HL incident on 2017-04-10 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$23,025
Incident datetime
2017-04-10 17:05
Report number
Location
OK
Narrative
On 4/10/2017, while marking the oneok artesia lateral for an upcoming internal inspection tool run, oneok contractors identified frost on the ground above the pipeline. Oneok field operations personnel were notified and confirmed the leak to be over the oneok pipeline. Pipeline was shut down and excavated exposing an ice ball on the pipe. Pipeline was purged of hydrocarbons and section of pipe was removed and replaced with previously tested pipe. The pipeline was returned to full operations at 15:30 on 4/13/2017. Field examination identified a pinhole in the pipe had occurred due to corrosion.
Detailed record list
Report Received Date
2017-05-09 00:00:00
Iyear
2017
Report Number
20170157
Supplemental Number
22322
Report Type
Original Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2017-04-10 17:05:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
3
Intentional Release Bbls
1000
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-04-10 17:05:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-04-11 10:00:00
Restart Datetime
2017-04-13 15:30:00
On Site Datetime
2017-04-10 17:05:00
Nrc Rpt Datetime
2017-04-10 18:00:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Oneok Artesia Lateral
Segment Name
Oneok Artesia Lateral Index Number 20490
Onshore State Abbreviation
Nm
Onshore Postal Code
88210
Onshore City Name
Not Within A Municipality
Onshore County Name
Eddy
Designated Location
Survey Station No.
Designated Name
4115+36
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6.625
Pipe Wall Thickness
0.156
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Cold Applied Tape
Installation Year
1960
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
40163
Est Cost Prop Damage
23025
Est Cost Emergency
5000
Est Cost Environmental
3000
Est Cost Other
0
Prpty
71188
Accident Psig
661
Mop Psig
1250
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
32736
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place prior to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2016
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2013
Geometry Recent Year
2013
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
N*** J****
Preparer Title
Requlatory Compliance Supervisor
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2017-05-09 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
N*********@o****.com
Narrative
On 4/10/2017, while marking the oneok artesia lateral for an upcoming internal inspection tool run, oneok contractors identified frost on the ground above the pipeline. Oneok field operations personnel were notified and confirmed the leak to be over the oneok pipeline. Pipeline was shut down and excavated exposing an ice ball on the pipe. Pipeline was purged of hydrocarbons and section of pipe was removed and replaced with previously tested pipe. The pipeline was returned to full operations at 15:30 on 4/13/2017. Field examination identified a pinhole in the pipe had occurred due to corrosion.
Report Received Date 2017-05-09 00:00:00
Iyear 2017
Report Number 20170157
Supplemental Number 22322
Report Type Original Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2017-04-10 17:05:00
Location Latitude 32.778539 Google Maps OpenStreetMap
Location Longitude -104.243318 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 3
Intentional Release Bbls 1000
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2017-04-10 17:05:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-04-11 10:00:00
Restart Datetime 2017-04-13 15:30:00
On Site Datetime 2017-04-10 17:05:00
Nrc Rpt Datetime 2017-04-10 18:00:00
Nrc Rpt Num 1175369 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Oneok Artesia Lateral
Segment Name Oneok Artesia Lateral Index Number 20490
Onshore State Abbreviation Nm
Onshore Postal Code 88210
Onshore City Name Not Within A Municipality
Onshore County Name Eddy
Designated Location Survey Station No.
Designated Name 4115+36
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6.625
Pipe Wall Thickness 0.156
Pipe Smys 42000
Pipe Specification Api 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Cold Applied Tape
Installation Year 1960
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 40163
Est Cost Prop Damage 23025
Est Cost Emergency 5000
Est Cost Environmental 3000
Est Cost Other 0
Prpty 71188
Accident Psig 661
Mop Psig 1250
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 32736
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had taken place prior to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2016
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2013
Geometry Recent Year 2013
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name N*** J****
Preparer Title Requlatory Compliance Supervisor
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2017-05-09 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email N*********@o****.com
Narrative On 4/10/2017, while marking the oneok artesia lateral for an upcoming internal inspection tool run, oneok contractors identified frost on the ground above the pipeline. Oneok field operations personnel were notified and confirmed the leak to be over the oneok pipeline. Pipeline was shut down and excavated exposing an ice ball on the pipe. Pipeline was purged of hydrocarbons and section of pipe was removed and replaced with previously tested pipe. The pipeline was returned to full operations at 15:30 on 4/13/2017. Field examination identified a pinhole in the pipe had occurred due to corrosion.

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