Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2017-04-11 — TX
Operator
Stateline Crude, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2017-04-11 06:00
Report number
Location
TX
Narrative
This incident was caused by equipment failure. Transfer pump failed due to power outage which resulted in overfilling the breakout tanks. Approximately 25 bbls of crude was spilled inside lined spcc berm. The lined containment allowed for a 100% recovery of spilled fluids. This spill did not impact the environment. Corrective actions: 1. Lined containment and tanks were pressure washed; all fluids were recovered and disposed 2. Transfer pump was repaired and additional 40 horsepower pump was installed 3. Backup power generator was installed 4. Wpx is planning to install four additional 500 bbl tanks to increase the storage volume
Detailed record list
Report Received Date
2017-05-05 00:00:00
Iyear
2017
Report Number
20170152
Supplemental Number
22325
Report Type
Supplemental Final
Operator Id
39589
Name
Stateline Crude, Llc
Operator Street Address
16211 La Cantera Parkway Suite 202
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78256
Local Datetime
2017-04-11 06:00:00
Location Latitude
31.972507
Location Longitude
-103.750274
Commodity Released Type
Crude Oil
Unintentional Release Bbls
25
Recovered Bbls
25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-04-11 06:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-04-11 06:00:00
Restart Datetime
2017-04-11 14:30:00
On Site Datetime
2017-04-11 06:30:00
Nrc Rpt Datetime
2017-04-12 13:36:00
Nrc Rpt Num
1175545
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
20 Acre Oil Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
79754-0000
Onshore City Name
Not Within A Municipality
Onshore County Name
Loving
Designated Location
Survey Station No.
Designated Name
T. & P. Rr. C
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
803
Est Cost Other Details
Spilled Crude Oil Recovery And Pressure Washing Tanks And Lined Containment.
Prpty
803
Accident Psig
0.5
Mop Psig
1
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Other
Other Pump Details
Electrical
Additional Electricity Ind
Yes
Preparer Name
K******* B*****
Preparer Title
Environmental Specialist
Preparer Email
K**************@w********.com
Preparer Telephone
9705890743
Preparer Fax
5758853509
Prepared Date
2017-05-11 00:00:00
Authorizer Name
L**** S****
Authorizer Telephone
817-727-9716
Authorizer Title
Hse Manager
Authorizer Email
L**********@w********.com
Narrative
This incident was caused by equipment failure. Transfer pump failed due to power outage which resulted in overfilling the breakout tanks. Approximately 25 bbls of crude was spilled inside lined spcc berm. The lined containment allowed for a 100% recovery of spilled fluids. This spill did not impact the environment. Corrective actions: 1. Lined containment and tanks were pressure washed; all fluids were recovered and disposed 2. Transfer pump was repaired and additional 40 horsepower pump was installed 3. Backup power generator was installed 4. Wpx is planning to install four additional 500 bbl tanks to increase the storage volume
| Report Received Date | 2017-05-05 00:00:00 |
|---|---|
| Iyear | 2017 |
| Report Number | 20170152 |
| Supplemental Number | 22325 |
| Report Type | Supplemental Final |
| Operator Id | 39589 PHMSA Enforcement |
| Name | Stateline Crude, Llc |
| Operator Street Address | 16211 La Cantera Parkway Suite 202 |
| Operator City Name | San Antonio |
| Operator State Abbreviation | TX |
| Operator Postal Code | 78256 |
| Local Datetime | 2017-04-11 06:00:00 |
| Location Latitude | 31.972507 Google Maps OpenStreetMap |
| Location Longitude | -103.750274 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 25 |
| Recovered Bbls | 25 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Contractor Working For The Operator |
| Incident Identified Datetime | 2017-04-11 06:00:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2017-04-11 06:00:00 |
| Restart Datetime | 2017-04-11 14:30:00 |
| On Site Datetime | 2017-04-11 06:30:00 |
| Nrc Rpt Datetime | 2017-04-12 13:36:00 |
| Nrc Rpt Num | 1175545 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | 20 Acre Oil Terminal |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 79754-0000 |
| Onshore City Name | Not Within A Municipality |
| Onshore County Name | Loving |
| Designated Location | Survey Station No. |
| Designated Name | T. & P. Rr. C |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Tank/vessel |
| Tank Vessel Subtype | Single Bottom System |
| Tank Type | Atmospheric |
| Installation Year | 2016 |
| Material Involved | Carbon Steel |
| Release Type | Overfill Or Overflow |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 803 |
| Est Cost Other Details | Spilled Crude Oil Recovery And Pressure Washing Tanks And Lined Containment. |
| Prpty | 803 |
| Accident Psig | 0.5 |
| Mop Psig | 1 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Other Pump Ind | Other |
| Other Pump Details | Electrical |
| Additional Electricity Ind | Yes |
| Preparer Name | K******* B***** |
| Preparer Title | Environmental Specialist |
| Preparer Email | K**************@w********.com |
| Preparer Telephone | 9705890743 |
| Preparer Fax | 5758853509 |
| Prepared Date | 2017-05-11 00:00:00 |
| Authorizer Name | L**** S**** |
| Authorizer Telephone | 817-727-9716 |
| Authorizer Title | Hse Manager |
| Authorizer Email | L**********@w********.com |
| Narrative | This incident was caused by equipment failure. Transfer pump failed due to power outage which resulted in overfilling the breakout tanks. Approximately 25 bbls of crude was spilled inside lined spcc berm. The lined containment allowed for a 100% recovery of spilled fluids. This spill did not impact the environment. Corrective actions: 1. Lined containment and tanks were pressure washed; all fluids were recovered and disposed 2. Transfer pump was repaired and additional 40 horsepower pump was installed 3. Backup power generator was installed 4. Wpx is planning to install four additional 500 bbl tanks to increase the storage volume |
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