HL incident on 2016-11-16 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,700
Incident datetime
2016-11-16 13:41
Report number
Location
OK
Narrative
On november 16th, 2016 oneok crews conducting excavations in preparation for pipeline change outs as part of a maintenance project discovered hydrocarbons in the soil. Pipeline was exposed and hydrocarbon vapors were identified coming from the pipeline. A plidco bolt on clamp was installed at the location to stop the leak and the pipeline was returned to normal service. On november 28th the pipeline was shutdown and evacuated. The section of pipe were the leak clamp was installed was removed from the pipeline and new pipe installed. Additional maintenance work was preformed on the pipeline prior to hydrotesting prior to returning the pipeline to service.
Detailed record list
Report Received Date
2016-12-14 00:00:00
Iyear
2016
Report Number
20160413
Supplemental Number
21953
Report Type
Original Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2016-11-16 13:41:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
4.2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-11-16 13:41:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Plidco Clamp Installed To Contain Leak. Pipe Changed At Later Date.
On Site Datetime
2016-11-16 13:41:00
Nrc Rpt Datetime
2016-11-16 14:07:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Oneok Scurry Lateral
Segment Name
Oneok Pipeline Index Number 20387
Onshore State Abbreviation
Tx
Onshore Postal Code
79549
Onshore City Name
Not Within A Municipality
Onshore County Name
Scurry
Designated Location
Milepost/valve Station
Designated Name
Mp 37.22
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
52
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
6.625
Pipe Wall Thickness
0.219
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1957
Manufactured Year
1957
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
6700
Est Cost Emergency
150
Est Cost Environmental
0
Est Cost Other
4029
Est Cost Other Details
Nitrogen To Purge Hvl's From Pipeline To Make Change Out.
Prpty
11079
Accident Psig
520
Mop Psig
1220
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
21523
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place. Field crews were excavating pipeline to perform maintenance work and discovered hydrocarbons in the soil.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Lack Of Fusion In Pipe Seam
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2015
Geometry Recent Year
2015
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
N*** J****
Preparer Title
Requlatory Compliance Supervisor
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2016-12-14 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
N*********@o****.com
Narrative
On november 16th, 2016 oneok crews conducting excavations in preparation for pipeline change outs as part of a maintenance project discovered hydrocarbons in the soil. Pipeline was exposed and hydrocarbon vapors were identified coming from the pipeline. A plidco bolt on clamp was installed at the location to stop the leak and the pipeline was returned to normal service. On november 28th the pipeline was shutdown and evacuated. The section of pipe were the leak clamp was installed was removed from the pipeline and new pipe installed. Additional maintenance work was preformed on the pipeline prior to hydrotesting prior to returning the pipeline to service.
Report Received Date 2016-12-14 00:00:00
Iyear 2016
Report Number 20160413
Supplemental Number 21953
Report Type Original Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2016-11-16 13:41:00
Location Latitude 32.665279 Google Maps OpenStreetMap
Location Longitude -101.057856 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 4.2
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-11-16 13:41:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Plidco Clamp Installed To Contain Leak. Pipe Changed At Later Date.
On Site Datetime 2016-11-16 13:41:00
Nrc Rpt Datetime 2016-11-16 14:07:00
Nrc Rpt Num 1164294 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Oneok Scurry Lateral
Segment Name Oneok Pipeline Index Number 20387
Onshore State Abbreviation Tx
Onshore Postal Code 79549
Onshore City Name Not Within A Municipality
Onshore County Name Scurry
Designated Location Milepost/valve Station
Designated Name Mp 37.22
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 52
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 6.625
Pipe Wall Thickness 0.219
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1957
Manufactured Year 1957
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 6700
Est Cost Emergency 150
Est Cost Environmental 0
Est Cost Other 4029
Est Cost Other Details Nitrogen To Purge Hvl's From Pipeline To Make Change Out.
Prpty 11079
Accident Psig 520
Mop Psig 1220
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 21523
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had taken place. Field crews were excavating pipeline to perform maintenance work and discovered hydrocarbons in the soil.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Lack Of Fusion In Pipe Seam
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2015
Geometry Recent Year 2015
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name N*** J****
Preparer Title Requlatory Compliance Supervisor
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2016-12-14 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email N*********@o****.com
Narrative On november 16th, 2016 oneok crews conducting excavations in preparation for pipeline change outs as part of a maintenance project discovered hydrocarbons in the soil. Pipeline was exposed and hydrocarbon vapors were identified coming from the pipeline. A plidco bolt on clamp was installed at the location to stop the leak and the pipeline was returned to normal service. On november 28th the pipeline was shutdown and evacuated. The section of pipe were the leak clamp was installed was removed from the pipeline and new pipe installed. Additional maintenance work was preformed on the pipeline prior to hydrotesting prior to returning the pipeline to service.

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