HL incident on 2016-10-17 — OK

Operator
Magellan Ammonia Pipeline, L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
1 fatality 1 injury
Property damage (nominal)
$184,500
Incident datetime
2016-10-17 21:14
Report number
Location
OK
Narrative
At 21:03:40 on 10/17/2016, a release occurred on the magellan ammonia pipeline, l.P. Valley to missouri river pipeline segment. At 21:14 magellan initiated a complete pipeline shutdown and isolation based on scada and the cpm (plm) system indications. While completing the pipeline shutdown and isolation, magellan received a telephonic notification from a third party regarding a vapor cloud and strong odor. Magellan declared a code red at 21:26:23, initiating a full emergency response. Field operations were notified and employees were dispatched to close manual valves. The psap (public access safety point) and nrc were notified and provided with an estimated release volume of ammonia. The initial nrc report number was 1161809. Additional nrc reports (1161815 and 116831) were made revising the estimated amounts released as additional information became available. Results of the national transportation safety board investigation indicate the probable cause of the pipeline rupture was corrosion fatigue cracks that grew and coalesced under disbonded polyethylene tape coating. Contributing to the location of the cracking was external loading that caused bending stress in the pipe in addition to the cyclic stresses in the pipe from the internal pressure of the ammonia transported. Decommissioning of the anhydrous ammonia pipeline system was successfully completed on april 10, 2020. Supplemental/final (5/19/2020): part c6, d8d, d8g, g5-1,3,4, h
Detailed record list
Report Received Date
2016-11-16 00:00:00
Iyear
2016
Report Number
20160377
Supplemental Number
33776
Report Type
Supplemental Final
Operator Id
Name
Magellan Ammonia Pipeline, L.p.
Operator Street Address
One Williams Center, Md 28
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2016-10-17 21:03:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
2587
Intentional Release Bbls
0
Recovered Bbls
1064
Fatality Ind
Yes
Num Emp Fatalities
0
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
1
Fatal
1
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
1
Injure
1
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2016-10-17 21:14:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-10-17 21:14:00
Restart Datetime
2016-11-15 15:30:00
On Site Datetime
2016-10-17 22:50:00
Nrc Rpt Datetime
2016-10-17 21:42:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
49
Pipe Fac Name
Valley To Whiting Anhydrous Ammonia Line
Segment Name
Line Number 502
Onshore State Abbreviation
Ne
Onshore Postal Code
68061
Onshore City Name
Not Within A Municipality
Onshore County Name
Burt
Designated Location
Milepost/valve Station
Designated Name
263.3178
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.156
Pipe Smys
46000
Pipe Specification
Api 5l-X46
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Lone Star Steel
Pipe Coating Type
Cold Applied Tape
Installation Year
1968
Manufactured Year
1968
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Other
Rupture Details
Spiral
Rupture Width
0.2
Rupture Length
11.9
Wildlife Impact Ind
Yes
Terrestrial Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
61397
Est Cost Gas Released
139077
Est Cost Prop Damage
184500
Est Cost Emergency
2359186
Est Cost Environmental
0
Est Cost Other
68338
Est Cost Other Details
Temporary Lodging, Food, Donations & Miscellaneous Expenses
Prpty
2812498
Accident Psig
800
Mop Psig
1198
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
119935
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Incompat Commod Ind
Yes
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Metallurgical Ind
Yes
Failure Type
Environmental Cracking-Related
Stress Subtype
Stress Corrosion Cracking
Additional Crack Ind
Yes
Collected Data Ind
Yes
Other Recent Year
2015
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2010
Hydrtst Most Rcnt Pressure
1516
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2020-05-19 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 21:03:40 on 10/17/2016, a release occurred on the magellan ammonia pipeline, l.P. Valley to missouri river pipeline segment. At 21:14 magellan initiated a complete pipeline shutdown and isolation based on scada and the cpm (plm) system indications. While completing the pipeline shutdown and isolation, magellan received a telephonic notification from a third party regarding a vapor cloud and strong odor. Magellan declared a code red at 21:26:23, initiating a full emergency response. Field operations were notified and employees were dispatched to close manual valves. The psap (public access safety point) and nrc were notified and provided with an estimated release volume of ammonia. The initial nrc report number was 1161809. Additional nrc reports (1161815 and 116831) were made revising the estimated amounts released as additional information became available. Results of the national transportation safety board investigation indicate the probable cause of the pipeline rupture was corrosion fatigue cracks that grew and coalesced under disbonded polyethylene tape coating. Contributing to the location of the cracking was external loading that caused bending stress in the pipe in addition to the cyclic stresses in the pipe from the internal pressure of the ammonia transported. Decommissioning of the anhydrous ammonia pipeline system was successfully completed on april 10, 2020. Supplemental/final (5/19/2020): part c6, d8d, d8g, g5-1,3,4, h
Report Received Date 2016-11-16 00:00:00
Iyear 2016
Report Number 20160377
Supplemental Number 33776
Report Type Supplemental Final
Operator Id 12105 PHMSA Enforcement
Name Magellan Ammonia Pipeline, L.p.
