Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2017-07-13 — CA
Operator
Southern California Gas Co
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$13
Incident datetime
2017-07-13 19:15
Report number
Location
CA, RIVERSIDE
Narrative
An rv struck the msa and the service riser of 14822 delfbush street, moreno valley, causing a release of gas and igniting the rv as well as the two houses at 14832 and 14822 delfbush street. Socalgas crew responded and controlled the gas by 21:31 of the incident date. No further damages or injuries resulted from this event. All repairs to the damaged service were completed by cutting the damaged service riser, clamping, and plugging the stopcock. The services to the damaged homes will be restored upon completion of repairs and at the request of the customers. This incident was reported to the DOT and to the cpuc when pipeline safety and compliance became aware that the damage cost exceeded $50,000. The 48-hour update was submitted under nrc 1193302. For any further questions, please contact ik song at (818) 279-5388.
Detailed record list
Occurred At
2017-07-13 19:15:00
Year
2017
Report Received Date
2017-11-13 00:00:00
Iyear
2017.0
Report Number
20170104.0
Supplemental Number
16699.0
Report Type
Supplemental Final
Operator Id
18484
Name
Southern California Gas Co
Operator Street Address
555 West Fifth Street
Operator City Name
Los Angeles
Operator State Abbreviation
CA
Operator Postal Code
90013
Local Datetime
2017-07-13 19:15:00
Location Street Address
14822 Delfbush Street
Location City Name
Moreno Valley
Location County Name
Riverside
Location State Abbreviation
CA
Location Postal Code
92553
Location Latitude
33.90539
Location Longitude
-117.22782
Nrc Rpt Datetime
2017-10-13 10:22:00
Nrc Rpt Num
1193174
Commodity Released Type
Natural Gas
Unintentional Release
25.43
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
8.0
Incident Identified Datetime
2017-07-13 19:15:00
On Site Datetime
2017-07-13 19:40:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service Riser
Installation Year
1973.0
Material Involved
Steel
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 3 Location
Est Cost Oper Paid
221958.0
Est Cost Prop Damage
13.0
Est Cost Emergency
1768.0
Est Cost Other
0.0
Est Cost Unintentional Release
153.0
Prpty
223892.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
2.0
Accident Psig
44.0
Normal Psig
45.0
Mop Psig
50.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Preparer Name
I* S***
Preparer Title
Pipeline Safety And Compliance Advisor
Preparer Email
I****@s**************.com
Preparer Telephone
818-279-5388
Authorizer Name
T*** B****
Authorizer Title
Pipeline Safety And Compliance Manager
Authorizer Telephone
909-335-7915
Authorizer Email
T*****@s**************.com
Narrative
An rv struck the msa and the service riser of 14822 delfbush street, moreno valley, causing a release of gas and igniting the rv as well as the two houses at 14832 and 14822 delfbush street. Socalgas crew responded and controlled the gas by 21:31 of the incident date. No further damages or injuries resulted from this event. All repairs to the damaged service were completed by cutting the damaged service riser, clamping, and plugging the stopcock. The services to the damaged homes will be restored upon completion of repairs and at the request of the customers. This incident was reported to the DOT and to the cpuc when pipeline safety and compliance became aware that the damage cost exceeded $50,000. The 48-hour update was submitted under nrc 1193302. For any further questions, please contact ik song at (818) 279-5388.
| Occurred At | 2017-07-13 19:15:00 |
|---|---|
| Year | 2017 |
| Report Received Date | 2017-11-13 00:00:00 |
| Iyear | 2017.0 |
| Report Number | 20170104.0 |
| Supplemental Number | 16699.0 |
| Report Type | Supplemental Final |
| Operator Id | 18484 PHMSA Enforcement |
| Name | Southern California Gas Co |
| Operator Street Address | 555 West Fifth Street |
| Operator City Name | Los Angeles |
| Operator State Abbreviation | CA |
| Operator Postal Code | 90013 |
| Local Datetime | 2017-07-13 19:15:00 |
| Location Street Address | 14822 Delfbush Street |
| Location City Name | Moreno Valley |
| Location County Name | Riverside |
| Location State Abbreviation | CA |
| Location Postal Code | 92553 |
| Location Latitude | 33.90539 Google Maps OpenStreetMap |
| Location Longitude | -117.22782 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2017-10-13 10:22:00 |
| Nrc Rpt Num | 1193174 NRC Report How to search |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 25.43 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Ignite Ind | Yes |
| Explode Ind | No |
| Num Pub Evacuated | 8.0 |
| Incident Identified Datetime | 2017-07-13 19:15:00 |
| On Site Datetime | 2017-07-13 19:40:00 |
| Federal | No |
| Location Type | Private Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set) |
| Crossing | No |
| Pipe Facility Type | Investor Owned |
| System Part Involved | Service Riser |
| Installation Year | 1973.0 |
| Material Involved | Steel |
| Release Type | Leak |
| Leak Type | Crack |
| Class Location Type | Class 3 Location |
| Est Cost Oper Paid | 221958.0 |
| Est Cost Prop Damage | 13.0 |
| Est Cost Emergency | 1768.0 |
| Est Cost Other | 0.0 |
| Est Cost Unintentional Release | 153.0 |
| Prpty | 223892.0 |
| Commercial Affected | 0.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 2.0 |
| Accident Psig | 44.0 |
| Normal Psig | 45.0 |
| Mop Psig | 50.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | No |
| Accident Identifier | Notification From Emergency Responder |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the incident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Other Outside Force Damage |
| Cause Details | Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation |
| Outside Force Type | Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation |
| Vehicle Subtype | Third Party |
| Preparer Name | I* S*** |
| Preparer Title | Pipeline Safety And Compliance Advisor |
| Preparer Email | I****@s**************.com |
| Preparer Telephone | 818-279-5388 |
| Authorizer Name | T*** B**** |
| Authorizer Title | Pipeline Safety And Compliance Manager |
| Authorizer Telephone | 909-335-7915 |
| Authorizer Email | T*****@s**************.com |
| Narrative | An rv struck the msa and the service riser of 14822 delfbush street, moreno valley, causing a release of gas and igniting the rv as well as the two houses at 14832 and 14822 delfbush street. Socalgas crew responded and controlled the gas by 21:31 of the incident date. No further damages or injuries resulted from this event. All repairs to the damaged service were completed by cutting the damaged service riser, clamping, and plugging the stopcock. The services to the damaged homes will be restored upon completion of repairs and at the request of the customers. This incident was reported to the DOT and to the cpuc when pipeline safety and compliance became aware that the damage cost exceeded $50,000. The 48-hour update was submitted under nrc 1193302. For any further questions, please contact ik song at (818) 279-5388. |
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