Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2016-11-16 — TX
Operator
Sfpp, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$50
Incident datetime
2016-11-16 11:10
Report number
Location
TX
Narrative
On 11/16/16, at approximately 1110, during a 20" cleaning pig launch inside of kinder morgan's sfpp, l.P., colton south terminal a 58.6 gallon diesel release occurred. The launcher is associated with ls 111 (colton to yuma 20"x22"). The release occurred from the scraper launcher door when the launcher was pressured up. The initial investigation revealed the scraper launcher door "o" ring fell out of its position when the door was closed and was damaged. Agency notifications were conducted and the "o" ring was replaced. No surface waters were impacted by the release. Cleanup and excavation activities were implemented immediately.
Detailed record list
Report Received Date
2016-12-07 00:00:00
Iyear
2016
Report Number
20160407
Supplemental Number
21937
Report Type
Original Final
Operator Id
18092
Name
Sfpp, Lp
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-11-16 11:10:00
Location Latitude
34.059928
Location Longitude
-117.366844
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
1.4
Recovered Bbls
1.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-11-16 11:10:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-11-16 11:15:00
Restart Datetime
2016-11-16 14:30:00
On Site Datetime
2016-11-16 11:10:00
Nrc Rpt Datetime
2016-11-16 11:15:00
Nrc Rpt Num
1164289
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Colton South Pump Station
Segment Name
Ls 111 Launcher
Onshore State Abbreviation
Ca
Onshore Postal Code
92316
Onshore City Name
Bloomington
Onshore County Name
San Bernardino
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
1987
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
86
Est Cost Prop Damage
50
Est Cost Emergency
2000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2136
Accident Psig
920
Mop Psig
2160
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a maintenance activity not associated the control room.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Unpredictable Maintenance Failure
Preparer Name
S**** M*******
Preparer Title
Mgr-Ccs
Preparer Email
S*************@k***********.com
Preparer Telephone
909-873-5146
Preparer Fax
303-984-3620
Prepared Date
2016-12-07 00:00:00
Authorizer Name
E***** A* F***
Authorizer Telephone
713-369-9454
Authorizer Title
Director Ccs
Authorizer Email
B********@k***********.com
Narrative
On 11/16/16, at approximately 1110, during a 20" cleaning pig launch inside of kinder morgan's sfpp, l.P., colton south terminal a 58.6 gallon diesel release occurred. The launcher is associated with ls 111 (colton to yuma 20"x22"). The release occurred from the scraper launcher door when the launcher was pressured up. The initial investigation revealed the scraper launcher door "o" ring fell out of its position when the door was closed and was damaged. Agency notifications were conducted and the "o" ring was replaced. No surface waters were impacted by the release. Cleanup and excavation activities were implemented immediately.
| Report Received Date | 2016-12-07 00:00:00 |
|---|---|
| Iyear | 2016 |
| Report Number | 20160407 |
| Supplemental Number | 21937 |
| Report Type | Original Final |
| Operator Id | 18092 PHMSA Enforcement |
| Name | Sfpp, Lp |
| Operator Street Address | 1001 Louisiana St., Suite 1000 |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2016-11-16 11:10:00 |
| Location Latitude | 34.059928 Google Maps OpenStreetMap |
| Location Longitude | -117.366844 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 1.4 |
| Recovered Bbls | 1.4 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2016-11-16 11:10:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2016-11-16 11:15:00 |
| Restart Datetime | 2016-11-16 14:30:00 |
| On Site Datetime | 2016-11-16 11:10:00 |
| Nrc Rpt Datetime | 2016-11-16 11:15:00 |
| Nrc Rpt Num | 1164289 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Colton South Pump Station |
| Segment Name | Ls 111 Launcher |
| Onshore State Abbreviation | Ca |
| Onshore Postal Code | 92316 |
| Onshore City Name | Bloomington |
| Onshore County Name | San Bernardino |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Scraper/pig Trap |
| Installation Year | 1987 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Usa Ecological Ind | Yes |
| Usa Ecological Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 86 |
| Est Cost Prop Damage | 50 |
| Est Cost Emergency | 2000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 2136 |
| Accident Psig | 920 |
| Mop Psig | 2160 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | This was a maintenance activity not associated the control room. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | O-Ring |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Unpredictable Maintenance Failure |
| Preparer Name | S**** M******* |
| Preparer Title | Mgr-Ccs |
| Preparer Email | S*************@k***********.com |
| Preparer Telephone | 909-873-5146 |
| Preparer Fax | 303-984-3620 |
| Prepared Date | 2016-12-07 00:00:00 |
| Authorizer Name | E***** A* F*** |
| Authorizer Telephone | 713-369-9454 |
| Authorizer Title | Director Ccs |
| Authorizer Email | B********@k***********.com |
| Narrative | On 11/16/16, at approximately 1110, during a 20" cleaning pig launch inside of kinder morgan's sfpp, l.P., colton south terminal a 58.6 gallon diesel release occurred. The launcher is associated with ls 111 (colton to yuma 20"x22"). The release occurred from the scraper launcher door when the launcher was pressured up. The initial investigation revealed the scraper launcher door "o" ring fell out of its position when the door was closed and was damaged. Agency notifications were conducted and the "o" ring was replaced. No surface waters were impacted by the release. Cleanup and excavation activities were implemented immediately. |
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