GD incident on 2017-03-29 — RI

Operator
Niagara Mohawk Power Corp
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$875,000
Incident datetime
2017-03-29 19:59
Report number
Location
RI, PROVIDENCE
Narrative
**supplemental report issued on august 14, 2020 to provide actual environmental remediation costs and to update the apparent cause section, part g3. *** on march 29, 2017 there was an emergency response to an uncontrolled release of gas from 12 inch, 99 psig steel pipeline at 30 allens ave, providence ri this subsequently resulted in unplanned supply interruption. What happened: gas control pressure alarms initiated emergency response with gas instrumentation & regulation (I&r) at 7:59 pm. Ri gas dispatch initiated cms response based on numerous odor calls at 8:05 pm. Providence lng initiated response activities after low pressure reading during rounds at 8:00 pm the release was controlled at 11:16 pm. Cms completed 59 shutoffs at 3:11 am on 3/30/17, c&m completed repairs at 3:30 am on 3/30/17, cms began relights at 3:40 am on 3/30/17. A 12 inch dresser coupling failed by separation allowing two 12 inch 99 psig pipe segments to be pulled apart. Root cause: there was insufficient support of a live gas main due to the fact that the earth was removed during construction activity allowing vibration and pressure to pull the segments out from the coupling. Contributing factors: march, 2017 - enbridge excavated around a pressurized 99 psig outlet main in preparation of tie-in for outlet piping for the newly constructed crary st gate station. The piping was left insufficiently supported in excavation. Removal of two 750 to 99 psig regulator runs allowed a piping header to shift and allow piping to move out of alignment, further adding to the forces acting to pull the segments from the coupling piping change in 2005 utilized unrestrained, short-barrel, insulating dresser couplings use of mechanical coupling; design & material choice unrestrained mechanical coupling used as permanent method of joining two pipe segments. Construction activity around a pressurized 99 psig main conducted with insufficient safeguards. Enbridge proceeded with tie-in excavation while 99 psig main was still in service.
Detailed record list
Occurred At
2017-03-29 19:59:00
Year
2017
Report Received Date
2017-04-28 00:00:00
Iyear
2017.0
Report Number
20170039.0
Supplemental Number
34154.0
Report Type
Supplemental Final
Operator Id
Name
Niagara Mohawk Power Corp
Operator Street Address
300 Erie Boulevard West
Operator City Name
Syracuse
Operator State Abbreviation
NY
Operator Postal Code
13202
Local Datetime
2017-03-29 19:59:00
Location Street Address
30 Allens Avenue
Location City Name
Providence
Location County Name
Providence
Location State Abbreviation
RI
Location Postal Code
02905
Location Latitude
Location Longitude
Nrc Rpt Datetime
2017-03-29 22:56:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
19000.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
30.0
Incident Identified Datetime
2017-03-29 19:59:00
On Site Datetime
2017-03-29 20:39:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Exposed Coupling
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
2005.0
Pipe Diameter
12.0
Pipe Specification
Api 5l X42
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.25
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 4 Location
Est Cost Oper Paid
25000.0
Est Cost Prop Damage
875000.0
Est Cost Emergency
12000.0
Est Cost Other
0.0
Est Cost Unintentional Release
59028.0
Prpty
971028.0
Commercial Affected
53.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
90.0
Normal Psig
90.0
Mop Psig
99.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Controller
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This is a mechanical failure of on exposed pipe not related to any activities within the control room. Controllers actions did not contribute to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Mechanical Joint Failure
Pwjf Failure Type
Mechanical Joint Failure
Mec Fitting Involved
Other Compression Type Fitting
Mec Fitting Invlvd Dtl
Insulating Mechanical Coupling
Mec Fitting Type
Coupling
Mec Manufacturer
Dresser
Mec Fitting Material
Other
Mec Fitting Material Detail
Materials Joined: 1st Steel, 2nd Steel
Additional Other Ind
Yes
Additional Factor Details
Loss Of Support Due To Third Party Encroachment, As Performed By A Conractor Of Enbridge, The Natural Gas Supply Company. This Was Done Outside Of The Public Right Of Way.
Result Construction Ind
Yes
Result Construction Subtype
Procedure Not Followed
Hydrotest Conducted Ind
No
Preparer Name
M****** G********
Preparer Title
Principal Engineer
Preparer Email
M****************@n***********.com
Preparer Telephone
7189635577
Authorizer Name
C****** B*****
Authorizer Title
Prin. Program Mgr Regulatory Management Of Change
Authorizer Telephone
5164924469
Authorizer Email
C*************@n***********.com
Narrative
**supplemental report issued on august 14, 2020 to provide actual environmental remediation costs and to update the apparent cause section, part g3. *** on march 29, 2017 there was an emergency response to an uncontrolled release of gas from 12 inch, 99 psig steel pipeline at 30 allens ave, providence ri this subsequently resulted in unplanned supply interruption. What happened: gas control pressure alarms initiated emergency response with gas instrumentation & regulation (I&r) at 7:59 pm. Ri gas dispatch initiated cms response based on numerous odor calls at 8:05 pm. Providence lng initiated response activities after low pressure reading during rounds at 8:00 pm the release was controlled at 11:16 pm. Cms completed 59 shutoffs at 3:11 am on 3/30/17, c&m completed repairs at 3:30 am on 3/30/17, cms began relights at 3:40 am on 3/30/17. A 12 inch dresser coupling failed by separation allowing two 12 inch 99 psig pipe segments to be pulled apart. Root cause: there was insufficient support of a live gas main due to the fact that the earth was removed during construction activity allowing vibration and pressure to pull the segments out from the coupling. Contributing factors: march, 2017 - enbridge excavated around a pressurized 99 psig outlet main in preparation of tie-in for outlet piping for the newly constructed crary st gate station. The piping was left insufficiently supported in excavation. Removal of two 750 to 99 psig regulator runs allowed a piping header to shift and allow piping to move out of alignment, further adding to the forces acting to pull the segments from the coupling piping change in 2005 utilized unrestrained, short-barrel, insulating dresser couplings use of mechanical coupling; design & material choice unrestrained mechanical coupling used as permanent method of joining two pipe segments. Construction activity around a pressurized 99 psig main conducted with insufficient safeguards. Enbridge proceeded with tie-in excavation while 99 psig main was still in service.
