GTG incident on 2017-02-14 — TX

Operator
Columbia Gas Transmission, Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500,000
Incident datetime
2017-02-14 10:32
Report number
Location
TX
Narrative
On february 14, 2017 an odor of gas complaint was called in at 09:54 am to the local distribution company (columbia gas of kentucky) monitoring center by a landowner on harper ridge road. The ldc monitoring center dispatched an employee who arrived at the site at approximately 10:13 am. After assessing the situation, the ldc employee notified the ldc monitoring center to alert the fire department and called a columbia gas transmission llc employee at 10:20am. The columbia gas transmission employee responded and notified the columbia gas transmission monitoring center at 10:32 am of the potential leak. The employee arrived on site at 10:45 am and determined that the leak was on 30" line em-7 owned and operated by columbia gas transmission llc. Columbia gas transmission field employees were notified and responded. The local fire department also responded and evacuated 6 families. Columbia gas transmission called the national response center at 11:39 am on february 14, 2017, and was placed on hold until 12:01 pm. The pipeline was removed from service. The pipeline was excavated and a crack found on a weld elbow fitting near a girth weld. The pipeline was repaired with replacement pipe and an weld elbow fitting, and placed back into service on february 20, 2017. The metallurgical and geotechnical analyses have been provided to PHMSA.
Detailed record list
Report Received Date
2017-03-14 00:00:00
Iyear
2017
Report Number
20170022
Supplemental Number
17348
Report Type
Supplemental Final
Operator Id
Name
Columbia Gas Transmission, Llc
Operator Street Address
700 Louisiana St. Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-02-14 09:54:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2017-02-14 11:39:00
Commodity Released Type
Natural Gas
Unintentional Release
15024
Intentional Release
17362
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-02-14 12:35:00
Restart Datetime
2017-02-20 21:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
19
Incident Identified Datetime
2017-02-14 10:32:00
On Site Datetime
2017-02-14 10:45:00
On Off Shore
Onshore
Onshore State Abbreviation
Ky
Onshore Postal Code
40353
Onshore City Name
Not Within A Municipality
Onshore County Name
Montgomery
Designated Location
Survey Station No.
Designated Name
500+33
Pipe Fac Name
Line Em-7
Segment Name
Line Em-7
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
120
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
30
Pipe Wall Thickness
0.312
Pipe Smys
65000
Pipe Specification
X-65
Pipe Seam Type
Dsaw
Pipe Manufacturer
Republic
Pipe Coating Type
Epoxy
Installation Year
1969
Manufactured Year
1969
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 2 Location
Could Be Hca
No
Pir Radius
752
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
20000
Est Cost Unintentional Release
47486
Est Cost Intentional Release
54864
Est Cost Prop Damage
500000
Est Cost Emergency
0
Est Cost Other
100000
Est Cost Other Details
Other Costs Include Geotechnical And Metallurgical Investigations.
Prpty
722350
Accident Psig
790
Mop Psig
1000
Mop Cfr Section
192.619(A)(2)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
73656
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Notification From Public
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
3
Num Employees Failed
0
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Pwjf Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Mechanical Stress
Yes
Additional Crack Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D**** A*******
Preparer Title
Regulatory Specialist
Preparer Email
D*************@t**********.com
Preparer Telephone
724-223-2766
Authorizer Name
H***** L** R*****
Authorizer Title
Manager
Authorizer Telephone
832-320-5215
Authorizer Email
L*********@t**********.com
Narrative
On february 14, 2017 an odor of gas complaint was called in at 09:54 am to the local distribution company (columbia gas of kentucky) monitoring center by a landowner on harper ridge road. The ldc monitoring center dispatched an employee who arrived at the site at approximately 10:13 am. After assessing the situation, the ldc employee notified the ldc monitoring center to alert the fire department and called a columbia gas transmission llc employee at 10:20am. The columbia gas transmission employee responded and notified the columbia gas transmission monitoring center at 10:32 am of the potential leak. The employee arrived on site at 10:45 am and determined that the leak was on 30" line em-7 owned and operated by columbia gas transmission llc. Columbia gas transmission field employees were notified and responded. The local fire department also responded and evacuated 6 families. Columbia gas transmission called the national response center at 11:39 am on february 14, 2017, and was placed on hold until 12:01 pm. The pipeline was removed from service. The pipeline was excavated and a crack found on a weld elbow fitting near a girth weld. The pipeline was repaired with replacement pipe and an weld elbow fitting, and placed back into service on february 20, 2017. The metallurgical and geotechnical analyses have been provided to PHMSA.
