HL incident on 2016-10-31 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-10-31 11:30
Report number
Location
TX
Narrative
During routine operator rounds, naphtha was found leaking from a manual pressure gauge on the tank 116 suction piping. Operations responded by immediately isolating the gauge and installing a piping plug. Personnel removed and containerized the contaminated soil in the area for disposal. As part of the facility small spill prevention plan, the facility is in the process of identifying and removing similar non-essential pressure gauges.
Detailed record list
Report Received Date
2016-11-30 00:00:00
Iyear
2016
Report Number
20160396
Supplemental Number
21900
Report Type
Original Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2016-10-31 11:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Naphtha
Unintentional Release Bbls
2.82
Recovered Bbls
2.82
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-10-31 11:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
System Was Down, Leaking Gauge Was Removed And Plugged.
On Site Datetime
2016-10-31 11:40:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Beaumont Terminal
Segment Name
Tank 116 Suction Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
77627
Onshore City Name
Nederland
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Naphtha Pipe
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Instrumentation
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
0
Est Cost Emergency
3500
Est Cost Environmental
1500
Est Cost Other
0
Est Cost Other Details
Cost Of Response And Cleanup Activities. Pressure Gauge Was Removed.
Prpty
5050
Accident Psig
50
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Pressure Gauge Internal Failure.
Preparer Name
J*** S*****
Preparer Title
Dot Coordinator
Preparer Email
J************@p**.com
Preparer Telephone
832-765-1858
Preparer Fax
918-977-8930
Prepared Date
2016-11-30 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director Dot Compliance
Authorizer Email
M***********@p**.com
Narrative
During routine operator rounds, naphtha was found leaking from a manual pressure gauge on the tank 116 suction piping. Operations responded by immediately isolating the gauge and installing a piping plug. Personnel removed and containerized the contaminated soil in the area for disposal. As part of the facility small spill prevention plan, the facility is in the process of identifying and removing similar non-essential pressure gauges.
Report Received Date 2016-11-30 00:00:00
Iyear 2016
Report Number 20160396
Supplemental Number 21900
Report Type Original Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2016-10-31 11:30:00
Location Latitude 29.994064 Google Maps OpenStreetMap
Location Longitude -93.986846 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Naphtha
Unintentional Release Bbls 2.82
Recovered Bbls 2.82
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-10-31 11:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain System Was Down, Leaking Gauge Was Removed And Plugged.
On Site Datetime 2016-10-31 11:40:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Beaumont Terminal
Segment Name Tank 116 Suction Piping
Onshore State Abbreviation Tx
Onshore Postal Code 77627
Onshore City Name Nederland
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name Naphtha Pipe
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Instrumentation
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 0
Est Cost Emergency 3500
Est Cost Environmental 1500
Est Cost Other 0
Est Cost Other Details Cost Of Response And Cleanup Activities. Pressure Gauge Was Removed.
Prpty 5050
Accident Psig 50
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Pressure Gauge Internal Failure.
Preparer Name J*** S*****
Preparer Title Dot Coordinator
Preparer Email J************@p**.com
Preparer Telephone 832-765-1858
Preparer Fax 918-977-8930
Prepared Date 2016-11-30 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 832-765-1632
Authorizer Title Director Dot Compliance
Authorizer Email M***********@p**.com
Narrative During routine operator rounds, naphtha was found leaking from a manual pressure gauge on the tank 116 suction piping. Operations responded by immediately isolating the gauge and installing a piping plug. Personnel removed and containerized the contaminated soil in the area for disposal. As part of the facility small spill prevention plan, the facility is in the process of identifying and removing similar non-essential pressure gauges.

All rights reserved. Copyright © by ClearPHMSA