Occurred At 2017-03-29 19:59:00
Year 2017
Report Received Date 2017-04-28 00:00:00
Iyear 2017.0
Report Number 20170039.0
Supplemental Number 34154.0
Report Type Supplemental Final
Operator Id 13480 PHMSA Enforcement
Name Niagara Mohawk Power Corp
Operator Street Address 300 Erie Boulevard West
Operator City Name Syracuse
Operator State Abbreviation NY
Operator Postal Code 13202
Local Datetime 2017-03-29 19:59:00
Location Street Address 30 Allens Avenue
Location City Name Providence
Location County Name Providence
Location State Abbreviation RI
Location Postal Code 02905
Location Latitude 41.813932 Google Maps OpenStreetMap
Location Longitude -71.406001 Google Maps OpenStreetMap
Nrc Rpt Datetime 2017-03-29 22:56:00
Nrc Rpt Num 1174380 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 19000.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 30.0
Incident Identified Datetime 2017-03-29 19:59:00
On Site Datetime 2017-03-29 20:39:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Exposed Coupling
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 2005.0
Pipe Diameter 12.0
Pipe Specification Api 5l X42
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.25
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 4 Location
Est Cost Oper Paid 25000.0
Est Cost Prop Damage 875000.0
Est Cost Emergency 12000.0
Est Cost Other 0.0
Est Cost Unintentional Release 59028.0
Prpty 971028.0
Commercial Affected 53.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 90.0
Normal Psig 90.0
Mop Psig 99.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Controller
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This is a mechanical failure of on exposed pipe not related to any activities within the control room. Controllers actions did not contribute to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Mechanical Joint Failure
Pwjf Failure Type Mechanical Joint Failure
Mec Fitting Involved Other Compression Type Fitting
Mec Fitting Invlvd Dtl Insulating Mechanical Coupling
Mec Fitting Type Coupling
Mec Manufacturer Dresser
Mec Fitting Material Other
Mec Fitting Material Detail Materials Joined: 1st Steel, 2nd Steel
Additional Other Ind Yes
Additional Factor Details Loss Of Support Due To Third Party Encroachment, As Performed By A Conractor Of Enbridge, The Natural Gas Supply Company. This Was Done Outside Of The Public Right Of Way.
Result Construction Ind Yes
Result Construction Subtype Procedure Not Followed
Hydrotest Conducted Ind No
Preparer Name M****** G********
Preparer Title Principal Engineer
Preparer Email M****************@n***********.com
Preparer Telephone 7189635577
Authorizer Name C****** B*****
Authorizer Title Prin. Program Mgr Regulatory Management Of Change
Authorizer Telephone 5164924469
Authorizer Email C*************@n***********.com
Narrative **supplemental report issued on august 14, 2020 to provide actual environmental remediation costs and to update the apparent cause section, part g3. *** on march 29, 2017 there was an emergency response to an uncontrolled release of gas from 12 inch, 99 psig steel pipeline at 30 allens ave, providence ri this subsequently resulted in unplanned supply interruption. What happened: gas control pressure alarms initiated emergency response with gas instrumentation & regulation (I&r) at 7:59 pm. Ri gas dispatch initiated cms response based on numerous odor calls at 8:05 pm. Providence lng initiated response activities after low pressure reading during rounds at 8:00 pm the release was controlled at 11:16 pm. Cms completed 59 shutoffs at 3:11 am on 3/30/17, c&m completed repairs at 3:30 am on 3/30/17, cms began relights at 3:40 am on 3/30/17. A 12 inch dresser coupling failed by separation allowing two 12 inch 99 psig pipe segments to be pulled apart. Root cause: there was insufficient support of a live gas main due to the fact that the earth was removed during construction activity allowing vibration and pressure to pull the segments out from the coupling. Contributing factors: march, 2017 - enbridge excavated around a pressurized 99 psig outlet main in preparation of tie-in for outlet piping for the newly constructed crary st gate station. The piping was left insufficiently supported in excavation. Removal of two 750 to 99 psig regulator runs allowed a piping header to shift and allow piping to move out of alignment, further adding to the forces acting to pull the segments from the coupling piping change in 2005 utilized unrestrained, short-barrel, insulating dresser couplings use of mechanical coupling; design & material choice unrestrained mechanical coupling used as permanent method of joining two pipe segments. Construction activity around a pressurized 99 psig main conducted with insufficient safeguards. Enbridge proceeded with tie-in excavation while 99 psig main was still in service.

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