HL incident on 2017-03-21 — TX

Operator
Enterprise Products Operating Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$265,000
Incident datetime
2017-03-21 12:40
Report number
Location
TX
Narrative
At 12:40 on 3/21/2017 a 3rd party called local operating personnel to inform them of a gas smell. An enterprise technician arrived at 14:15 and verified lel was present over an enterprise pipeline. The line had been previously shut down but was blocked in after discovery of the leak. An estimated 2 bbls of ethane/propane mix was released. Approximately 3.9 miles of line was flared (block valve to block valve) and the leak site was excavated, uncovering a pinhole leak. The failed section of pipe was cut out and replaced. The line was filled with product at 17:50 on 3/29/2017. At 18:00 on 3/21 it was determined that the total cost would exceed $50,000, necessitating an nrc call which was made 18:58. The cause is under investigation and the failed section of pipe was sent in for metallurgical analysis. A final report will be submitted upon receipt of the results. No costs associated with emergency response or environmental remediation. The area was flagged off. The area was backfilled with existing soil. 5/31/2017 it was determined from the metallurgical analysis that the original crack was predominately formed during manufacturing.
Detailed record list
Report Received Date
2017-04-19 00:00:00
Iyear
2017
Report Number
20170132
Supplemental Number
22926
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-03-21 12:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane/propane
Unintentional Release Bbls
2
Intentional Release Bbls
4000
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2017-03-21 12:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-03-21 15:30:00
Restart Datetime
2017-03-29 17:50:00
On Site Datetime
2017-03-21 13:40:00
Nrc Rpt Datetime
2017-03-21 18:58:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Seminole Mainline
Segment Name
1
Onshore State Abbreviation
Tx
Onshore Postal Code
77541
Onshore City Name
Clute
Onshore County Name
Brazoria
Designated Location
Milepost/valve Station
Designated Name
Mp 553.8
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
74
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
14
Pipe Wall Thickness
0.375
Pipe Smys
46000
Pipe Specification
Api-5l-X46
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
American Steel
Pipe Coating Type
Other
Pipe Coating Details
Polyken Tape
Installation Year
1981
Manufactured Year
1980
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
250
Est Cost Prop Damage
265000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
12000
Est Cost Other Details
Metallurgical Analysis.
Prpty
277250
Accident Psig
1000
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
20592
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller was not a contributing factor to the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Crack
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Axial Recent Year
2016
Circ Wave Recent Year
2016
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr
2017
Non Destructive Exam Ind
No
Preparer Name
R****** R*****
Preparer Title
Sr. Pipeline Compliance Engineer
Preparer Email
R*******@e****.com
Preparer Telephone
713-381-6841
Prepared Date
2017-12-12 00:00:00
Authorizer Name
R****** R*****
Authorizer Telephone
713-381-6841
Authorizer Title
Sr. Pipeline Compliance Engineer
Authorizer Email
R*******@e****.com
Narrative
At 12:40 on 3/21/2017 a 3rd party called local operating personnel to inform them of a gas smell. An enterprise technician arrived at 14:15 and verified lel was present over an enterprise pipeline. The line had been previously shut down but was blocked in after discovery of the leak. An estimated 2 bbls of ethane/propane mix was released. Approximately 3.9 miles of line was flared (block valve to block valve) and the leak site was excavated, uncovering a pinhole leak. The failed section of pipe was cut out and replaced. The line was filled with product at 17:50 on 3/29/2017. At 18:00 on 3/21 it was determined that the total cost would exceed $50,000, necessitating an nrc call which was made 18:58. The cause is under investigation and the failed section of pipe was sent in for metallurgical analysis. A final report will be submitted upon receipt of the results. No costs associated with emergency response or environmental remediation. The area was flagged off. The area was backfilled with existing soil. 5/31/2017 it was determined from the metallurgical analysis that the original crack was predominately formed during manufacturing.
Report Received Date 2017-04-19 00:00:00
Iyear 2017
Report Number 20170132
Supplemental Number 22926
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-03-21 12:30:00
Location Latitude 29.052181 Google Maps OpenStreetMap
Location Longitude -95.351156 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane/propane
Unintentional Release Bbls 2
Intentional Release Bbls 4000
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2017-03-21 12:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-03-21 15:30:00
Restart Datetime 2017-03-29 17:50:00
On Site Datetime 2017-03-21 13:40:00
Nrc Rpt Datetime 2017-03-21 18:58:00
Nrc Rpt Num 1173788 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Seminole Mainline
Segment Name 1
Onshore State Abbreviation Tx
Onshore Postal Code 77541
Onshore City Name Clute
Onshore County Name Brazoria
Designated Location Milepost/valve Station
Designated Name Mp 553.8
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 74
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 14
Pipe Wall Thickness 0.375
Pipe Smys 46000
Pipe Specification Api-5l-X46
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer American Steel
Pipe Coating Type Other
Pipe Coating Details Polyken Tape
Installation Year 1981
Manufactured Year 1980
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 250
Est Cost Prop Damage 265000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 12000
Est Cost Other Details Metallurgical Analysis.
Prpty 277250
Accident Psig 1000
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 20592
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller was not a contributing factor to the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Crack
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Axial Recent Year 2016
Circ Wave Recent Year 2016
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr 2017
Non Destructive Exam Ind No
Preparer Name R****** R*****
Preparer Title Sr. Pipeline Compliance Engineer
Preparer Email R*******@e****.com
Preparer Telephone 713-381-6841
Prepared Date 2017-12-12 00:00:00
Authorizer Name R****** R*****
Authorizer Telephone 713-381-6841
Authorizer Title Sr. Pipeline Compliance Engineer
Authorizer Email R*******@e****.com
Narrative At 12:40 on 3/21/2017 a 3rd party called local operating personnel to inform them of a gas smell. An enterprise technician arrived at 14:15 and verified lel was present over an enterprise pipeline. The line had been previously shut down but was blocked in after discovery of the leak. An estimated 2 bbls of ethane/propane mix was released. Approximately 3.9 miles of line was flared (block valve to block valve) and the leak site was excavated, uncovering a pinhole leak. The failed section of pipe was cut out and replaced. The line was filled with product at 17:50 on 3/29/2017. At 18:00 on 3/21 it was determined that the total cost would exceed $50,000, necessitating an nrc call which was made 18:58. The cause is under investigation and the failed section of pipe was sent in for metallurgical analysis. A final report will be submitted upon receipt of the results. No costs associated with emergency response or environmental remediation. The area was flagged off. The area was backfilled with existing soil. 5/31/2017 it was determined from the metallurgical analysis that the original crack was predominately formed during manufacturing.

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