HL incident on 2017-04-11 — TX

Operator
Stateline Crude, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-04-11 06:00
Report number
Location
TX
Narrative
This incident was caused by equipment failure. Transfer pump failed due to power outage which resulted in overfilling the breakout tanks. Approximately 25 bbls of crude was spilled inside lined spcc berm. The lined containment allowed for a 100% recovery of spilled fluids. This spill did not impact the environment. Corrective actions: 1. Lined containment and tanks were pressure washed; all fluids were recovered and disposed 2. Transfer pump was repaired and additional 40 horsepower pump was installed 3. Backup power generator was installed 4. Wpx is planning to install four additional 500 bbl tanks to increase the storage volume
Detailed record list
Report Received Date
2017-05-05 00:00:00
Iyear
2017
Report Number
20170152
Supplemental Number
22325
Report Type
Supplemental Final
Operator Id
Name
Stateline Crude, Llc
Operator Street Address
16211 La Cantera Parkway Suite 202
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78256
Local Datetime
2017-04-11 06:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
25
Recovered Bbls
25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-04-11 06:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-04-11 06:00:00
Restart Datetime
2017-04-11 14:30:00
On Site Datetime
2017-04-11 06:30:00
Nrc Rpt Datetime
2017-04-12 13:36:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
20 Acre Oil Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
79754-0000
Onshore City Name
Not Within A Municipality
Onshore County Name
Loving
Designated Location
Survey Station No.
Designated Name
T. & P. Rr. C
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
803
Est Cost Other Details
Spilled Crude Oil Recovery And Pressure Washing Tanks And Lined Containment.
Prpty
803
Accident Psig
0.5
Mop Psig
1
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Other
Other Pump Details
Electrical
Additional Electricity Ind
Yes
Preparer Name
K******* B*****
Preparer Title
Environmental Specialist
Preparer Email
K**************@w********.com
Preparer Telephone
9705890743
Preparer Fax
5758853509
Prepared Date
2017-05-11 00:00:00
Authorizer Name
L**** S****
Authorizer Telephone
817-727-9716
Authorizer Title
Hse Manager
Authorizer Email
L**********@w********.com
Narrative
This incident was caused by equipment failure. Transfer pump failed due to power outage which resulted in overfilling the breakout tanks. Approximately 25 bbls of crude was spilled inside lined spcc berm. The lined containment allowed for a 100% recovery of spilled fluids. This spill did not impact the environment. Corrective actions: 1. Lined containment and tanks were pressure washed; all fluids were recovered and disposed 2. Transfer pump was repaired and additional 40 horsepower pump was installed 3. Backup power generator was installed 4. Wpx is planning to install four additional 500 bbl tanks to increase the storage volume
Report Received Date 2017-05-05 00:00:00
Iyear 2017
Report Number 20170152
Supplemental Number 22325
Report Type Supplemental Final
Operator Id 39589 PHMSA Enforcement
Name Stateline Crude, Llc
Operator Street Address 16211 La Cantera Parkway Suite 202
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78256
Local Datetime 2017-04-11 06:00:00
Location Latitude 31.972507 Google Maps OpenStreetMap
Location Longitude -103.750274 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 25
Recovered Bbls 25
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2017-04-11 06:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-04-11 06:00:00
Restart Datetime 2017-04-11 14:30:00
On Site Datetime 2017-04-11 06:30:00
Nrc Rpt Datetime 2017-04-12 13:36:00
Nrc Rpt Num 1175545 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 20 Acre Oil Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 79754-0000
Onshore City Name Not Within A Municipality
Onshore County Name Loving
Designated Location Survey Station No.
Designated Name T. & P. Rr. C
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Single Bottom System
Tank Type Atmospheric
Installation Year 2016
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 803
Est Cost Other Details Spilled Crude Oil Recovery And Pressure Washing Tanks And Lined Containment.
Prpty 803
Accident Psig 0.5
Mop Psig 1
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Other
Other Pump Details Electrical
Additional Electricity Ind Yes
Preparer Name K******* B*****
Preparer Title Environmental Specialist
Preparer Email K**************@w********.com
Preparer Telephone 9705890743
Preparer Fax 5758853509
Prepared Date 2017-05-11 00:00:00
Authorizer Name L**** S****
Authorizer Telephone 817-727-9716
Authorizer Title Hse Manager
Authorizer Email L**********@w********.com
Narrative This incident was caused by equipment failure. Transfer pump failed due to power outage which resulted in overfilling the breakout tanks. Approximately 25 bbls of crude was spilled inside lined spcc berm. The lined containment allowed for a 100% recovery of spilled fluids. This spill did not impact the environment. Corrective actions: 1. Lined containment and tanks were pressure washed; all fluids were recovered and disposed 2. Transfer pump was repaired and additional 40 horsepower pump was installed 3. Backup power generator was installed 4. Wpx is planning to install four additional 500 bbl tanks to increase the storage volume

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