HL incident on 2017-04-07 — AL

Operator
Southern Company Pipelines
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$13,110
Incident datetime
2017-04-07 15:13
Report number
Location
AL
Narrative
Operator employee found leaking plug valve body about 3" above the grease fitting. Operator employee isolated the leaking plug valve. Operator employee reported the leak as greater than 5 gallons to management. The following day, leaking plug valve was replaced.
Detailed record list
Report Received Date
2017-05-07 00:00:00
Iyear
2017
Report Number
20170154
Supplemental Number
32723
Report Type
Supplemental Final
Operator Id
Name
Southern Company Pipelines
Operator Street Address
3535 Colonnade Parkway Bin S-675-Ec
Operator City Name
Birmingham
Operator State Abbreviation
AL
Operator Postal Code
35243
Local Datetime
2017-04-07 15:13:00
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
1
Intentional Release Bbls
1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-04-07 15:13:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Isolated And Removed From Service Without Disrupting Mainline Flow.
On Site Datetime
2017-04-07 15:13:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Kemper Co2
Segment Name
Segment 3
Onshore State Abbreviation
Ms
Onshore Postal Code
39307
Onshore City Name
Meridian
Onshore County Name
Lauderdale
Designated Location
Milepost/valve Station
Designated Name
Mlv3
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
6
Est Cost Prop Damage
13110
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
13116
Accident Psig
1500
Mop Psig
2875
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
15
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The fact that this was a leak from the body of a plug valve.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Additional Defect Ind
Yes
Preparer Name
J** D*****
Preparer Title
Senior Operations-Compliance Engineer
Preparer Email
J*******@s*********.com
Preparer Telephone
2059926376
Prepared Date
2019-09-19 00:00:00
Authorizer Name
H***** I***
Authorizer Telephone
2059926553
Authorizer Title
Vp Technical Services
Authorizer Email
H*****@s*********.com
Narrative
Operator employee found leaking plug valve body about 3" above the grease fitting. Operator employee isolated the leaking plug valve. Operator employee reported the leak as greater than 5 gallons to management. The following day, leaking plug valve was replaced.
Report Received Date 2017-05-07 00:00:00
Iyear 2017
Report Number 20170154
Supplemental Number 32723
Report Type Supplemental Final
Operator Id 31724 PHMSA Enforcement
Name Southern Company Pipelines
Operator Street Address 3535 Colonnade Parkway Bin S-675-Ec
Operator City Name Birmingham
Operator State Abbreviation AL
Operator Postal Code 35243
Local Datetime 2017-04-07 15:13:00
Location Latitude 32.348372 Google Maps OpenStreetMap
Location Longitude -88.771227 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 1
Intentional Release Bbls 1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-04-07 15:13:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Valve Isolated And Removed From Service Without Disrupting Mainline Flow.
On Site Datetime 2017-04-07 15:13:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Kemper Co2
Segment Name Segment 3
Onshore State Abbreviation Ms
Onshore Postal Code 39307
Onshore City Name Meridian
Onshore County Name Lauderdale
Designated Location Milepost/valve Station
Designated Name Mlv3
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 6
Est Cost Prop Damage 13110
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 13116
Accident Psig 1500
Mop Psig 2875
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 15
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The fact that this was a leak from the body of a plug valve.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Additional Defect Ind Yes
Preparer Name J** D*****
Preparer Title Senior Operations-Compliance Engineer
Preparer Email J*******@s*********.com
Preparer Telephone 2059926376
Prepared Date 2019-09-19 00:00:00
Authorizer Name H***** I***
Authorizer Telephone 2059926553
Authorizer Title Vp Technical Services
Authorizer Email H*****@s*********.com
Narrative Operator employee found leaking plug valve body about 3" above the grease fitting. Operator employee isolated the leaking plug valve. Operator employee reported the leak as greater than 5 gallons to management. The following day, leaking plug valve was replaced.

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