HL incident on 2016-11-30 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2016-11-30 07:30
Report number
Location
GA
Narrative
On 11/30/16, at 07:30 an employee performing duties in the station yard smelled gasoline odors and, upon investigation, discovered a product sheen on an area drainage ditch and on one of the facility retention ponds. He immediately notified the lead operator who subsequently notified the operations manager. Other employees and contractors responded and started source investigation as well as product containment and recovery including placing absorbent and containment boom across the retention pond. All spilled product remained on facility property. During these activities, other personnel identified the release source as the line 1 takeoff control valve. The line 1 delivery was shut down and the segment was isolated at approximately 07:57 which stopped the leak. The segment was drained up and technicians replaced the control valve packing ("rope" packing). Final repairs were completed at 11:40 and the delivery line was restarted at 12:18. The parish lepc, state of la and nrc were each notified and a courtesy call was made to PHMSA southern and southwestern regional offices.
Detailed record list
Report Received Date
2016-12-27 00:00:00
Iyear
2016
Report Number
20160428
Supplemental Number
21988
Report Type
Original Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2016-11-30 05:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
5.1
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-11-30 07:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-11-30 08:57:00
Restart Datetime
2016-11-30 13:18:00
On Site Datetime
2016-11-30 07:30:00
Nrc Rpt Datetime
2016-11-30 10:36:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Baton Rouge Junction
Segment Name
Line 1 Takeoff Control Valve
Onshore State Abbreviation
La
Onshore Postal Code
70748
Onshore City Name
Jackson
Onshore County Name
East Feliciana
Designated Location
Milepost/valve Station
Designated Name
222
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1976
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
300
Est Cost Prop Damage
5000
Est Cost Emergency
25000
Est Cost Environmental
20000
Est Cost Other
0
Prpty
50300
Accident Psig
34
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller and/or control room issues were not factors that caused or contributed to this incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Age/fatigue Of Packing Material
Preparer Name
K**** M****
Preparer Title
Compliance Coordinator
Preparer Email
K*****@c******.com
Preparer Telephone
601-765-9168
Preparer Fax
770-754-8489
Prepared Date
2016-12-27 00:00:00
Authorizer Name
D*** L*****
Authorizer Telephone
678-7622872
Authorizer Title
Acting Director Compliance
Authorizer Email
D******@c******.com
Narrative
On 11/30/16, at 07:30 an employee performing duties in the station yard smelled gasoline odors and, upon investigation, discovered a product sheen on an area drainage ditch and on one of the facility retention ponds. He immediately notified the lead operator who subsequently notified the operations manager. Other employees and contractors responded and started source investigation as well as product containment and recovery including placing absorbent and containment boom across the retention pond. All spilled product remained on facility property. During these activities, other personnel identified the release source as the line 1 takeoff control valve. The line 1 delivery was shut down and the segment was isolated at approximately 07:57 which stopped the leak. The segment was drained up and technicians replaced the control valve packing ("rope" packing). Final repairs were completed at 11:40 and the delivery line was restarted at 12:18. The parish lepc, state of la and nrc were each notified and a courtesy call was made to PHMSA southern and southwestern regional offices.
Report Received Date 2016-12-27 00:00:00
Iyear 2016
Report Number 20160428
Supplemental Number 21988
Report Type Original Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2016-11-30 05:30:00
Location Latitude 30.713929 Google Maps OpenStreetMap
Location Longitude -91.275048 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 5.1
Recovered Bbls 5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-11-30 07:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-11-30 08:57:00
Restart Datetime 2016-11-30 13:18:00
On Site Datetime 2016-11-30 07:30:00
Nrc Rpt Datetime 2016-11-30 10:36:00
Nrc Rpt Num 1165254 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Baton Rouge Junction
Segment Name Line 1 Takeoff Control Valve
Onshore State Abbreviation La
Onshore Postal Code 70748
Onshore City Name Jackson
Onshore County Name East Feliciana
Designated Location Milepost/valve Station
Designated Name 222
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1976
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 300
Est Cost Prop Damage 5000
Est Cost Emergency 25000
Est Cost Environmental 20000
Est Cost Other 0
Prpty 50300
Accident Psig 34
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller and/or control room issues were not factors that caused or contributed to this incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Age/fatigue Of Packing Material
Preparer Name K**** M****
Preparer Title Compliance Coordinator
Preparer Email K*****@c******.com
Preparer Telephone 601-765-9168
Preparer Fax 770-754-8489
Prepared Date 2016-12-27 00:00:00
Authorizer Name D*** L*****
Authorizer Telephone 678-7622872
Authorizer Title Acting Director Compliance
Authorizer Email D******@c******.com
Narrative On 11/30/16, at 07:30 an employee performing duties in the station yard smelled gasoline odors and, upon investigation, discovered a product sheen on an area drainage ditch and on one of the facility retention ponds. He immediately notified the lead operator who subsequently notified the operations manager. Other employees and contractors responded and started source investigation as well as product containment and recovery including placing absorbent and containment boom across the retention pond. All spilled product remained on facility property. During these activities, other personnel identified the release source as the line 1 takeoff control valve. The line 1 delivery was shut down and the segment was isolated at approximately 07:57 which stopped the leak. The segment was drained up and technicians replaced the control valve packing ("rope" packing). Final repairs were completed at 11:40 and the delivery line was restarted at 12:18. The parish lepc, state of la and nrc were each notified and a courtesy call was made to PHMSA southern and southwestern regional offices.

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