HL incident on 2016-10-20 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$16,404
Incident datetime
2016-10-20 09:48
Report number
Location
TX
Narrative
On october 20, 2016 at 9:48 am, while completing routine rounds at the deer river, minnesota pump station, the mechanical technician discovered approximately 6.5 gallons of crude oil on the line 2 pump room floor. The edmonton control center was contacted. The pipelines in the area had already been shut down due to an odor call in the cass lake area, unrelated to the incident at the deer river pump station where the oil was discovered. Initial investigation revealed that the line 2 unit 2 outboard pump seal had failed. The unit was locked out until the seal was replaced on october 25, 2016. There was no contaminated soil associated with this leak.
Detailed record list
Report Received Date
2016-11-18 00:00:00
Iyear
2016
Report Number
20160385
Supplemental Number
21870
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2016-10-20 09:48:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.15
Recovered Bbls
0.15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-10-20 09:48:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipelines Already Shut Down For An Odor Call Earlier That Same Morning
On Site Datetime
2016-10-20 09:48:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Deer River Station
Segment Name
Line 2 Unit 2
Onshore State Abbreviation
Mn
Onshore Postal Code
56636
Onshore City Name
Deer River
Onshore County Name
Itasca
Designated Location
Milepost/valve Station
Designated Name
996
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2002
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
6
Est Cost Prop Damage
16404
Est Cost Emergency
162
Est Cost Environmental
0
Est Cost Other
0
Prpty
16572
Accident Psig
601
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear And Tear
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-394-1564
Prepared Date
2016-11-18 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On october 20, 2016 at 9:48 am, while completing routine rounds at the deer river, minnesota pump station, the mechanical technician discovered approximately 6.5 gallons of crude oil on the line 2 pump room floor. The edmonton control center was contacted. The pipelines in the area had already been shut down due to an odor call in the cass lake area, unrelated to the incident at the deer river pump station where the oil was discovered. Initial investigation revealed that the line 2 unit 2 outboard pump seal had failed. The unit was locked out until the seal was replaced on october 25, 2016. There was no contaminated soil associated with this leak.
Report Received Date 2016-11-18 00:00:00
Iyear 2016
Report Number 20160385
Supplemental Number 21870
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2016-10-20 09:48:00
Location Latitude 47.324386 Google Maps OpenStreetMap
Location Longitude -93.762975 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.15
Recovered Bbls 0.15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-10-20 09:48:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipelines Already Shut Down For An Odor Call Earlier That Same Morning
On Site Datetime 2016-10-20 09:48:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Deer River Station
Segment Name Line 2 Unit 2
Onshore State Abbreviation Mn
Onshore Postal Code 56636
Onshore City Name Deer River
Onshore County Name Itasca
Designated Location Milepost/valve Station
Designated Name 996
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2002
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 6
Est Cost Prop Damage 16404
Est Cost Emergency 162
Est Cost Environmental 0
Est Cost Other 0
Prpty 16572
Accident Psig 601
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear And Tear
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-394-1564
Prepared Date 2016-11-18 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On october 20, 2016 at 9:48 am, while completing routine rounds at the deer river, minnesota pump station, the mechanical technician discovered approximately 6.5 gallons of crude oil on the line 2 pump room floor. The edmonton control center was contacted. The pipelines in the area had already been shut down due to an odor call in the cass lake area, unrelated to the incident at the deer river pump station where the oil was discovered. Initial investigation revealed that the line 2 unit 2 outboard pump seal had failed. The unit was locked out until the seal was replaced on october 25, 2016. There was no contaminated soil associated with this leak.

All rights reserved. Copyright © by ClearPHMSA