HL incident on 2016-11-08 — TX

Operator
Enterprise Products Operating Llc
Cause
Notification Issue
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$196,988
Incident datetime
2016-11-08 15:48
Report number
Location
TX
Narrative
On november 8, 2016, a third-party contractor was using a bulldozer to perform road work on a private road located on the row of the a3 pipeline. The third-party contractor did not place a one-call notification or contact enterprise personnel before performing the road work. At approximately 15:36 the third-party contractor hit the a3 pipeline at mp 98 which resulted in a release of approximately 1,820 bbls of propane. There was no fire, explosion, injuries, or fatalities as a result of this release. The line was isolated at 15:48 by the control center via remotely operated valves. Enterprise personnel arrived on site at 15:57 and confirmed the release at 16:25. An nrc notification was made at 17:21 (#1163598). 15 people were evacuated from nearby homes as a precaution but were allowed to return to their homes later that evening. The pipeline was repaired and returned to service on november 13, 2016.
Detailed record list
Report Received Date
2016-12-07 00:00:00
Iyear
2016
Report Number
20160406
Supplemental Number
21935
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-11-08 15:36:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
1820
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2016-11-08 15:48:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-11-08 15:48:00
Restart Datetime
2016-11-13 08:40:00
On Site Datetime
2016-11-08 15:57:00
Nrc Rpt Datetime
2016-11-08 17:21:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
15
Pipe Fac Name
Greensburg To Chelsea
Segment Name
A3
Onshore State Abbreviation
Pa
Onshore Postal Code
15961
Onshore City Name
Vintondale
Onshore County Name
Cambria
Designated Location
Milepost/valve Station
Designated Name
98
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
9
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Uncased
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6.625
Pipe Wall Thickness
0.28
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1942
Manufactured Year
1942
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
3
Puncture Circum
2
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
43000
Est Cost Prop Damage
196988
Est Cost Emergency
15302
Est Cost Environmental
0
Est Cost Other
0
Prpty
255290
Accident Psig
902
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
49104
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Road Work
One Call Notified Ind
No
Service Interruption
Yes
Service Interruption Hours
113
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2015
Geometry Recent Year
2015
Other Recent Year
2011
Insp Compl Before Damage Ind
Yes
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2003
Hydrtst Most Rcnt Pressure
1917
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
E**** W*******
Preparer Title
Pipeline Compliance Engineer
Preparer Email
E********@e****.com
Preparer Telephone
713-381-5757
Prepared Date
2016-12-07 00:00:00
Authorizer Name
E**** W*******
Authorizer Telephone
713-381-5757
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
E********@e****.com
Narrative
On november 8, 2016, a third-party contractor was using a bulldozer to perform road work on a private road located on the row of the a3 pipeline. The third-party contractor did not place a one-call notification or contact enterprise personnel before performing the road work. At approximately 15:36 the third-party contractor hit the a3 pipeline at mp 98 which resulted in a release of approximately 1,820 bbls of propane. There was no fire, explosion, injuries, or fatalities as a result of this release. The line was isolated at 15:48 by the control center via remotely operated valves. Enterprise personnel arrived on site at 15:57 and confirmed the release at 16:25. An nrc notification was made at 17:21 (#1163598). 15 people were evacuated from nearby homes as a precaution but were allowed to return to their homes later that evening. The pipeline was repaired and returned to service on november 13, 2016.
Report Received Date 2016-12-07 00:00:00
Iyear 2016
Report Number 20160406
Supplemental Number 21935
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-11-08 15:36:00
Location Latitude 40.4329 Google Maps OpenStreetMap
Location Longitude -78.9279 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 1820
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2016-11-08 15:48:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-11-08 15:48:00
Restart Datetime 2016-11-13 08:40:00
On Site Datetime 2016-11-08 15:57:00
Nrc Rpt Datetime 2016-11-08 17:21:00
Nrc Rpt Num 1163598 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 15
Pipe Fac Name Greensburg To Chelsea
Segment Name A3
Onshore State Abbreviation Pa
Onshore Postal Code 15961
Onshore City Name Vintondale
Onshore County Name Cambria
Designated Location Milepost/valve Station
Designated Name 98
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 9
Crossing Yes
Road Crossing Ind Yes
Road Type Uncased
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6.625
Pipe Wall Thickness 0.28
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1942
Manufactured Year 1942
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 3
Puncture Circum 2
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 43000
Est Cost Prop Damage 196988
Est Cost Emergency 15302
Est Cost Environmental 0
Est Cost Other 0
Prpty 255290
Accident Psig 902
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 49104
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Road Work
One Call Notified Ind No
Service Interruption Yes
Service Interruption Hours 113
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2015
Geometry Recent Year 2015
Other Recent Year 2011
Insp Compl Before Damage Ind Yes
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2003
Hydrtst Most Rcnt Pressure 1917
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name E**** W*******
Preparer Title Pipeline Compliance Engineer
Preparer Email E********@e****.com
Preparer Telephone 713-381-5757
Prepared Date 2016-12-07 00:00:00
Authorizer Name E**** W*******
Authorizer Telephone 713-381-5757
Authorizer Title Pipeline Compliance Engineer
Authorizer Email E********@e****.com
Narrative On november 8, 2016, a third-party contractor was using a bulldozer to perform road work on a private road located on the row of the a3 pipeline. The third-party contractor did not place a one-call notification or contact enterprise personnel before performing the road work. At approximately 15:36 the third-party contractor hit the a3 pipeline at mp 98 which resulted in a release of approximately 1,820 bbls of propane. There was no fire, explosion, injuries, or fatalities as a result of this release. The line was isolated at 15:48 by the control center via remotely operated valves. Enterprise personnel arrived on site at 15:57 and confirmed the release at 16:25. An nrc notification was made at 17:21 (#1163598). 15 people were evacuated from nearby homes as a precaution but were allowed to return to their homes later that evening. The pipeline was repaired and returned to service on november 13, 2016.

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