GD incident on 2017-07-27 — CA

Operator
Pacific Gas & Electric Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$248,476
Incident datetime
2017-07-27 14:17
Report number
Location
CA, SAN JOAQUIN
Narrative
On july 27, 2017 at 1401 hours, pg&e received an erx alarm in acampo. At 1417 hours, pg&e was notified of a third party dig-in at 216 w taddei rd, acampo. Third party contractor was ripping/plowing the field and severed a 6' steel gas main, resulting in an unintentional release of gas. There was a valid USA ticket (#w719900024) and pg&e facilities were properly located & marked. The dig-in was a result of failing to raise the ripper shank prior to driving over the gas pipeline. In addition, the excavator did not determine the exact location of the line using hand tools within the tolerance zone. Pg&e gas service representative (gsr) arrived on site at 1441 hours. The flow of gas was stopped at 1527 hours by shutting in the reg station and closing valves. Approximately 738 customer gas services were impacted. Repairs to the main were completed by 2030 hours. Gsrs were deployed and service restoration operations began on 7/28/17 at 1300 hours. All services have been restored. Fire department, highway patrol and the local sheriff were reported on-site. Media was reported on site on 7/28/17. There were no injuries, fatalities, or ignition associated with this incident. Approximately 4.9 mmcf of natural gas was unintentionally released. This incident was reported to DOT (1185473) due to the large customer outage resulting in damages greater than $50k and unintentional release of gas greater than 3 mmcf. The volume update was provided to the DOT (1185576) on 7/28/17.
Detailed record list
Occurred At
2017-07-27 14:17:00
Year
2017
Report Received Date
2017-08-25 00:00:00
Iyear
2017.0
Report Number
20170072.0
Supplemental Number
16630.0
Report Type
Supplemental Final
Operator Id
Name
Pacific Gas & Electric Co
Operator Street Address
6121 Bollinger Canyon Rd.
Operator City Name
San Ramon
Operator State Abbreviation
CA
Operator Postal Code
94583
Local Datetime
2017-07-27 14:01:00
Location Street Address
216 W Taddei Rd
Location City Name
Acampo
Location County Name
San Joaquin
Location State Abbreviation
CA
Location Postal Code
95220
Location Latitude
Location Longitude
Nrc Rpt Datetime
2017-07-27 15:56:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
4900.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
10.0
Incident Identified Datetime
2017-07-27 14:17:00
On Site Datetime
2017-07-27 14:41:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1946.0
Pipe Diameter
6.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Electric Resistance Welded
Release Type
Mechanical Puncture
Puncture Axial
6.0
Puncture Circum
6.0
Class Location Type
Class 2 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
248476.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
14700.0
Prpty
263176.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
738.0
Accident Psig
54.0
Normal Psig
54.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Event was caused by a 3rd party dig in. Third party contractor was ripping/plowing the field and severed the 6" steel gas main.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Contractor
Excavator Equipment
Farm Equipment
Work Performed
Agriculture
One Call Notified Ind
Yes
One Call Ticket Num
719900024
One Call Center Name
811
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
22.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
E*** B******
Preparer Title
Senior Program Manager
Preparer Email
E***@p**.com
Preparer Telephone
925-357-7889
Authorizer Name
S**** R*******
Authorizer Title
Manager Regulatory Compliance
Authorizer Telephone
925-328-5776
Authorizer Email
G***@p**.com
Narrative
On july 27, 2017 at 1401 hours, pg&e received an erx alarm in acampo. At 1417 hours, pg&e was notified of a third party dig-in at 216 w taddei rd, acampo. Third party contractor was ripping/plowing the field and severed a 6' steel gas main, resulting in an unintentional release of gas. There was a valid USA ticket (#w719900024) and pg&e facilities were properly located & marked. The dig-in was a result of failing to raise the ripper shank prior to driving over the gas pipeline. In addition, the excavator did not determine the exact location of the line using hand tools within the tolerance zone. Pg&e gas service representative (gsr) arrived on site at 1441 hours. The flow of gas was stopped at 1527 hours by shutting in the reg station and closing valves. Approximately 738 customer gas services were impacted. Repairs to the main were completed by 2030 hours. Gsrs were deployed and service restoration operations began on 7/28/17 at 1300 hours. All services have been restored. Fire department, highway patrol and the local sheriff were reported on-site. Media was reported on site on 7/28/17. There were no injuries, fatalities, or ignition associated with this incident. Approximately 4.9 mmcf of natural gas was unintentionally released. This incident was reported to DOT (1185473) due to the large customer outage resulting in damages greater than $50k and unintentional release of gas greater than 3 mmcf. The volume update was provided to the DOT (1185576) on 7/28/17.
