Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2016-10-31 — TX
Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2016-10-31 11:30
Report number
Location
TX
Narrative
During routine operator rounds, naphtha was found leaking from a manual pressure gauge on the tank 116 suction piping. Operations responded by immediately isolating the gauge and installing a piping plug. Personnel removed and containerized the contaminated soil in the area for disposal. As part of the facility small spill prevention plan, the facility is in the process of identifying and removing similar non-essential pressure gauges.
Detailed record list
Report Received Date
2016-11-30 00:00:00
Iyear
2016
Report Number
20160396
Supplemental Number
21900
Report Type
Original Final
Operator Id
31684
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2016-10-31 11:30:00
Location Latitude
29.994064
Location Longitude
-93.986846
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Naphtha
Unintentional Release Bbls
2.82
Recovered Bbls
2.82
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-10-31 11:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
System Was Down, Leaking Gauge Was Removed And Plugged.
On Site Datetime
2016-10-31 11:40:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Beaumont Terminal
Segment Name
Tank 116 Suction Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
77627
Onshore City Name
Nederland
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Naphtha Pipe
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Instrumentation
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
0
Est Cost Emergency
3500
Est Cost Environmental
1500
Est Cost Other
0
Est Cost Other Details
Cost Of Response And Cleanup Activities. Pressure Gauge Was Removed.
Prpty
5050
Accident Psig
50
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Pressure Gauge Internal Failure.
Preparer Name
J*** S*****
Preparer Title
Dot Coordinator
Preparer Email
J************@p**.com
Preparer Telephone
832-765-1858
Preparer Fax
918-977-8930
Prepared Date
2016-11-30 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director Dot Compliance
Authorizer Email
M***********@p**.com
Narrative
During routine operator rounds, naphtha was found leaking from a manual pressure gauge on the tank 116 suction piping. Operations responded by immediately isolating the gauge and installing a piping plug. Personnel removed and containerized the contaminated soil in the area for disposal. As part of the facility small spill prevention plan, the facility is in the process of identifying and removing similar non-essential pressure gauges.
| Report Received Date | 2016-11-30 00:00:00 |
|---|---|
| Iyear | 2016 |
| Report Number | 20160396 |
| Supplemental Number | 21900 |
| Report Type | Original Final |
| Operator Id | 31684 PHMSA Enforcement |
| Name | Phillips 66 Pipeline Llc |
| Operator Street Address | 2331 Citywest Blvd |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77042 |
| Local Datetime | 2016-10-31 11:30:00 |
| Location Latitude | 29.994064 Google Maps OpenStreetMap |
| Location Longitude | -93.986846 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Other |
| Commodity Details | Naphtha |
| Unintentional Release Bbls | 2.82 |
| Recovered Bbls | 2.82 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2016-10-31 11:30:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | System Was Down, Leaking Gauge Was Removed And Plugged. |
| On Site Datetime | 2016-10-31 11:40:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Beaumont Terminal |
| Segment Name | Tank 116 Suction Piping |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77627 |
| Onshore City Name | Nederland |
| Onshore County Name | Jefferson |
| Designated Location | Milepost/valve Station |
| Designated Name | Naphtha Pipe |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Instrumentation |
| Installation Year | Unknown |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 50 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 3500 |
| Est Cost Environmental | 1500 |
| Est Cost Other | 0 |
| Est Cost Other Details | Cost Of Response And Cleanup Activities. Pressure Gauge Was Removed. |
| Prpty | 5050 |
| Accident Psig | 50 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | O-Ring |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Pressure Gauge Internal Failure. |
| Preparer Name | J*** S***** |
| Preparer Title | Dot Coordinator |
| Preparer Email | J************@p**.com |
| Preparer Telephone | 832-765-1858 |
| Preparer Fax | 918-977-8930 |
| Prepared Date | 2016-11-30 00:00:00 |
| Authorizer Name | T*** F**** |
| Authorizer Telephone | 832-765-1632 |
| Authorizer Title | Director Dot Compliance |
| Authorizer Email | M***********@p**.com |
| Narrative | During routine operator rounds, naphtha was found leaking from a manual pressure gauge on the tank 116 suction piping. Operations responded by immediately isolating the gauge and installing a piping plug. Personnel removed and containerized the contaminated soil in the area for disposal. As part of the facility small spill prevention plan, the facility is in the process of identifying and removing similar non-essential pressure gauges. |
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