HL incident on 2017-04-02 — OK

Operator
Explorer Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,250
Incident datetime
2017-04-02 01:26
Report number
Location
OK
Narrative
On april 2, 2017 an operation technician discovered a release of jet fuel from an oil water separation system at the hammond tank farm. The product that was released was totally contained on the property and any impacted soil was immediately addressed. The direct cause of the release was from a failed gasket associated with the nemo progressive pump. The pump feeds a gravity fed product and water mixture in a sump from water draws to an oil water separator. No obstructions were identified with the pump or drain lines. The estimated pressure directly downstream of the pump and upstream of the relief from post incident field testing indicated to be approximately 50 psi. However, it's believe an overpressure on the nemo pump gasket on the oil water separator was the direct cause. A newly design system has been installed to mitigate any potential future occurrences with the oil water separator.
Detailed record list
Report Received Date
2017-04-28 00:00:00
Iyear
2017
Report Number
20170139
Supplemental Number
30502
Report Type
Supplemental Final
Operator Id
Name
Explorer Pipeline Co
Operator Street Address
Po Box 2650
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74101
Local Datetime
2017-04-02 01:26:00
Location Latitude
Location Longitude
-87.43874523
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
20.4
Recovered Bbls
20.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-04-02 01:26:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release From Oil Water Seperator System.
On Site Datetime
2017-04-02 01:26:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Hammond Tank Farm
Segment Name
Hammond Tank Farm
Onshore State Abbreviation
In
Onshore Postal Code
46323
Onshore City Name
Hammond
Onshore County Name
Lake
Designated Location
Milepost/valve Station
Designated Name
650.92
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Cast Iron
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
125
Est Cost Prop Damage
1250
Est Cost Emergency
6000
Est Cost Environmental
0
Est Cost Other
0
Prpty
7375
Accident Psig
50
Mop Psig
250
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release was from a station oil water separator under local operation. The action or inaction from the controller didn't cause or contribute to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Overpressure Ind
Yes
Preparer Name
K**** E* B****
Preparer Title
Dot Administrator
Preparer Email
K*****@e***.com
Preparer Telephone
9184935104
Prepared Date
2018-06-14 00:00:00
Authorizer Name
J** S****
Authorizer Telephone
9184935143
Authorizer Title
Dot Engineering And Hsse
Authorizer Email
J*****@e***.com
Narrative
On april 2, 2017 an operation technician discovered a release of jet fuel from an oil water separation system at the hammond tank farm. The product that was released was totally contained on the property and any impacted soil was immediately addressed. The direct cause of the release was from a failed gasket associated with the nemo progressive pump. The pump feeds a gravity fed product and water mixture in a sump from water draws to an oil water separator. No obstructions were identified with the pump or drain lines. The estimated pressure directly downstream of the pump and upstream of the relief from post incident field testing indicated to be approximately 50 psi. However, it's believe an overpressure on the nemo pump gasket on the oil water separator was the direct cause. A newly design system has been installed to mitigate any potential future occurrences with the oil water separator.
Report Received Date 2017-04-28 00:00:00
Iyear 2017
Report Number 20170139
Supplemental Number 30502
Report Type Supplemental Final
Operator Id 4805 PHMSA Enforcement
Name Explorer Pipeline Co
Operator Street Address Po Box 2650
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74101
Local Datetime 2017-04-02 01:26:00
Location Latitude 41.60766736 Google Maps OpenStreetMap
Location Longitude -87.43874523 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 20.4
Recovered Bbls 20.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-04-02 01:26:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Release From Oil Water Seperator System.
On Site Datetime 2017-04-02 01:26:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Hammond Tank Farm
Segment Name Hammond Tank Farm
Onshore State Abbreviation In
Onshore Postal Code 46323
Onshore City Name Hammond
Onshore County Name Lake
Designated Location Milepost/valve Station
Designated Name 650.92
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Cast Iron
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 125
Est Cost Prop Damage 1250
Est Cost Emergency 6000
Est Cost Environmental 0
Est Cost Other 0
Prpty 7375
Accident Psig 50
Mop Psig 250
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release was from a station oil water separator under local operation. The action or inaction from the controller didn't cause or contribute to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Overpressure Ind Yes
Preparer Name K**** E* B****
Preparer Title Dot Administrator
Preparer Email K*****@e***.com
Preparer Telephone 9184935104
Prepared Date 2018-06-14 00:00:00
Authorizer Name J** S****
Authorizer Telephone 9184935143
Authorizer Title Dot Engineering And Hsse
Authorizer Email J*****@e***.com
Narrative On april 2, 2017 an operation technician discovered a release of jet fuel from an oil water separation system at the hammond tank farm. The product that was released was totally contained on the property and any impacted soil was immediately addressed. The direct cause of the release was from a failed gasket associated with the nemo progressive pump. The pump feeds a gravity fed product and water mixture in a sump from water draws to an oil water separator. No obstructions were identified with the pump or drain lines. The estimated pressure directly downstream of the pump and upstream of the relief from post incident field testing indicated to be approximately 50 psi. However, it's believe an overpressure on the nemo pump gasket on the oil water separator was the direct cause. A newly design system has been installed to mitigate any potential future occurrences with the oil water separator.

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