Occurred At 2017-07-27 14:17:00
Year 2017
Report Received Date 2017-08-25 00:00:00
Iyear 2017.0
Report Number 20170072.0
Supplemental Number 16630.0
Report Type Supplemental Final
Operator Id 15007 PHMSA Enforcement
Name Pacific Gas & Electric Co
Operator Street Address 6121 Bollinger Canyon Rd.
Operator City Name San Ramon
Operator State Abbreviation CA
Operator Postal Code 94583
Local Datetime 2017-07-27 14:01:00
Location Street Address 216 W Taddei Rd
Location City Name Acampo
Location County Name San Joaquin
Location State Abbreviation CA
Location Postal Code 95220
Location Latitude 38.190379 Google Maps OpenStreetMap
Location Longitude -121.321087 Google Maps OpenStreetMap
Nrc Rpt Datetime 2017-07-27 15:56:00
Nrc Rpt Num 1185473 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 4900.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 10.0
Incident Identified Datetime 2017-07-27 14:17:00
On Site Datetime 2017-07-27 14:41:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1946.0
Pipe Diameter 6.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Electric Resistance Welded
Release Type Mechanical Puncture
Puncture Axial 6.0
Puncture Circum 6.0
Class Location Type Class 2 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 248476.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Est Cost Unintentional Release 14700.0
Prpty 263176.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 738.0
Accident Psig 54.0
Normal Psig 54.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Event was caused by a 3rd party dig in. Third party contractor was ripping/plowing the field and severed the 6" steel gas main.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Contractor
Excavator Equipment Farm Equipment
Work Performed Agriculture
One Call Notified Ind Yes
One Call Ticket Num 719900024
One Call Center Name 811
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 22.0
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name E*** B******
Preparer Title Senior Program Manager
Preparer Email E***@p**.com
Preparer Telephone 925-357-7889
Authorizer Name S**** R*******
Authorizer Title Manager Regulatory Compliance
Authorizer Telephone 925-328-5776
Authorizer Email G***@p**.com
Narrative On july 27, 2017 at 1401 hours, pg&e received an erx alarm in acampo. At 1417 hours, pg&e was notified of a third party dig-in at 216 w taddei rd, acampo. Third party contractor was ripping/plowing the field and severed a 6' steel gas main, resulting in an unintentional release of gas. There was a valid USA ticket (#w719900024) and pg&e facilities were properly located & marked. The dig-in was a result of failing to raise the ripper shank prior to driving over the gas pipeline. In addition, the excavator did not determine the exact location of the line using hand tools within the tolerance zone. Pg&e gas service representative (gsr) arrived on site at 1441 hours. The flow of gas was stopped at 1527 hours by shutting in the reg station and closing valves. Approximately 738 customer gas services were impacted. Repairs to the main were completed by 2030 hours. Gsrs were deployed and service restoration operations began on 7/28/17 at 1300 hours. All services have been restored. Fire department, highway patrol and the local sheriff were reported on-site. Media was reported on site on 7/28/17. There were no injuries, fatalities, or ignition associated with this incident. Approximately 4.9 mmcf of natural gas was unintentionally released. This incident was reported to DOT (1185473) due to the large customer outage resulting in damages greater than $50k and unintentional release of gas greater than 3 mmcf. The volume update was provided to the DOT (1185576) on 7/28/17.

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