Operator Street Address One Williams Center, Md 28
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2016-10-17 21:03:00
Location Latitude 41.90199 Google Maps OpenStreetMap
Location Longitude -96.24944 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 2587
Intentional Release Bbls 0
Recovered Bbls 1064
Fatality Ind Yes
Num Emp Fatalities 0
Num Contr Fatalities 0
Num Er Fatalities 0
Num Worker Fatalities 0
Num Gp Fatalities 1
Fatal 1
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 1
Injure 1
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2016-10-17 21:14:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-10-17 21:14:00
Restart Datetime 2016-11-15 15:30:00
On Site Datetime 2016-10-17 22:50:00
Nrc Rpt Datetime 2016-10-17 21:42:00
Nrc Rpt Num 1161809 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 49
Pipe Fac Name Valley To Whiting Anhydrous Ammonia Line
Segment Name Line Number 502
Onshore State Abbreviation Ne
Onshore Postal Code 68061
Onshore City Name Not Within A Municipality
Onshore County Name Burt
Designated Location Milepost/valve Station
Designated Name 263.3178
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.156
Pipe Smys 46000
Pipe Specification Api 5l-X46
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Lone Star Steel
Pipe Coating Type Cold Applied Tape
Installation Year 1968
Manufactured Year 1968
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Other
Rupture Details Spiral
Rupture Width 0.2
Rupture Length 11.9
Wildlife Impact Ind Yes
Terrestrial Impact Ind Yes
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 61397
Est Cost Gas Released 139077
Est Cost Prop Damage 184500
Est Cost Emergency 2359186
Est Cost Environmental 0
Est Cost Other 68338
Est Cost Other Details Temporary Lodging, Food, Donations & Miscellaneous Expenses
Prpty 2812498
Accident Psig 800
Mop Psig 1198
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 119935
Internal Inspection Ind Yes
Operation Complications Ind Yes
Incompat Commod Ind Yes
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Metallurgical Ind Yes
Failure Type Environmental Cracking-Related
Stress Subtype Stress Corrosion Cracking
Additional Crack Ind Yes
Collected Data Ind Yes
Other Recent Year 2015
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2010
Hydrtst Most Rcnt Pressure 1516
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2020-05-19 00:00:00
Authorizer Name G**** R****
Authorizer Telephone 918-574-7165
Authorizer Title Supervisor Integrity Management
Authorizer Email G**********@m*********.com
Narrative At 21:03:40 on 10/17/2016, a release occurred on the magellan ammonia pipeline, l.P. Valley to missouri river pipeline segment. At 21:14 magellan initiated a complete pipeline shutdown and isolation based on scada and the cpm (plm) system indications. While completing the pipeline shutdown and isolation, magellan received a telephonic notification from a third party regarding a vapor cloud and strong odor. Magellan declared a code red at 21:26:23, initiating a full emergency response. Field operations were notified and employees were dispatched to close manual valves. The psap (public access safety point) and nrc were notified and provided with an estimated release volume of ammonia. The initial nrc report number was 1161809. Additional nrc reports (1161815 and 116831) were made revising the estimated amounts released as additional information became available. Results of the national transportation safety board investigation indicate the probable cause of the pipeline rupture was corrosion fatigue cracks that grew and coalesced under disbonded polyethylene tape coating. Contributing to the location of the cracking was external loading that caused bending stress in the pipe in addition to the cyclic stresses in the pipe from the internal pressure of the ammonia transported. Decommissioning of the anhydrous ammonia pipeline system was successfully completed on april 10, 2020. Supplemental/final (5/19/2020): part c6, d8d, d8g, g5-1,3,4, h

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