GTG incident on 2017-05-31 — TX

Operator
Cypress Gas Pipeline Company
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$70,000
Incident datetime
2017-05-31 01:05
Report number
Location
TX
Narrative
An unknown third party reported to nrc, #1179785, "that a barge broke free of its moorings and collided with an underwater pipeline in the mississippi river resulting in a release of natural gas." cypress gas pipeline manually isolated the mississippi river crossing on the east and west bank. A side scan sonar investigation indicates the pipeline to be broken at approximately 50 feet below the current river level. The sonar data did not have clarity due to the river conditions to determine what may have caused this incident. The pipeline has been abandoned. Cypress gas pipeline made a 48 hour notification update to the nrc, #1179998, on june 1, 2017 at 18:09 updating volume released.
Detailed record list
Report Received Date
2017-06-26 00:00:00
Iyear
2017
Report Number
20170046
Supplemental Number
30882
Report Type
Supplemental Final
Operator Id
Name
Cypress Gas Pipeline Company
Operator Street Address
1100 Louisiana St.
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-05-31 00:01:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2017-05-31 02:36:00
Commodity Released Type
Natural Gas
Unintentional Release
21000
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-05-31 01:19:00
Still Shutdown Ind
Yes
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2017-05-31 01:05:00
On Site Datetime
2017-05-31 01:05:00
On Off Shore
Onshore
Onshore State Abbreviation
La
Onshore Postal Code
70069
Onshore City Name
Gramercy
Onshore County Name
St. John The Babtist
Designated Location
Milepost
Designated Name
1330+00
Pipe Fac Name
Lake Boeuf To Gramercy
Segment Name
Brs 101
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Crossing
Yes
Water Crossing Ind
Yes
Water Type
Uncased
Water Name
Mississippi River
Water Depth
50
Water Subtype
Below Water, Pipe On Or Above Bottom
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.5
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Youngstown Steel
Pipe Coating Type
Other
Pipe Coating Details
Cement
Installation Year
1959
Manufactured Year
1959
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Side Scan Sonar Indicated A Break In The Pipeline.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
248
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
67000
Est Cost Intentional Release
0
Est Cost Prop Damage
70000
Est Cost Emergency
0
Est Cost Other
0
Prpty
137000
Accident Psig
750
Mop Psig
900
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
4623
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
There Are No Pigging Facilities On This Section Of Pipeline.
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Controller
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Possible third party damage due to a barge strike in mississippi river.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
1
Num Employees Failed
0
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Other Incident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Investigation Complete, Cause Of Incident Unknown
Preparer Name
N***** L* G*** J**
Preparer Title
Senior Pipeline Compliance Specialst
Preparer Email
N****@e****.com
Preparer Telephone
9854934629
Authorizer Name
N***** L* G*** J**
Authorizer Title
Senior Pipeline Compliance Specialst
Authorizer Telephone
9854934629
Authorizer Email
N****@e****.com
Narrative
An unknown third party reported to nrc, #1179785, "that a barge broke free of its moorings and collided with an underwater pipeline in the mississippi river resulting in a release of natural gas." cypress gas pipeline manually isolated the mississippi river crossing on the east and west bank. A side scan sonar investigation indicates the pipeline to be broken at approximately 50 feet below the current river level. The sonar data did not have clarity due to the river conditions to determine what may have caused this incident. The pipeline has been abandoned. Cypress gas pipeline made a 48 hour notification update to the nrc, #1179998, on june 1, 2017 at 18:09 updating volume released.
Report Received Date 2017-06-26 00:00:00
Iyear 2017
Report Number 20170046
Supplemental Number 30882
Report Type Supplemental Final
Operator Id 12696 PHMSA Enforcement
Name Cypress Gas Pipeline Company
Operator Street Address 1100 Louisiana St.
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-05-31 00:01:00
Location Latitude 30.04764 Google Maps OpenStreetMap
Location Longitude -90.66066 Google Maps OpenStreetMap
Nrc Rpt Num 1179788 NRC Report How to search
Nrc Rpt Datetime 2017-05-31 02:36:00
Commodity Released Type Natural Gas
Unintentional Release 21000
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-05-31 01:19:00
Still Shutdown Ind Yes
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2017-05-31 01:05:00
On Site Datetime 2017-05-31 01:05:00
On Off Shore Onshore
Onshore State Abbreviation La
Onshore Postal Code 70069
Onshore City Name Gramercy
Onshore County Name St. John The Babtist
Designated Location Milepost
Designated Name 1330+00
Pipe Fac Name Lake Boeuf To Gramercy
Segment Name Brs 101
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Crossing Yes
Water Crossing Ind Yes
Water Type Uncased
Water Name Mississippi River
Water Depth 50
Water Subtype Below Water, Pipe On Or Above Bottom
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12
Pipe Wall Thickness 0.5
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Youngstown Steel
Pipe Coating Type Other
Pipe Coating Details Cement
Installation Year 1959
Manufactured Year 1959
Material Involved Carbon Steel
Release Type Other
Release Type Details Side Scan Sonar Indicated A Break In The Pipeline.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 248
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 67000
Est Cost Intentional Release 0
Est Cost Prop Damage 70000
Est Cost Emergency 0
Est Cost Other 0
Prpty 137000
Accident Psig 750
Mop Psig 900
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 4623
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details There Are No Pigging Facilities On This Section Of Pipeline.
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Controller
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Possible third party damage due to a barge strike in mississippi river.
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 1
Num Employees Failed 0
Num Contractors Tested 1
Num Contractors Failed 0
Cause Other Incident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Investigation Complete, Cause Of Incident Unknown
Preparer Name N***** L* G*** J**
Preparer Title Senior Pipeline Compliance Specialst
Preparer Email N****@e****.com
Preparer Telephone 9854934629
Authorizer Name N***** L* G*** J**
Authorizer Title Senior Pipeline Compliance Specialst
Authorizer Telephone 9854934629
Authorizer Email N****@e****.com
Narrative An unknown third party reported to nrc, #1179785, "that a barge broke free of its moorings and collided with an underwater pipeline in the mississippi river resulting in a release of natural gas." cypress gas pipeline manually isolated the mississippi river crossing on the east and west bank. A side scan sonar investigation indicates the pipeline to be broken at approximately 50 feet below the current river level. The sonar data did not have clarity due to the river conditions to determine what may have caused this incident. The pipeline has been abandoned. Cypress gas pipeline made a 48 hour notification update to the nrc, #1179998, on june 1, 2017 at 18:09 updating volume released.

All rights reserved. Copyright © by ClearPHMSA