HL incident on 2017-04-03 — WY

Operator
Express Holdings (Usa), Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,803
Incident datetime
2017-04-03 07:00
Report number
Location
WY
Narrative
At approximately 7:00 a.M. Mst on april 3, 2017, a company employee was conducting a routine maintenance check of the tank farm and discovered petroleum crude oil outside of tank number 501. Upon discovery of the release, the employee identified that 0708-tank mixer on tank number 501 was the source for the leak. The tank mixer was immediate turned off and locked out. At the time of discovery, it was conservatively estimated the total release was less than 1 barrel and the spill was contained in the dike. It was estimated 0.5 barrel of oil was recovered and the other half was part of contaminated rock and soil that was hauled off and disposed by environmental services. The leak did not meet the nrc notification criteria so no notification was made. A courtesy call was made to PHMSA western region. As a result of the investigation, it was determined the leak on the mixer was due to normal wear and tear on the seal.
Detailed record list
Report Received Date
2017-05-01 00:00:00
Iyear
2017
Report Number
20170141
Supplemental Number
22585
Report Type
Supplemental Final
Operator Id
Name
Express Holdings (Usa), Llc
Operator Street Address
800 Werner Ct
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82601
Local Datetime
2017-04-03 07:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-04-03 07:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Mixer On Tank #501 Was Turned Off, And Locked Out.
On Site Datetime
2017-04-03 07:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Platte Pipeline System/guernsey Tank Farm
Segment Name
Platte Pipeline/western District
Onshore State Abbreviation
Wy
Onshore Postal Code
82214
Onshore City Name
Guernsey
Onshore County Name
Platte
Designated Location
Milepost/valve Station
Designated Name
Tank Farm
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
5803
Est Cost Emergency
2637
Est Cost Environmental
2637
Est Cost Other
0
Est Cost Other Details
The Majority Of The Costs Were Environmental Clean Up On The Property.
Prpty
11107
Accident Psig
13
Mop Psig
20
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No alarms were received; the leak was too small to trigger an alarm.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Normal Wear And Tear On Mixer Seal.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear And Tear On Mixer Seal.
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-398-4802
Prepared Date
2017-08-22 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
At approximately 7:00 a.M. Mst on april 3, 2017, a company employee was conducting a routine maintenance check of the tank farm and discovered petroleum crude oil outside of tank number 501. Upon discovery of the release, the employee identified that 0708-tank mixer on tank number 501 was the source for the leak. The tank mixer was immediate turned off and locked out. At the time of discovery, it was conservatively estimated the total release was less than 1 barrel and the spill was contained in the dike. It was estimated 0.5 barrel of oil was recovered and the other half was part of contaminated rock and soil that was hauled off and disposed by environmental services. The leak did not meet the nrc notification criteria so no notification was made. A courtesy call was made to PHMSA western region. As a result of the investigation, it was determined the leak on the mixer was due to normal wear and tear on the seal.
Report Received Date 2017-05-01 00:00:00
Iyear 2017
Report Number 20170141
Supplemental Number 22585
Report Type Supplemental Final
Operator Id 31720 PHMSA Enforcement
Name Express Holdings (Usa), Llc
Operator Street Address 800 Werner Ct
Operator City Name Casper
Operator State Abbreviation WY
Operator Postal Code 82601
Local Datetime 2017-04-03 07:00:00
Location Latitude 42.2243735 Google Maps OpenStreetMap
Location Longitude -104.692557 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-04-03 07:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Mixer On Tank #501 Was Turned Off, And Locked Out.
On Site Datetime 2017-04-03 07:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Platte Pipeline System/guernsey Tank Farm
Segment Name Platte Pipeline/western District
Onshore State Abbreviation Wy
Onshore Postal Code 82214
Onshore City Name Guernsey
Onshore County Name Platte
Designated Location Milepost/valve Station
Designated Name Tank Farm
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Mixer
Tank Type Atmospheric
Installation Year 2015
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 5803
Est Cost Emergency 2637
Est Cost Environmental 2637
Est Cost Other 0
Est Cost Other Details The Majority Of The Costs Were Environmental Clean Up On The Property.
Prpty 11107
Accident Psig 13
Mop Psig 20
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No alarms were received; the leak was too small to trigger an alarm.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Normal Wear And Tear On Mixer Seal.
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear And Tear On Mixer Seal.
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-398-4802
Prepared Date 2017-08-22 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative At approximately 7:00 a.M. Mst on april 3, 2017, a company employee was conducting a routine maintenance check of the tank farm and discovered petroleum crude oil outside of tank number 501. Upon discovery of the release, the employee identified that 0708-tank mixer on tank number 501 was the source for the leak. The tank mixer was immediate turned off and locked out. At the time of discovery, it was conservatively estimated the total release was less than 1 barrel and the spill was contained in the dike. It was estimated 0.5 barrel of oil was recovered and the other half was part of contaminated rock and soil that was hauled off and disposed by environmental services. The leak did not meet the nrc notification criteria so no notification was made. A courtesy call was made to PHMSA western region. As a result of the investigation, it was determined the leak on the mixer was due to normal wear and tear on the seal.

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