HL incident on 2016-11-16 — KS

Operator
Jayhawk Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2016-11-16 11:38
Report number
Location
KS
Narrative
This release was a result of the failure of an insulating gasket. The gasket was installed on may 9, 2016 by oq qualified jayhawk employees. Valve replacement was the only scope of work the crew was performing at the time. Per the incident investigation, the crew followed the existing procedures for bolted flanges, however, the installation of the new valve eliminated the valve's contact with the existing support. Jayhawk has completed the incident investigation and determined the root cause of the incident to be inadequate pipe support spacing with a possible contributing factor of inadequate flange torque. Jayhawk is in the process of evaluating mainline pipe support spacing and reviewing the need to incorporate torque specifications into existing procedures. The total product lost from the pipeline was 72 barrels. 41 barrels of free product were recovered and the 31 barrel balance was cleaned up with approximately 286 cubic yards of contaminated material being placed on an existing remediation plot.
Detailed record list
Report Received Date
2016-12-15 00:00:00
Iyear
2016
Report Number
20160417
Supplemental Number
23193
Report Type
Supplemental Final
Operator Id
Name
Jayhawk Pipeline Llc
Operator Street Address
2000 S. Main
Operator City Name
Mcpherson
Operator State Abbreviation
KS
Operator Postal Code
67460
Local Datetime
2016-11-16 11:38:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
72
Recovered Bbls
72
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-11-16 11:38:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-11-16 11:38:00
Restart Datetime
2016-11-16 16:20:00
On Site Datetime
2016-11-16 11:38:00
Nrc Rpt Datetime
2016-11-16 12:38:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Chase Station
Segment Name
Chase To Mcpherson
Onshore State Abbreviation
Ks
Onshore Postal Code
67524
Onshore City Name
Not Within A Municipality
Onshore County Name
Rice
Designated Location
Milepost/valve Station
Designated Name
Chase Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2016
Material Involved
Material Other Than Carbon Steel
Material Details
Insulating Gasket
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1178
Est Cost Prop Damage
1000
Est Cost Emergency
1500
Est Cost Environmental
2500
Est Cost Other
5000
Est Cost Other Details
Management Response, Travel, Phmsa Reporting, Etc.
Prpty
11178
Accident Psig
1023
Mop Psig
1293
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak did not trigger leak detection alarms nor provide adequate information to trigger the controller to take action, given the information available.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Support Ind
Yes
Preparer Name
M******* S*****
Preparer Title
Manager Dot Compliance
Preparer Email
M**************@c*****.com
Preparer Telephone
4068619284
Preparer Fax
4066285393
Prepared Date
2018-02-28 00:00:00
Authorizer Name
R****** S* P*******
Authorizer Telephone
6202419240
Authorizer Title
Vp Pipelines And Terminals
Authorizer Email
R***************@c*****.com
Narrative
This release was a result of the failure of an insulating gasket. The gasket was installed on may 9, 2016 by oq qualified jayhawk employees. Valve replacement was the only scope of work the crew was performing at the time. Per the incident investigation, the crew followed the existing procedures for bolted flanges, however, the installation of the new valve eliminated the valve's contact with the existing support. Jayhawk has completed the incident investigation and determined the root cause of the incident to be inadequate pipe support spacing with a possible contributing factor of inadequate flange torque. Jayhawk is in the process of evaluating mainline pipe support spacing and reviewing the need to incorporate torque specifications into existing procedures. The total product lost from the pipeline was 72 barrels. 41 barrels of free product were recovered and the 31 barrel balance was cleaned up with approximately 286 cubic yards of contaminated material being placed on an existing remediation plot.
Report Received Date 2016-12-15 00:00:00
Iyear 2016
Report Number 20160417
Supplemental Number 23193
Report Type Supplemental Final
Operator Id 9175 PHMSA Enforcement
Name Jayhawk Pipeline Llc
Operator Street Address 2000 S. Main
Operator City Name Mcpherson
Operator State Abbreviation KS
Operator Postal Code 67460
Local Datetime 2016-11-16 11:38:00
Location Latitude 38.340005 Google Maps OpenStreetMap
Location Longitude -98.311832 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 72
Recovered Bbls 72
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-11-16 11:38:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-11-16 11:38:00
Restart Datetime 2016-11-16 16:20:00
On Site Datetime 2016-11-16 11:38:00
Nrc Rpt Datetime 2016-11-16 12:38:00
Nrc Rpt Num 1164284 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Chase Station
Segment Name Chase To Mcpherson
Onshore State Abbreviation Ks
Onshore Postal Code 67524
Onshore City Name Not Within A Municipality
Onshore County Name Rice
Designated Location Milepost/valve Station
Designated Name Chase Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 2016
Material Involved Material Other Than Carbon Steel
Material Details Insulating Gasket
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1178
Est Cost Prop Damage 1000
Est Cost Emergency 1500
Est Cost Environmental 2500
Est Cost Other 5000
Est Cost Other Details Management Response, Travel, Phmsa Reporting, Etc.
Prpty 11178
Accident Psig 1023
Mop Psig 1293
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak did not trigger leak detection alarms nor provide adequate information to trigger the controller to take action, given the information available.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Support Ind Yes
Preparer Name M******* S*****
Preparer Title Manager Dot Compliance
Preparer Email M**************@c*****.com
Preparer Telephone 4068619284
Preparer Fax 4066285393
Prepared Date 2018-02-28 00:00:00
Authorizer Name R****** S* P*******
Authorizer Telephone 6202419240
Authorizer Title Vp Pipelines And Terminals
Authorizer Email R***************@c*****.com
Narrative This release was a result of the failure of an insulating gasket. The gasket was installed on may 9, 2016 by oq qualified jayhawk employees. Valve replacement was the only scope of work the crew was performing at the time. Per the incident investigation, the crew followed the existing procedures for bolted flanges, however, the installation of the new valve eliminated the valve's contact with the existing support. Jayhawk has completed the incident investigation and determined the root cause of the incident to be inadequate pipe support spacing with a possible contributing factor of inadequate flange torque. Jayhawk is in the process of evaluating mainline pipe support spacing and reviewing the need to incorporate torque specifications into existing procedures. The total product lost from the pipeline was 72 barrels. 41 barrels of free product were recovered and the 31 barrel balance was cleaned up with approximately 286 cubic yards of contaminated material being placed on an existing remediation plot.

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