GD incident on 2017-01-19 — WA

Operator
Cascade Natural Gas Corp
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$365
Incident datetime
2017-01-19 07:24
Report number
Location
WA, CHELAN
Narrative
The cascade natural gas corporation (cngc) pipeline affected was a 2" steel main that was installed in 1967. The pipeline separated at a girth weld causing the unintentional release of more than 3 million cubic feet of gas, total gas loss was estimated to be 3,875 mcf. The area in which the release occurred was experiencing extreme cold weather and substantial underground frost. The damage to the pipeline observed was consistent with damage caused by frost heave. Frost heave is thought to be a contributing factor to the release. The separated girth weld was retained by cngc and underwent an examination by qualified staff. The examination concluded that the weld had failed and cngc classified the leak as a "pipe, weld or joint failure" as a result. The sub cause was determined to be a construction defect caused by poor workmanship. Cngc worked closely with emergency responders and quickly mobilized resources and equipment to ensure public safety. No injuries, damage to property (other than cngc pipeline) or ignition occurred.
Detailed record list
Occurred At
2017-01-19 07:24:00
Year
2017
Report Received Date
2017-02-06 00:00:00
Iyear
2017.0
Report Number
20170015.0
Supplemental Number
16512.0
Report Type
Supplemental Final
Operator Id
Name
Cascade Natural Gas Corp
Operator Street Address
8113 W. Grandridge Blvd
Operator City Name
Kennewick
Operator State Abbreviation
WA
Operator Postal Code
99336
Local Datetime
2017-01-19 18:24:00
Location Street Address
1317 South Hills Drive
Location City Name
Wenatchee
Location County Name
Chelan
Location State Abbreviation
WA
Location Postal Code
98801-1985
Location Latitude
Location Longitude
Nrc Rpt Datetime
2017-01-23 14:11:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
3875.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2017-01-19 07:24:00
On Site Datetime
2017-01-19 07:50:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
34.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1967.0
Pipe Diameter
2.375
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.154
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
6.5
Rupture Width
2.1
Class Location Type
Class 3 Location
Est Cost Oper Paid
2000.0
Est Cost Prop Damage
365.0
Est Cost Emergency
7642.0
Est Cost Other
0.0
Est Cost Unintentional Release
20000.0
Prpty
30007.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Accident Psig
54.0
Normal Psig
54.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Butt Weld
Pwjf Failure Type
Butt Weld
Butt Weld Subtype
Pipe
Additional Other Ind
Yes
Additional Factor Details
None
Result Construction Ind
Yes
Result Construction Subtype
Poor Workmanship
Hydrotest Conducted Ind
No
Preparer Name
C**** G******
Preparer Title
Manager Standards And Compliance
Preparer Email
C******************@c***.com
Preparer Telephone
509-531-6427
Authorizer Name
M*** E*****
Authorizer Title
Director Operation Services
Authorizer Telephone
509-734-4576
Authorizer Email
M**********@c***.com
Narrative
The cascade natural gas corporation (cngc) pipeline affected was a 2" steel main that was installed in 1967. The pipeline separated at a girth weld causing the unintentional release of more than 3 million cubic feet of gas, total gas loss was estimated to be 3,875 mcf. The area in which the release occurred was experiencing extreme cold weather and substantial underground frost. The damage to the pipeline observed was consistent with damage caused by frost heave. Frost heave is thought to be a contributing factor to the release. The separated girth weld was retained by cngc and underwent an examination by qualified staff. The examination concluded that the weld had failed and cngc classified the leak as a "pipe, weld or joint failure" as a result. The sub cause was determined to be a construction defect caused by poor workmanship. Cngc worked closely with emergency responders and quickly mobilized resources and equipment to ensure public safety. No injuries, damage to property (other than cngc pipeline) or ignition occurred.
Occurred At 2017-01-19 07:24:00
Year 2017
Report Received Date 2017-02-06 00:00:00
Iyear 2017.0
Report Number 20170015.0
Supplemental Number 16512.0
Report Type Supplemental Final
Operator Id 2128 PHMSA Enforcement
Name Cascade Natural Gas Corp
Operator Street Address 8113 W. Grandridge Blvd
Operator City Name Kennewick
Operator State Abbreviation WA
Operator Postal Code 99336
Local Datetime 2017-01-19 18:24:00
Location Street Address 1317 South Hills Drive
Location City Name Wenatchee
Location County Name Chelan
Location State Abbreviation WA
Location Postal Code 98801-1985
Location Latitude 47.405795 Google Maps OpenStreetMap
Location Longitude -120.332825 Google Maps OpenStreetMap
Nrc Rpt Datetime 2017-01-23 14:11:00
Nrc Rpt Num 1169311 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 3875.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2017-01-19 07:24:00
On Site Datetime 2017-01-19 07:50:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 34.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 1967.0
Pipe Diameter 2.375
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.154
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 6.5
Rupture Width 2.1
Class Location Type Class 3 Location
Est Cost Oper Paid 2000.0
Est Cost Prop Damage 365.0
Est Cost Emergency 7642.0
Est Cost Other 0.0
Est Cost Unintentional Release 20000.0
Prpty 30007.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 1.0
Accident Psig 54.0
Normal Psig 54.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Butt Weld
Pwjf Failure Type Butt Weld
Butt Weld Subtype Pipe
Additional Other Ind Yes
Additional Factor Details None
Result Construction Ind Yes
Result Construction Subtype Poor Workmanship
Hydrotest Conducted Ind No
Preparer Name C**** G******
Preparer Title Manager Standards And Compliance
Preparer Email C******************@c***.com
Preparer Telephone 509-531-6427
Authorizer Name M*** E*****
Authorizer Title Director Operation Services
Authorizer Telephone 509-734-4576
Authorizer Email M**********@c***.com
Narrative The cascade natural gas corporation (cngc) pipeline affected was a 2" steel main that was installed in 1967. The pipeline separated at a girth weld causing the unintentional release of more than 3 million cubic feet of gas, total gas loss was estimated to be 3,875 mcf. The area in which the release occurred was experiencing extreme cold weather and substantial underground frost. The damage to the pipeline observed was consistent with damage caused by frost heave. Frost heave is thought to be a contributing factor to the release. The separated girth weld was retained by cngc and underwent an examination by qualified staff. The examination concluded that the weld had failed and cngc classified the leak as a "pipe, weld or joint failure" as a result. The sub cause was determined to be a construction defect caused by poor workmanship. Cngc worked closely with emergency responders and quickly mobilized resources and equipment to ensure public safety. No injuries, damage to property (other than cngc pipeline) or ignition occurred.

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