GD incident on 2017-03-24 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$129,445
Incident datetime
2017-03-24 11:30
Report number
Location
TX, TARRANT
Narrative
Atmos energy received prior notification of the excavation activity and marked the location of the line. On march 24, 2017 at approximately 11:30, the third party contractor failed to expose the active pipe prior to boring and bored into an electric conduit then into a 12" gas line/main. Gas then migrated into the electric conduit, traveling up a pole and igniting. A representative from the city of fort worth was at the location when the incident occurred and immediately notified atmos energy. The line was shutdown at 22:13 on march 24, 2017 so repairs could commence. Approximately 300 people were evacuated from nearby housing. Repairs were completed and the pipeline restarted at 19:15 on march 25, 2017. The national response center report number indicated on the original incident report, 1174102, was incorrect. The report number has been changed on this supplemental report to the correct number, 1174002.
Detailed record list
Occurred At
2017-03-24 11:30:00
Year
2017
Report Received Date
2017-04-21 00:00:00
Iyear
2017.0
Report Number
20170036.0
Supplemental Number
31845.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5420 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2017-03-24 11:30:00
Location Street Address
200 Block Of Pecan St.
Location City Name
Fort Worth
Location County Name
Tarrant
Location State Abbreviation
TX
Location Postal Code
76102
Location Latitude
Location Longitude
Nrc Rpt Datetime
2017-03-24 12:10:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
5408.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
300.0
Incident Identified Datetime
2017-03-24 11:30:00
On Site Datetime
2017-03-24 11:45:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
96.0
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Bored/drilled
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
2003.0
Pipe Diameter
12.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Driscoplex
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11.5
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
3.0
Puncture Circum
3.0
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
129445.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
30296.0
Prpty
159741.0
Commercial Affected
7.0
Industrial Affected
0.0
Residences Affected
55.0
Accident Psig
28.0
Normal Psig
28.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Boring
Work Performed
Telecommunications
One Call Notified Ind
Yes
One Call Ticket Num
1757295504
One Call Center Name
Texas811
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
22.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
S**** K****
Preparer Title
Field Supervisor
Preparer Email
W************@a**********.com
Preparer Telephone
469-261-2011
Preparer Fax
817-517-2088
Authorizer Name
M**** S*****
Authorizer Title
Director Regulatory And Compliance
Authorizer Telephone
214-206-2033
Authorizer Email
M***********@a**********.com
Narrative
Atmos energy received prior notification of the excavation activity and marked the location of the line. On march 24, 2017 at approximately 11:30, the third party contractor failed to expose the active pipe prior to boring and bored into an electric conduit then into a 12" gas line/main. Gas then migrated into the electric conduit, traveling up a pole and igniting. A representative from the city of fort worth was at the location when the incident occurred and immediately notified atmos energy. The line was shutdown at 22:13 on march 24, 2017 so repairs could commence. Approximately 300 people were evacuated from nearby housing. Repairs were completed and the pipeline restarted at 19:15 on march 25, 2017. The national response center report number indicated on the original incident report, 1174102, was incorrect. The report number has been changed on this supplemental report to the correct number, 1174002.
Occurred At 2017-03-24 11:30:00
Year 2017
Report Received Date 2017-04-21 00:00:00
Iyear 2017.0
Report Number 20170036.0
Supplemental Number 31845.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5420 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2017-03-24 11:30:00
Location Street Address 200 Block Of Pecan St.
Location City Name Fort Worth
Location County Name Tarrant
Location State Abbreviation TX
Location Postal Code 76102
Location Latitude 32.75828 Google Maps OpenStreetMap
Location Longitude -97.32871 Google Maps OpenStreetMap
Nrc Rpt Datetime 2017-03-24 12:10:00
Nrc Rpt Num 1174002 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 5408.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 300.0
Incident Identified Datetime 2017-03-24 11:30:00
On Site Datetime 2017-03-24 11:45:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 96.0
Crossing Yes
Road Crossing Ind Yes
Road Type Bored/drilled
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 2003.0
Pipe Diameter 12.0
Pipe Specification Astm D2513
Pipe Manufacturer Driscoplex
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11.5
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 3.0
Puncture Circum 3.0
Class Location Type Class 4 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 129445.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Est Cost Unintentional Release 30296.0
Prpty 159741.0
Commercial Affected 7.0
Industrial Affected 0.0
Residences Affected 55.0
Accident Psig 28.0
Normal Psig 28.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Boring
Work Performed Telecommunications
One Call Notified Ind Yes
One Call Ticket Num 1757295504
One Call Center Name Texas811
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 22.0
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name S**** K****
Preparer Title Field Supervisor
Preparer Email W************@a**********.com
Preparer Telephone 469-261-2011
Preparer Fax 817-517-2088
Authorizer Name M**** S*****
Authorizer Title Director Regulatory And Compliance
Authorizer Telephone 214-206-2033
Authorizer Email M***********@a**********.com
Narrative Atmos energy received prior notification of the excavation activity and marked the location of the line. On march 24, 2017 at approximately 11:30, the third party contractor failed to expose the active pipe prior to boring and bored into an electric conduit then into a 12" gas line/main. Gas then migrated into the electric conduit, traveling up a pole and igniting. A representative from the city of fort worth was at the location when the incident occurred and immediately notified atmos energy. The line was shutdown at 22:13 on march 24, 2017 so repairs could commence. Approximately 300 people were evacuated from nearby housing. Repairs were completed and the pipeline restarted at 19:15 on march 25, 2017. The national response center report number indicated on the original incident report, 1174102, was incorrect. The report number has been changed on this supplemental report to the correct number, 1174002.

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