HL incident on 2014-08-26 — TX

Operator
Wyoming Pipeline Company
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300
Incident datetime
2014-08-26 14:00
Report number
Location
TX
Narrative
The leak was discovered by contract workers; who, notified mccc. The spill was located on wpc row; the crew did not see any spill in the morning hours as they went by; however, they discovered it on their return in the afternoon and phoned it in. No pipeline valves were shut due to the leak, a clamp was installed to stop the pinhole from leaking. Again, section e question 5 won't allow not entering that valves were shut. The fact that it indicates that manual valves were shut and they were 1 foot apart was only entered to satisfy the mandatory entries required by the form.
Detailed record list
Report Received Date
2016-11-18 00:00:00
Iyear
2014
Report Number
20160384
Supplemental Number
31802
Report Type
Supplemental Final
Operator Id
Name
Wyoming Pipeline Company
Operator Street Address
825 Town & Country Lane
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2014-08-26 14:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2014-08-26 14:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Leak Was Mitigated With A Clamp While The Line Was In Operation
On Site Datetime
2014-08-26 14:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Wyoming Pipeline Company
Segment Name
Buck Creek 8" Main Line
Onshore State Abbreviation
Wy
Onshore Postal Code
82701
Onshore City Name
Not Within A Municipality
Onshore County Name
Weston
Designated Location
Milepost/valve Station
Designated Name
D & W Livstk
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.277
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
300
Est Cost Emergency
7185
Est Cost Environmental
1730
Est Cost Other
0
Prpty
9265
Accident Psig
10
Mop Psig
308
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
Unknown
Internal Inspection Ind
No
Other Restrictions Ind
Yes
Operation Complications Ind
No
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Microbiological Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2014
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
W****** B M********
Preparer Title
Compliance Consultant
Preparer Email
W*****@c**.net
Preparer Telephone
405-820-1304
Prepared Date
2019-03-18 00:00:00
Authorizer Name
M***** E*****
Authorizer Telephone
307-746-9803
Authorizer Title
Logistics Manager
Authorizer Email
M******@p*********.com
Narrative
The leak was discovered by contract workers; who, notified mccc. The spill was located on wpc row; the crew did not see any spill in the morning hours as they went by; however, they discovered it on their return in the afternoon and phoned it in. No pipeline valves were shut due to the leak, a clamp was installed to stop the pinhole from leaking. Again, section e question 5 won't allow not entering that valves were shut. The fact that it indicates that manual valves were shut and they were 1 foot apart was only entered to satisfy the mandatory entries required by the form.
Report Received Date 2016-11-18 00:00:00
Iyear 2014
Report Number 20160384
Supplemental Number 31802
Report Type Supplemental Final
Operator Id 32537 PHMSA Enforcement
Name Wyoming Pipeline Company
Operator Street Address 825 Town & Country Lane
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77024
Local Datetime 2014-08-26 14:00:00
Location Latitude 43.635044 Google Maps OpenStreetMap
Location Longitude -104.318047 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2014-08-26 14:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Leak Was Mitigated With A Clamp While The Line Was In Operation
On Site Datetime 2014-08-26 14:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Wyoming Pipeline Company
Segment Name Buck Creek 8" Main Line
Onshore State Abbreviation Wy
Onshore Postal Code 82701
Onshore City Name Not Within A Municipality
Onshore County Name Weston
Designated Location Milepost/valve Station
Designated Name D & W Livstk
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.277
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 300
Est Cost Emergency 7185
Est Cost Environmental 1730
Est Cost Other 0
Prpty 9265
Accident Psig 10
Mop Psig 308
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated Unknown
Internal Inspection Ind No
Other Restrictions Ind Yes
Operation Complications Ind No
Pipeline Function =< 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Microbiological Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2014
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name W****** B M********
Preparer Title Compliance Consultant
Preparer Email W*****@c**.net
Preparer Telephone 405-820-1304
Prepared Date 2019-03-18 00:00:00
Authorizer Name M***** E*****
Authorizer Telephone 307-746-9803
Authorizer Title Logistics Manager
Authorizer Email M******@p*********.com
Narrative The leak was discovered by contract workers; who, notified mccc. The spill was located on wpc row; the crew did not see any spill in the morning hours as they went by; however, they discovered it on their return in the afternoon and phoned it in. No pipeline valves were shut due to the leak, a clamp was installed to stop the pinhole from leaking. Again, section e question 5 won't allow not entering that valves were shut. The fact that it indicates that manual valves were shut and they were 1 foot apart was only entered to satisfy the mandatory entries required by the form.

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