GD incident on 2017-09-20 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Equipment Failure
Commodity
Program
GD
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$0
Incident datetime
2017-09-20 21:02
Report number
Location
TX, DALLAS
Narrative
Additional nrc report number 1191273 on september 20, 2017, gas ignition occurred while performing a tie-in weld on a 16" main at 1847 levee st. And turtle creek in dallas, texas. There was a malfunction with the configuration of the gas mover system and the stopple valves, which reintroduced a small amount of gas into the pipe near where the welding operations were occurring. The air compressor was identified to be the source of the malfunction. The hoses were then disconnected and reconnected to a secondary compressor. When welding commenced on the 16" tie-in, the flash/ignition occurred within the main. Two employees of driver pipeline were injured and transported by ambulance to parkland hospital. One welder was released from the emergency room not requiring hospitalization, and the other welder was hospitalized and released on the afternoon of september 23, 2017 with minor injuries.
Detailed record list
Occurred At
2017-09-20 21:02:00
Year
2017
Report Received Date
2017-10-20 00:00:00
Iyear
2017.0
Report Number
20170092.0
Supplemental Number
30683.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2017-09-20 21:02:00
Location Street Address
1847 E. Levee St. And Turtle Creek
Location City Name
Dallas
Location County Name
Dallas
Location State Abbreviation
TX
Location Postal Code
75207
Location Latitude
Location Longitude
Nrc Rpt Datetime
2017-09-20 22:43:00
Nrc Rpt Num
Unintentional Release
1.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
1
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2017-09-20 21:02:00
On Site Datetime
2017-09-20 21:02:00
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
2017.0
Pipe Diameter
16.0
Pipe Specification
Api-5l 45th-Psl2
Pipe Manufacturer
Csi Tubular
Material Involved
Steel
Wt Steel
0.375
Release Type
Leak
Leak Type
Seal Or Packing
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
0.0
Est Cost Emergency
0.0
Est Cost Other
152.0
Est Cost Other Details
2 Overtime Hours For Sr. Field Construction Coordinator
Est Cost Unintentional Release
7.0
Prpty
159.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
21.0
Normal Psig
21.0
Mop Psig
55.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No investigation of the control room was required since the control of pressure did not contribute to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
8
Num Contractors Failed
0
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Eq Failure Details
Electronic Malfunction In The Sul Air Compressor
Preparer Name
M***** D*******
Preparer Title
Operations Supervisor
Preparer Email
M**************@a**********.com
Preparer Telephone
214-426-7082
Preparer Fax
214-426-7081
Authorizer Name
M**** S*****
Authorizer Title
Director Regulatory And Compliance
Authorizer Telephone
214-206-2033
Authorizer Email
M***********@a**********.com
Narrative
Additional nrc report number 1191273 on september 20, 2017, gas ignition occurred while performing a tie-in weld on a 16" main at 1847 levee st. And turtle creek in dallas, texas. There was a malfunction with the configuration of the gas mover system and the stopple valves, which reintroduced a small amount of gas into the pipe near where the welding operations were occurring. The air compressor was identified to be the source of the malfunction. The hoses were then disconnected and reconnected to a secondary compressor. When welding commenced on the 16" tie-in, the flash/ignition occurred within the main. Two employees of driver pipeline were injured and transported by ambulance to parkland hospital. One welder was released from the emergency room not requiring hospitalization, and the other welder was hospitalized and released on the afternoon of september 23, 2017 with minor injuries.
Occurred At 2017-09-20 21:02:00
Year 2017
Report Received Date 2017-10-20 00:00:00
Iyear 2017.0
Report Number 20170092.0
Supplemental Number 30683.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2017-09-20 21:02:00
Location Street Address 1847 E. Levee St. And Turtle Creek
Location City Name Dallas
Location County Name Dallas
Location State Abbreviation TX
Location Postal Code 75207
Location Latitude 32.7914 Google Maps OpenStreetMap
Location Longitude -96.8285 Google Maps OpenStreetMap
Nrc Rpt Datetime 2017-09-20 22:43:00
Nrc Rpt Num 1191038 NRC Report How to search
Unintentional Release 1.0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 1
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2017-09-20 21:02:00
On Site Datetime 2017-09-20 21:02:00
Federal No
Location Type Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 48.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 2017.0
Pipe Diameter 16.0
Pipe Specification Api-5l 45th-Psl2
Pipe Manufacturer Csi Tubular
Material Involved Steel
Wt Steel 0.375
Release Type Leak
Leak Type Seal Or Packing
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 0.0
Est Cost Emergency 0.0
Est Cost Other 152.0
Est Cost Other Details 2 Overtime Hours For Sr. Field Construction Coordinator
Est Cost Unintentional Release 7.0
Prpty 159.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 21.0
Normal Psig 21.0
Mop Psig 55.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No investigation of the control room was required since the control of pressure did not contribute to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 8
Num Contractors Failed 0
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Eq Failure Details Electronic Malfunction In The Sul Air Compressor
Preparer Name M***** D*******
Preparer Title Operations Supervisor
Preparer Email M**************@a**********.com
Preparer Telephone 214-426-7082
Preparer Fax 214-426-7081
Authorizer Name M**** S*****
Authorizer Title Director Regulatory And Compliance
Authorizer Telephone 214-206-2033
Authorizer Email M***********@a**********.com
Narrative Additional nrc report number 1191273 on september 20, 2017, gas ignition occurred while performing a tie-in weld on a 16" main at 1847 levee st. And turtle creek in dallas, texas. There was a malfunction with the configuration of the gas mover system and the stopple valves, which reintroduced a small amount of gas into the pipe near where the welding operations were occurring. The air compressor was identified to be the source of the malfunction. The hoses were then disconnected and reconnected to a secondary compressor. When welding commenced on the 16" tie-in, the flash/ignition occurred within the main. Two employees of driver pipeline were injured and transported by ambulance to parkland hospital. One welder was released from the emergency room not requiring hospitalization, and the other welder was hospitalized and released on the afternoon of september 23, 2017 with minor injuries.

All rights reserved. Copyright © by ClearPHMSA