GD incident on 2017-09-14 — TX

Operator
Texas Community Propane, Ltd.
Cause
Incorrect Operation
Commodity
Propane Gas
Program
GD
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$175
Incident datetime
2017-09-14 14:09
Report number
Location
TX, TRAVIS
Narrative
Concrete company drove a metal stake into a silt fence and a bobcat impaled the stake down into the 2 inch main, causing a slow release. Operator employees arrived and during attempted repair of damaged pipe, caused ignition, burning one employee, other employee closed isolation valve shutting gas supply off. Burned employee taken to hospital, main was repaired and service restored to customers. Burned employee released the following morning. Both employees were written up for not following policy and both admitted they knew better, but believed themselves to be out of the gas environment. Additionally, both employees were suspended without pay.
Detailed record list
Occurred At
2017-09-14 14:09:00
Year
2017
Report Received Date
2017-09-15 00:00:00
Iyear
2017.0
Report Number
20170083.0
Supplemental Number
31501.0
Report Type
Supplemental Final
Operator Id
Name
Texas Community Propane, Ltd.
Operator Street Address
2579 Western Trails Blvd., Suite 240
Operator City Name
Austin
Operator State Abbreviation
TX
Operator Postal Code
78745
Local Datetime
2017-09-14 16:55:00
Location Street Address
22320 Chipotle Pass
Location City Name
Spicewood
Location County Name
Travis
Location State Abbreviation
TX
Location Postal Code
78669
Location Latitude
Location Longitude
Nrc Rpt Datetime
2017-09-14 21:47:00
Nrc Rpt Num
Commodity Released Type
Propane Gas
Unintentional Release
88.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
1
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2017-09-14 14:09:00
On Site Datetime
2017-09-14 14:25:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
32.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
2014.0
Pipe Diameter
2.0
Pipe Specification
Pe2406 Astm 2513
Pipe Manufacturer
Driscoplex
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Wt Plastic
0.25
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
0.5
Puncture Circum
0.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
175.0
Est Cost Emergency
2655.0
Est Cost Other
0.0
Est Cost Unintentional Release
5194.0
Prpty
8024.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
25.0
Accident Psig
30.0
Normal Psig
30.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Other
Accident Details
Homebuilder Called In Leak - His Contractor Caused Damage
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
Yes
Num Employees Tested
2
Num Employees Failed
0
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Tcp Employees Were To Repair A Damaged Main And Used An Electrical Tool In A Gas Environment, Against Company Policy. This Resulted In An Ignition And Burn Injuries To One Employee.
Related Failure Follow Ind
Yes
Category Type
Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
J***** B****
Preparer Title
Office Manager
Preparer Email
C*********************@t********************.com
Preparer Telephone
5122725503
Authorizer Name
J***** B****
Authorizer Title
Office Manager
Authorizer Telephone
5122725503
Authorizer Email
C*********************@t********************.com
Narrative
Concrete company drove a metal stake into a silt fence and a bobcat impaled the stake down into the 2 inch main, causing a slow release. Operator employees arrived and during attempted repair of damaged pipe, caused ignition, burning one employee, other employee closed isolation valve shutting gas supply off. Burned employee taken to hospital, main was repaired and service restored to customers. Burned employee released the following morning. Both employees were written up for not following policy and both admitted they knew better, but believed themselves to be out of the gas environment. Additionally, both employees were suspended without pay.
Occurred At 2017-09-14 14:09:00
Year 2017
Report Received Date 2017-09-15 00:00:00
Iyear 2017.0
Report Number 20170083.0
Supplemental Number 31501.0
Report Type Supplemental Final
Operator Id 32061 PHMSA Enforcement
Name Texas Community Propane, Ltd.
Operator Street Address 2579 Western Trails Blvd., Suite 240
Operator City Name Austin
Operator State Abbreviation TX
Operator Postal Code 78745
Local Datetime 2017-09-14 16:55:00
Location Street Address 22320 Chipotle Pass
Location City Name Spicewood
Location County Name Travis
Location State Abbreviation TX
Location Postal Code 78669
Location Latitude 30.35303 Google Maps OpenStreetMap
Location Longitude -98.08693 Google Maps OpenStreetMap
Nrc Rpt Datetime 2017-09-14 21:47:00
Nrc Rpt Num 1190371 NRC Report How to search
Commodity Released Type Propane Gas
Unintentional Release 88.0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 1
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2017-09-14 14:09:00
On Site Datetime 2017-09-14 14:25:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 32.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 2014.0
Pipe Diameter 2.0
Pipe Specification Pe2406 Astm 2513
Pipe Manufacturer Driscoplex
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Wt Plastic 0.25
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 0.5
Puncture Circum 0.5
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 175.0
Est Cost Emergency 2655.0
Est Cost Other 0.0
Est Cost Unintentional Release 5194.0
Prpty 8024.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 25.0
Accident Psig 30.0
Normal Psig 30.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Other
Accident Details Homebuilder Called In Leak - His Contractor Caused Damage
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind Yes
Num Employees Tested 2
Num Employees Failed 0
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Tcp Employees Were To Repair A Damaged Main And Used An Electrical Tool In A Gas Environment, Against Company Policy. This Resulted In An Ignition And Burn Injuries To One Employee.
Related Failure Follow Ind Yes
Category Type Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name J***** B****
Preparer Title Office Manager
Preparer Email C*********************@t********************.com
Preparer Telephone 5122725503
Authorizer Name J***** B****
Authorizer Title Office Manager
Authorizer Telephone 5122725503
Authorizer Email C*********************@t********************.com
Narrative Concrete company drove a metal stake into a silt fence and a bobcat impaled the stake down into the 2 inch main, causing a slow release. Operator employees arrived and during attempted repair of damaged pipe, caused ignition, burning one employee, other employee closed isolation valve shutting gas supply off. Burned employee taken to hospital, main was repaired and service restored to customers. Burned employee released the following morning. Both employees were written up for not following policy and both admitted they knew better, but believed themselves to be out of the gas environment. Additionally, both employees were suspended without pay.

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