HL incident on 2016-10-17 — TX

Operator
Dcp Midstream
Cause
Other Accident Cause
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-10-17 09:00
Report number
Location
TX
Narrative
Sonora pump station, pump cases were swapped out to increase the flows through the site. A spare pump case was sent to spx to be upgraded to a high flow bundle, and then transported to the sonora pump station. The roof was removed to facilitate the removal of pump p101. P101 was shut down, locked out and vented down for the pump case swap. This event was inadvertently reported. Dcp is required to notify the nrc about releases greater than 5 bbls resulting from a pipeline maintenance activity. However, the 26.42 bbls that were reported were not released to the atmosphere, but rather was flared off onsite, therefore no notification to the nrc was required.
Detailed record list
Report Received Date
2016-11-07 00:00:00
Iyear
2016
Report Number
20160364
Supplemental Number
21933
Report Type
Supplemental Final
Operator Id
Name
Dcp Midstream
Operator Street Address
2331 Citywest Blvd. Hq-08-S812-02
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2016-10-17 12:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0
Intentional Release Bbls
26.42
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Controlled Released That Was Flared During Maintenance Activities
Incident Identified Datetime
2016-10-17 09:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Maintenance Activity That Did Not Cause A Shut Down Of Operations
On Site Datetime
2016-10-17 09:00:00
Nrc Rpt Datetime
2016-10-17 00:00:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Sandhills West
Segment Name
Sahi-1
Onshore State Abbreviation
Tx
Onshore Postal Code
76950
Onshore City Name
Sonora
Onshore County Name
Sutton
Designated Location
Milepost/valve Station
Designated Name
Sonora Statio
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Controlled Release That Was Flared During Maintenance Activites
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
0
Accident Psig
400
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controlled released that was flared during maintenance activities
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
This Was A Controlled Release As A Result Of Maintenance Activities To Increase The Flows Through The Site . During This Time The Amount Of Ngl Released Was Flared.
Preparer Name
K*** F*****
Preparer Title
Ngl Pipeline Compliance And Integrity Specialist
Preparer Email
K*******@d***********.com
Preparer Telephone
7137353719
Prepared Date
2016-12-07 00:00:00
Authorizer Name
B****** P*****
Authorizer Telephone
7132687400
Authorizer Title
Director Ngl Pipeline Integrity And Compliance
Authorizer Email
B*******@d***********.com
Narrative
Sonora pump station, pump cases were swapped out to increase the flows through the site. A spare pump case was sent to spx to be upgraded to a high flow bundle, and then transported to the sonora pump station. The roof was removed to facilitate the removal of pump p101. P101 was shut down, locked out and vented down for the pump case swap. This event was inadvertently reported. Dcp is required to notify the nrc about releases greater than 5 bbls resulting from a pipeline maintenance activity. However, the 26.42 bbls that were reported were not released to the atmosphere, but rather was flared off onsite, therefore no notification to the nrc was required.
Report Received Date 2016-11-07 00:00:00
Iyear 2016
Report Number 20160364
Supplemental Number 21933
Report Type Supplemental Final
Operator Id 31130 PHMSA Enforcement
Name Dcp Midstream
Operator Street Address 2331 Citywest Blvd. Hq-08-S812-02
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2016-10-17 12:30:00
Location Latitude 30.50214 Google Maps OpenStreetMap
Location Longitude -100.58349 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0
Intentional Release Bbls 26.42
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Controlled Released That Was Flared During Maintenance Activities
Incident Identified Datetime 2016-10-17 09:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Maintenance Activity That Did Not Cause A Shut Down Of Operations
On Site Datetime 2016-10-17 09:00:00
Nrc Rpt Datetime 2016-10-17 00:00:00
Nrc Rpt Num 1161761 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Sandhills West
Segment Name Sahi-1
Onshore State Abbreviation Tx
Onshore Postal Code 76950
Onshore City Name Sonora
Onshore County Name Sutton
Designated Location Milepost/valve Station
Designated Name Sonora Statio
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Controlled Release That Was Flared During Maintenance Activites
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 0
Accident Psig 400
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controlled released that was flared during maintenance activities
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details This Was A Controlled Release As A Result Of Maintenance Activities To Increase The Flows Through The Site . During This Time The Amount Of Ngl Released Was Flared.
Preparer Name K*** F*****
Preparer Title Ngl Pipeline Compliance And Integrity Specialist
Preparer Email K*******@d***********.com
Preparer Telephone 7137353719
Prepared Date 2016-12-07 00:00:00
Authorizer Name B****** P*****
Authorizer Telephone 7132687400
Authorizer Title Director Ngl Pipeline Integrity And Compliance
Authorizer Email B*******@d***********.com
Narrative Sonora pump station, pump cases were swapped out to increase the flows through the site. A spare pump case was sent to spx to be upgraded to a high flow bundle, and then transported to the sonora pump station. The roof was removed to facilitate the removal of pump p101. P101 was shut down, locked out and vented down for the pump case swap. This event was inadvertently reported. Dcp is required to notify the nrc about releases greater than 5 bbls resulting from a pipeline maintenance activity. However, the 26.42 bbls that were reported were not released to the atmosphere, but rather was flared off onsite, therefore no notification to the nrc was required.

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