HL incident on 2016-11-15 — TX

Operator
Enterprise Products Operating Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$127,747
Incident datetime
2016-11-15 16:46
Report number
Location
TX
Narrative
On november 15, 2016 a welding crew was finishing the final weld of a type b in-service reinforcement sleeve at mp 647.7 on the p62 pipeline. At approximately 16:46 a flash fire occurred from the area between the external sleeve and the line pipe. The flash was reported as 3" in length and similar to a pilot light in flame size and intensity. The crew shut down work, notified pipeline control, and began monitoring the area. At that time, the source of the lel was suspected to be from the bondo curing under the sleeve and not from an active leak. The site was monitored throughout the night to determine the source of the lel. On november 16, 2016 at 10:01 the source of the lel was confirmed to be from a leak under the b sleeve, and the nrc was notified at 10:39. The pipe was repaired with the installation of an oversleeve and was returned to normal operation november 30, 2016.
Detailed record list
Report Received Date
2016-12-14 00:00:00
Iyear
2016
Report Number
20160415
Supplemental Number
22256
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-11-15 16:46:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane
Unintentional Release Bbls
0.1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2016-11-15 16:46:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Repair Method Did Not Necessitate Shutdown
On Site Datetime
2016-11-15 16:46:00
Nrc Rpt Datetime
2016-11-16 10:39:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Seymour To Beaumont (Atex)
Segment Name
P62
Onshore State Abbreviation
Il
Onshore Postal Code
62917
Onshore City Name
Brushy Township
Onshore County Name
Saline
Designated Location
Milepost/valve Station
Designated Name
647.7
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
46
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
16
Pipe Wall Thickness
0.267
Pipe Smys
60000
Pipe Specification
Api-5l-X-60
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
U.s. Steel
Pipe Coating Type
Other
Pipe Coating Details
Tape Coating
Weld Subtype
Pipe Girth Weld
Installation Year
1974
Manufactured Year
1974
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1
Est Cost Prop Damage
127747
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
127748
Accident Psig
799
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Not Mandated
Length Segment Isolated
65630
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Mechanical Stress
Yes
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Emat Ind
Yes
Other Tool Tech Ind
Yes
Axial Recent Year
2016
Geometry Recent Year
2016
Emat Recent Year
2016
Other Tool
Emat
Other Recent Year
2016
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1979
Hydrtst Most Rcnt Pressure
2001
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Handl Ultrasonic Rcnt Year
2016
Exm Wet Mgnt Partcl Rcnt Year
2016
Exm Handl Ultrasonic Rcnt Ind
Yes
Exm Wet Mgnt Partcl Rcnt Ind
Yes
Preparer Name
E**** W*******
Preparer Title
Pipeline Compliance Engineer
Preparer Email
E********@e****.com
Preparer Telephone
713-381-5757
Prepared Date
2017-04-07 00:00:00
Authorizer Name
E**** W*******
Authorizer Telephone
713-381-5757
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
E********@e****.com
Narrative
On november 15, 2016 a welding crew was finishing the final weld of a type b in-service reinforcement sleeve at mp 647.7 on the p62 pipeline. At approximately 16:46 a flash fire occurred from the area between the external sleeve and the line pipe. The flash was reported as 3" in length and similar to a pilot light in flame size and intensity. The crew shut down work, notified pipeline control, and began monitoring the area. At that time, the source of the lel was suspected to be from the bondo curing under the sleeve and not from an active leak. The site was monitored throughout the night to determine the source of the lel. On november 16, 2016 at 10:01 the source of the lel was confirmed to be from a leak under the b sleeve, and the nrc was notified at 10:39. The pipe was repaired with the installation of an oversleeve and was returned to normal operation november 30, 2016.
Report Received Date 2016-12-14 00:00:00
Iyear 2016
Report Number 20160415
Supplemental Number 22256
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-11-15 16:46:00
Location Latitude 37.745816 Google Maps OpenStreetMap
Location Longitude -88.689864 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane
Unintentional Release Bbls 0.1
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2016-11-15 16:46:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Leak Repair Method Did Not Necessitate Shutdown
On Site Datetime 2016-11-15 16:46:00
Nrc Rpt Datetime 2016-11-16 10:39:00
Nrc Rpt Num 1164264 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Seymour To Beaumont (Atex)
Segment Name P62
Onshore State Abbreviation Il
Onshore Postal Code 62917
Onshore City Name Brushy Township
Onshore County Name Saline
Designated Location Milepost/valve Station
Designated Name 647.7
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 46
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 16
Pipe Wall Thickness 0.267
Pipe Smys 60000
Pipe Specification Api-5l-X-60
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer U.s. Steel
Pipe Coating Type Other
Pipe Coating Details Tape Coating
Weld Subtype Pipe Girth Weld
Installation Year 1974
Manufactured Year 1974
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1
Est Cost Prop Damage 127747
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 127748
Accident Psig 799
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Not Mandated
Length Segment Isolated 65630
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Mechanical Stress Yes
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Emat Ind Yes
Other Tool Tech Ind Yes
Axial Recent Year 2016
Geometry Recent Year 2016
Emat Recent Year 2016
Other Tool Emat
Other Recent Year 2016
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1979
Hydrtst Most Rcnt Pressure 2001
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Handl Ultrasonic Rcnt Year 2016
Exm Wet Mgnt Partcl Rcnt Year 2016
Exm Handl Ultrasonic Rcnt Ind Yes
Exm Wet Mgnt Partcl Rcnt Ind Yes
Preparer Name E**** W*******
Preparer Title Pipeline Compliance Engineer
Preparer Email E********@e****.com
Preparer Telephone 713-381-5757
Prepared Date 2017-04-07 00:00:00
Authorizer Name E**** W*******
Authorizer Telephone 713-381-5757
Authorizer Title Pipeline Compliance Engineer
Authorizer Email E********@e****.com
Narrative On november 15, 2016 a welding crew was finishing the final weld of a type b in-service reinforcement sleeve at mp 647.7 on the p62 pipeline. At approximately 16:46 a flash fire occurred from the area between the external sleeve and the line pipe. The flash was reported as 3" in length and similar to a pilot light in flame size and intensity. The crew shut down work, notified pipeline control, and began monitoring the area. At that time, the source of the lel was suspected to be from the bondo curing under the sleeve and not from an active leak. The site was monitored throughout the night to determine the source of the lel. On november 16, 2016 at 10:01 the source of the lel was confirmed to be from a leak under the b sleeve, and the nrc was notified at 10:39. The pipe was repaired with the installation of an oversleeve and was returned to normal operation november 30, 2016.

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