Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2017-04-13 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,000
Incident datetime
2017-04-13 13:30
Report number
Location
TX
Narrative
Enterprise employee discovered the tank mixer seal leaking on tank #2568 at healdton station. 0.2 barrels of crude oil released. 10' x 15' area of contaminated soil. All contamination contained inside dike area. The mixer seal has been replaced.
Detailed record list
Report Received Date
2017-05-10 00:00:00
Iyear
2017
Report Number
20170158
Supplemental Number
22323
Report Type
Original Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-04-13 13:30:00
Location Latitude
34.2374
Location Longitude
-97.4937
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-04-13 13:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Facility Was Not Shut Down As The Leak Was On A Mixer And Contained.
On Site Datetime
2017-04-13 13:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Healdton
Segment Name
Tank 2568
Onshore State Abbreviation
Ok
Onshore Postal Code
73438
Onshore City Name
Healdton
Onshore County Name
Carter
Designated Location
Survey Station No.
Designated Name
See Lat-Lon
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Tank Type
Atmospheric
Item Involved Details
Mixer
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Rubber
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
5
Est Cost Prop Damage
1000
Est Cost Emergency
1000
Est Cost Environmental
1000
Est Cost Other
0
Prpty
3005
Accident Psig
4
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Mixer seal failure is not attributable to the pipeline control center operators.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear And Tear
Preparer Name
A***** A*****
Preparer Email
A******@e****.com
Preparer Telephone
713-281-4218
Prepared Date
2017-05-10 00:00:00
Authorizer Name
A***** A*****
Authorizer Telephone
713-281-4218
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
A******@e****.com
Narrative
Enterprise employee discovered the tank mixer seal leaking on tank #2568 at healdton station. 0.2 barrels of crude oil released. 10' x 15' area of contaminated soil. All contamination contained inside dike area. The mixer seal has been replaced.
| Report Received Date | 2017-05-10 00:00:00 |
|---|---|
| Iyear | 2017 |
| Report Number | 20170158 |
| Supplemental Number | 22323 |
| Report Type | Original Final |
| Operator Id | 30829 PHMSA Enforcement |
| Name | Enterprise Crude Pipeline Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2017-04-13 13:30:00 |
| Location Latitude | 34.2374 Google Maps OpenStreetMap |
| Location Longitude | -97.4937 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.2 |
| Recovered Bbls | 0.2 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2017-04-13 13:30:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Pipeline Facility Was Not Shut Down As The Leak Was On A Mixer And Contained. |
| On Site Datetime | 2017-04-13 13:30:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Healdton |
| Segment Name | Tank 2568 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 73438 |
| Onshore City Name | Healdton |
| Onshore County Name | Carter |
| Designated Location | Survey Station No. |
| Designated Name | See Lat-Lon |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Other |
| Tank Type | Atmospheric |
| Item Involved Details | Mixer |
| Installation Year | Unknown |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Rubber |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 5 |
| Est Cost Prop Damage | 1000 |
| Est Cost Emergency | 1000 |
| Est Cost Environmental | 1000 |
| Est Cost Other | 0 |
| Prpty | 3005 |
| Accident Psig | 4 |
| Mop Psig | 720 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Gathering |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Mixer seal failure is not attributable to the pipeline control center operators. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Seal (Not Pump Seal) Or Packing |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Normal Wear And Tear |
| Preparer Name | A***** A***** |
| Preparer Email | A******@e****.com |
| Preparer Telephone | 713-281-4218 |
| Prepared Date | 2017-05-10 00:00:00 |
| Authorizer Name | A***** A***** |
| Authorizer Telephone | 713-281-4218 |
| Authorizer Title | Pipeline Compliance Engineer |
| Authorizer Email | A******@e****.com |
| Narrative | Enterprise employee discovered the tank mixer seal leaking on tank #2568 at healdton station. 0.2 barrels of crude oil released. 10' x 15' area of contaminated soil. All contamination contained inside dike area. The mixer seal has been replaced. |
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