HL incident on 2017-03-27 — TX

Operator
Sunoco Pipeline L.p.
Cause
Notification Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$28,321
Incident datetime
2017-03-27 16:52
Report number
Location
TX
Narrative
At 16:52 on 3/27/2017 sunoco pipeline control center received a leak warn alarm on the maysville to seminole 6" line segment and the line segment was immediately shut down. At 17:01 a landowner notified the control center that he had hit the line with a bulldozer and confirmed oil on the ground. Sunoco personnel arrived at the block valves at 17:16 and isolated the line by 17:24. Approximately 37 barrels of crude was released. Al free crude was recovered via vacuum truck and contaminated soil/debris was remediated onsite. A plidco clamp was installed and a controlled startup initiated to verify line/clamp integrity. The line was returned to service on 3/28/2017 by 19:40. Permanent repair of the failure involved cut out ad replacement of the affected piping.
Detailed record list
Report Received Date
2017-04-20 00:00:00
Iyear
2017
Report Number
20170133
Supplemental Number
22442
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-03-27 16:52:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
37
Recovered Bbls
32
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
Incident Identified Datetime
2017-03-27 16:52:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-03-27 16:52:00
Restart Datetime
2017-03-28 20:30:00
On Site Datetime
2017-03-27 17:16:00
Nrc Rpt Datetime
2017-03-27 18:45:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Mysv-Semi-6
Segment Name
553012-6" Maysville To Seminole
Onshore State Abbreviation
Ok
Onshore Postal Code
74831
Onshore City Name
Rosedale
Onshore County Name
Mcclain
Designated Location
Survey Station No.
Designated Name
844+72
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
27
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6.625
Pipe Wall Thickness
0.156
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Lap Welded
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
5
Puncture Circum
1.5
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
221
Est Cost Prop Damage
28321
Est Cost Emergency
31444
Est Cost Environmental
10726
Est Cost Other
2945
Est Cost Other Details
Row Contractor Costs
Prpty
73657
Accident Psig
500
Mop Psig
680
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
46428
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Pipeline Easement Row Ind
Yes
Excavator Type
Occupant
Excavator Equipment
Grader/scraper
Work Performed
Grading
One Call Notified Ind
No
Service Interruption
Yes
Service Interruption Hours
24
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
T*** G* N*******
Preparer Title
Sr. Manager Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2017-06-27 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Sr. Manager Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
At 16:52 on 3/27/2017 sunoco pipeline control center received a leak warn alarm on the maysville to seminole 6" line segment and the line segment was immediately shut down. At 17:01 a landowner notified the control center that he had hit the line with a bulldozer and confirmed oil on the ground. Sunoco personnel arrived at the block valves at 17:16 and isolated the line by 17:24. Approximately 37 barrels of crude was released. Al free crude was recovered via vacuum truck and contaminated soil/debris was remediated onsite. A plidco clamp was installed and a controlled startup initiated to verify line/clamp integrity. The line was returned to service on 3/28/2017 by 19:40. Permanent repair of the failure involved cut out ad replacement of the affected piping.
Report Received Date 2017-04-20 00:00:00
Iyear 2017
Report Number 20170133
Supplemental Number 22442
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-03-27 16:52:00
Location Latitude 34.92554 Google Maps OpenStreetMap
Location Longitude -97.21707 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 37
Recovered Bbls 32
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Third Party That Caused The Accident
Incident Identified Datetime 2017-03-27 16:52:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-03-27 16:52:00
Restart Datetime 2017-03-28 20:30:00
On Site Datetime 2017-03-27 17:16:00
Nrc Rpt Datetime 2017-03-27 18:45:00
Nrc Rpt Num 1174206 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Mysv-Semi-6
Segment Name 553012-6" Maysville To Seminole
Onshore State Abbreviation Ok
Onshore Postal Code 74831
Onshore City Name Rosedale
Onshore County Name Mcclain
Designated Location Survey Station No.
Designated Name 844+72
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 27
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6.625
Pipe Wall Thickness 0.156
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Lap Welded
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 5
Puncture Circum 1.5
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 221
Est Cost Prop Damage 28321
Est Cost Emergency 31444
Est Cost Environmental 10726
Est Cost Other 2945
Est Cost Other Details Row Contractor Costs
Prpty 73657
Accident Psig 500
Mop Psig 680
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 46428
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Pipeline Easement Row Ind Yes
Excavator Type Occupant
Excavator Equipment Grader/scraper
Work Performed Grading
One Call Notified Ind No
Service Interruption Yes
Service Interruption Hours 24
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name T*** G* N*******
Preparer Title Sr. Manager Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2017-06-27 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Sr. Manager Dot Compliance
Authorizer Email T************@e*************.com
Narrative At 16:52 on 3/27/2017 sunoco pipeline control center received a leak warn alarm on the maysville to seminole 6" line segment and the line segment was immediately shut down. At 17:01 a landowner notified the control center that he had hit the line with a bulldozer and confirmed oil on the ground. Sunoco personnel arrived at the block valves at 17:16 and isolated the line by 17:24. Approximately 37 barrels of crude was released. Al free crude was recovered via vacuum truck and contaminated soil/debris was remediated onsite. A plidco clamp was installed and a controlled startup initiated to verify line/clamp integrity. The line was returned to service on 3/28/2017 by 19:40. Permanent repair of the failure involved cut out ad replacement of the affected piping.

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