nipple
Additional Vibration Ind Yes
Preparer Name C**** A******
Preparer Email C*******@e****.com
Preparer Telephone 713-381-6426
Prepared Date 2017-05-12 00:00:00
Authorizer Name C**** A******
Authorizer Telephone 713-381-6426
Authorizer Title Pipeline Compliance
Authorizer Email C*******@e****.com
Narrative On 04/21/2017 at approximately 1300 a pipeline technician was completing work on the station sump for lawson jct. At that time a 1" nipple broke causing a release of 4 barrels. The line was immediately shutdown and the leak isolated. Clean-up is complete and a new nipple has been installed. A different style sump pump has been installed to reduce the potential for future vibration events.

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