Report Received Date 2017-03-14 00:00:00
Iyear 2017
Report Number 20170022
Supplemental Number 17348
Report Type Supplemental Final
Operator Id 2616 PHMSA Enforcement
Name Columbia Gas Transmission, Llc
Operator Street Address 700 Louisiana St. Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-02-14 09:54:00
Location Latitude 38.06107 Google Maps OpenStreetMap
Location Longitude -83.8596 Google Maps OpenStreetMap
Nrc Rpt Num 1171048 NRC Report How to search
Nrc Rpt Datetime 2017-02-14 11:39:00
Commodity Released Type Natural Gas
Unintentional Release 15024
Intentional Release 17362
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-02-14 12:35:00
Restart Datetime 2017-02-20 21:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 19
Incident Identified Datetime 2017-02-14 10:32:00
On Site Datetime 2017-02-14 10:45:00
On Off Shore Onshore
Onshore State Abbreviation Ky
Onshore Postal Code 40353
Onshore City Name Not Within A Municipality
Onshore County Name Montgomery
Designated Location Survey Station No.
Designated Name 500+33
Pipe Fac Name Line Em-7
Segment Name Line Em-7
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 120
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 30
Pipe Wall Thickness 0.312
Pipe Smys 65000
Pipe Specification X-65
Pipe Seam Type Dsaw
Pipe Manufacturer Republic
Pipe Coating Type Epoxy
Installation Year 1969
Manufactured Year 1969
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Class Location Type Class 2 Location
Could Be Hca No
Pir Radius 752
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 20000
Est Cost Unintentional Release 47486
Est Cost Intentional Release 54864
Est Cost Prop Damage 500000
Est Cost Emergency 0
Est Cost Other 100000
Est Cost Other Details Other Costs Include Geotechnical And Metallurgical Investigations.
Prpty 722350
Accident Psig 790
Mop Psig 1000
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 73656
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Notification From Public
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 3
Num Employees Failed 0
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Pwjf Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind Yes
Mechanical Stress Yes
Additional Crack Ind Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name D**** A*******
Preparer Title Regulatory Specialist
Preparer Email D*************@t**********.com
Preparer Telephone 724-223-2766
Authorizer Name H***** L** R*****
Authorizer Title Manager
Authorizer Telephone 832-320-5215
Authorizer Email L*********@t**********.com
Narrative On february 14, 2017 an odor of gas complaint was called in at 09:54 am to the local distribution company (columbia gas of kentucky) monitoring center by a landowner on harper ridge road. The ldc monitoring center dispatched an employee who arrived at the site at approximately 10:13 am. After assessing the situation, the ldc employee notified the ldc monitoring center to alert the fire department and called a columbia gas transmission llc employee at 10:20am. The columbia gas transmission employee responded and notified the columbia gas transmission monitoring center at 10:32 am of the potential leak. The employee arrived on site at 10:45 am and determined that the leak was on 30" line em-7 owned and operated by columbia gas transmission llc. Columbia gas transmission field employees were notified and responded. The local fire department also responded and evacuated 6 families. Columbia gas transmission called the national response center at 11:39 am on february 14, 2017, and was placed on hold until 12:01 pm. The pipeline was removed from service. The pipeline was excavated and a crack found on a weld elbow fitting near a girth weld. The pipeline was repaired with replacement pipe and an weld elbow fitting, and placed back into service on february 20, 2017. The metallurgical and geotechnical analyses have been provided to PHMSA.

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