Incident details
Operator, cause, commodity and consequences with raw source fields.
GTG incident on 2017-06-26 — TX
Operator
Texas Eastern Transmission, Lp (Spectra Energy Partners, Lp)
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$600,000
Incident datetime
2017-06-26 14:30
Report number
Location
TX
Narrative
Indications of bubbles on the water surface in vermilion block 265 were reported by a third party helicopter on june 26, 2017. Upon investigation, it was determined the leak was caused by a pinhole leak resulting from internal corrosion on texas eastern transmission, l.P. 20-inch line 41-a-2 natural gas pipeline. Repair by installation of a leak clamp was completed august 9, 2017 and the pipeline was returned to service.
Detailed record list
Report Received Date
2017-07-18 00:00:00
Iyear
2017
Report Number
20170058
Supplemental Number
17424
Report Type
Supplemental Final
Operator Id
19235
Name
Texas Eastern Transmission, Lp (Spectra Energy Partners, Lp)
Operator Street Address
915 North Eldridge Parkway
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2017-06-26 12:30:00
Location Latitude
28.5116666
Location Longitude
-92.453
Nrc Rpt Num
1182332
Nrc Rpt Datetime
2017-06-26 14:30:00
Commodity Released Type
Natural Gas
Unintentional Release
105
Intentional Release
17660
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-06-26 17:31:00
Restart Datetime
2017-08-09 08:01:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2017-06-26 14:30:00
On Site Datetime
2017-06-26 14:30:00
On Off Shore
Offshore
Off Water Depth
150
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
Vermillion
Off Ocs Block
265
Off Area Accident Type
Below Water, Pipe On Or Above Seabed
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
20
Pipe Wall Thickness
0.406
Pipe Smys
52000
Pipe Specification
Api-5l
Pipe Seam Type
Seamless
Pipe Manufacturer
U.s. Steel
Pipe Coating Type
Other
Pipe Coating Details
Somastic And Concrete
Installation Year
1971
Manufactured Year
1971
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
524
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
315
Est Cost Intentional Release
52980
Est Cost Prop Damage
600000
Est Cost Emergency
0
Est Cost Other
0
Prpty
653295
Accident Psig
761
Mop Psig
1440
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
170024
Internal Inspection Ind
No
Other Restrictions Ind
Yes
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Other
Accident Details
Located By Third Party Personnel During Routine Fly Over
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was too small to be identified by the control room personnel. A review of operating records found abnormal operating conditions did not contribute to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Recent History Of The Pipeline
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D***** T**********
Preparer Title
Senior Technical Advisor
Preparer Email
D*****************@e*******.com
Preparer Telephone
713-627-5573
Authorizer Name
N***** A****
Authorizer Title
Supervisor Operational Compliance
Authorizer Telephone
713-627-5008
Authorizer Email
N***********@e*******.com
Narrative
Indications of bubbles on the water surface in vermilion block 265 were reported by a third party helicopter on june 26, 2017. Upon investigation, it was determined the leak was caused by a pinhole leak resulting from internal corrosion on texas eastern transmission, l.P. 20-inch line 41-a-2 natural gas pipeline. Repair by installation of a leak clamp was completed august 9, 2017 and the pipeline was returned to service.
| Report Received Date | 2017-07-18 00:00:00 |
|---|---|
| Iyear | 2017 |
| Report Number | 20170058 |
| Supplemental Number | 17424 |
| Report Type | Supplemental Final |
| Operator Id | 19235 PHMSA Enforcement |
| Name | Texas Eastern Transmission, Lp (Spectra Energy Partners, Lp) |
| Operator Street Address | 915 North Eldridge Parkway |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77079 |
| Local Datetime | 2017-06-26 12:30:00 |
| Location Latitude | 28.5116666 Google Maps OpenStreetMap |
| Location Longitude | -92.453 Google Maps OpenStreetMap |
| Nrc Rpt Num | 1182332 NRC Report How to search |
| Nrc Rpt Datetime | 2017-06-26 14:30:00 |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 105 |
| Intentional Release | 17660 |
| Accompanying Liquid | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2017-06-26 17:31:00 |
| Restart Datetime | 2017-08-09 08:01:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Incident Identified Datetime | 2017-06-26 14:30:00 |
| On Site Datetime | 2017-06-26 14:30:00 |
| On Off Shore | Offshore |
| Off Water Depth | 150 |
| Off Accident Origin | On The Outer Continental Shelf (Ocs) |
| Off Ocs Area | Vermillion |
| Off Ocs Block | 265 |
| Off Area Accident Type | Below Water, Pipe On Or Above Seabed |
| Pipe Facility Type | Interstate |
| System Part Involved | Offshore Pipeline, Including Riser And Riser Bend |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 20 |
| Pipe Wall Thickness | 0.406 |
| Pipe Smys | 52000 |
| Pipe Specification | Api-5l |
| Pipe Seam Type | Seamless |
| Pipe Manufacturer | U.s. Steel |
| Pipe Coating Type | Other |
| Pipe Coating Details | Somastic And Concrete |
| Installation Year | 1971 |
| Manufactured Year | 1971 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Class Location Type | Class 1 Location |
| Could Be Hca | No |
| Pir Radius | 524 |
| Heat Damage Ind | No |
| Non Heat Damage Ind | No |
| Hca Fatalities Ind | No |
| Est Cost Oper Paid | 0 |
| Est Cost Unintentional Release | 315 |
| Est Cost Intentional Release | 52980 |
| Est Cost Prop Damage | 600000 |
| Est Cost Emergency | 0 |
| Est Cost Other | 0 |
| Prpty | 653295 |
| Accident Psig | 761 |
| Mop Psig | 1440 |
| Mop Cfr Section | 192.619(A)(1) View CFR 49 §192 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Pressure Restriction Ind | No |
| Upstream Valve Type Ind | Manual |
| Downstream Valve Type Ind | Manual |
| Length Segment Isolated | 170024 |
| Internal Inspection Ind | No |
| Other Restrictions Ind | Yes |
| Operation Complications Ind | Yes |
| Low Flow Ind | Yes |
| Pipeline Function | Transmission System |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Accident Identifier | Other |
| Accident Details | Located By Third Party Personnel During Routine Fly Over |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The leak was too small to be identified by the control room personnel. A review of operating records found abnormal operating conditions did not contribute to the incident. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Int Visual Exam Results | Localized Pitting |
| Int Microbiological Ind | Yes |
| Int Other Basis Ind | Yes |
| Int Corrosion Basis Details | Recent History Of The Pipeline |
| Int Low Point Pipe Loc Ind | Yes |
| Corrosion Inhibitors | Yes |
| Corrosion Lining | No |
| Cleaning Dewatering | No |
| Corrosion Coupons | Yes |
| Collected Data Ind | No |
| Has Hydrtst Conduc Before Ind | No |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | D***** T********** |
| Preparer Title | Senior Technical Advisor |
| Preparer Email | D*****************@e*******.com |
| Preparer Telephone | 713-627-5573 |
| Authorizer Name | N***** A**** |
| Authorizer Title | Supervisor Operational Compliance |
| Authorizer Telephone | 713-627-5008 |
| Authorizer Email | N***********@e*******.com |
| Narrative | Indications of bubbles on the water surface in vermilion block 265 were reported by a third party helicopter on june 26, 2017. Upon investigation, it was determined the leak was caused by a pinhole leak resulting from internal corrosion on texas eastern transmission, l.P. 20-inch line 41-a-2 natural gas pipeline. Repair by installation of a leak clamp was completed august 9, 2017 and the pipeline was returned to service. |
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