HL incident on 2017-04-05 — TX

Operator
Enterprise Products Operating Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$30,000
Incident datetime
2017-04-05 17:26
Report number
Location
TX
Narrative
At 17:26 on 4/5/2017 an aerial patrol noticed dead vegetation over enterprise's quanah pipeline. The same day at 19:00 an employee was dispatched to the site and did not see or smell any vapors. On 4/8 an employee was dispatched again and detected lel readings, indicating a leak on enterprise's pipeline. Approximately 1 bbl was estimated to have been released. The line was shut down and blocked in at 22:00 on 4/8. The site was excavated and a pinhole leak in the pipe seam was discovered. A sleeve was installed over the leak and the pipeline resumed operation at 17:00 on 4/11. At 21:49 on 4/8 it was expected that the total cost would exceed $50,000, necessitating the nrc call made at 22:17. 3/8/18: updated accident time and closed report. 7/3/2018: updated report and submitted final.
Detailed record list
Report Received Date
2017-05-03 00:00:00
Iyear
2017
Report Number
20170143
Supplemental Number
30584
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-04-05 17:26:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-04-05 17:26:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-04-08 22:00:00
Restart Datetime
2017-04-11 17:03:00
On Site Datetime
2017-04-05 19:00:00
Nrc Rpt Datetime
2017-04-08 22:17:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Sonora To Roberts Ranch
Segment Name
C82
Onshore State Abbreviation
Tx
Onshore Postal Code
76932
Onshore City Name
Stiles
Onshore County Name
Reagan
Designated Location
Milepost/valve Station
Designated Name
Mp 91.5
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
8
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
Api 5-L-X-52
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Us Steel
Pipe Coating Type
Other
Pipe Coating Details
Polyken Tape
Installation Year
1977
Manufactured Year
1977
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
30000
Est Cost Emergency
1000
Est Cost Environmental
8000
Est Cost Other
0
Prpty
39100
Accident Psig
938
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
53008
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller was not a contributing factor to the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Field Examination Revealed Pinhole Leak On Pipe Seam.
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2012
Geometry Recent Year
2012
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R****** R*****
Preparer Title
Sr. Pipeline Compliance Engineer
Preparer Email
R*******@e****.com
Preparer Telephone
713-381-6841
Prepared Date
2018-07-03 00:00:00
Authorizer Name
R****** R*****
Authorizer Telephone
713-381-6841
Authorizer Title
Sr. Pipeline Compliance Engineer
Authorizer Email
R*******@e****.com
Narrative
At 17:26 on 4/5/2017 an aerial patrol noticed dead vegetation over enterprise's quanah pipeline. The same day at 19:00 an employee was dispatched to the site and did not see or smell any vapors. On 4/8 an employee was dispatched again and detected lel readings, indicating a leak on enterprise's pipeline. Approximately 1 bbl was estimated to have been released. The line was shut down and blocked in at 22:00 on 4/8. The site was excavated and a pinhole leak in the pipe seam was discovered. A sleeve was installed over the leak and the pipeline resumed operation at 17:00 on 4/11. At 21:49 on 4/8 it was expected that the total cost would exceed $50,000, necessitating the nrc call made at 22:17. 3/8/18: updated accident time and closed report. 7/3/2018: updated report and submitted final.
Report Received Date 2017-05-03 00:00:00
Iyear 2017
Report Number 20170143
Supplemental Number 30584
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-04-05 17:26:00
Location Latitude 31.521032 Google Maps OpenStreetMap
Location Longitude -101.545231 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 1
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2017-04-05 17:26:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-04-08 22:00:00
Restart Datetime 2017-04-11 17:03:00
On Site Datetime 2017-04-05 19:00:00
Nrc Rpt Datetime 2017-04-08 22:17:00
Nrc Rpt Num 1175193 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Sonora To Roberts Ranch
Segment Name C82
Onshore State Abbreviation Tx
Onshore Postal Code 76932
Onshore City Name Stiles
Onshore County Name Reagan
Designated Location Milepost/valve Station
Designated Name Mp 91.5
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 8
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification Api 5-L-X-52
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Us Steel
Pipe Coating Type Other
Pipe Coating Details Polyken Tape
Installation Year 1977
Manufactured Year 1977
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 30000
Est Cost Emergency 1000
Est Cost Environmental 8000
Est Cost Other 0
Prpty 39100
Accident Psig 938
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 53008
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller was not a contributing factor to the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Field Examination Revealed Pinhole Leak On Pipe Seam.
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2012
Geometry Recent Year 2012
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R****** R*****
Preparer Title Sr. Pipeline Compliance Engineer
Preparer Email R*******@e****.com
Preparer Telephone 713-381-6841
Prepared Date 2018-07-03 00:00:00
Authorizer Name R****** R*****
Authorizer Telephone 713-381-6841
Authorizer Title Sr. Pipeline Compliance Engineer
Authorizer Email R*******@e****.com
Narrative At 17:26 on 4/5/2017 an aerial patrol noticed dead vegetation over enterprise's quanah pipeline. The same day at 19:00 an employee was dispatched to the site and did not see or smell any vapors. On 4/8 an employee was dispatched again and detected lel readings, indicating a leak on enterprise's pipeline. Approximately 1 bbl was estimated to have been released. The line was shut down and blocked in at 22:00 on 4/8. The site was excavated and a pinhole leak in the pipe seam was discovered. A sleeve was installed over the leak and the pipeline resumed operation at 17:00 on 4/11. At 21:49 on 4/8 it was expected that the total cost would exceed $50,000, necessitating the nrc call made at 22:17. 3/8/18: updated accident time and closed report. 7/3/2018: updated report and submitted final.

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