HL incident on 2016-10-02 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2016-10-02 19:03
Report number
Location
PA
Narrative
On 10/02/2016 at 19:03 the bth facility was recirculating a 250 series tank in order to blend the tank as per design. This recirculation process is completed utilizing in-plant facility piping, pumps, and recirculation equipment. When the recirculation process was complete and the process was shutdown, local operating personnel noticed crude oil leaking from the pump used for the transfer. All crude oil was contained within the concrete pump containment and immediate area. An estimated .5 barrels of product was released and all free product was recovered. No further remediation is necessary. 07/19/2017 the root cause of this release has been attributed to the incorrect installation of the seal by the manufacturer.
Detailed record list
Report Received Date
2016-10-31 00:00:00
Iyear
2016
Report Number
20160358
Supplemental Number
22491
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2016-10-02 19:03:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-10-02 19:03:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Incident Was Discovered After Shutdown
On Site Datetime
2016-10-02 19:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Buckeye Texas Hub
Onshore State Abbreviation
Tx
Onshore Postal Code
78409
Onshore City Name
Corpus Christi
Onshore County Name
Nueces
Designated Location
Milepost/valve Station
Designated Name
Ln Plant
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
2016
Material Involved
Material Other Than Carbon Steel
Material Details
Pump Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
25
Est Cost Prop Damage
2500
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
3525
Accident Psig
40
Mop Psig
225
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Additional Defect Ind
Yes
Additional Installation Ind
Yes
Preparer Name
V****** G**************
Preparer Title
District Compliance Specialist
Preparer Email
V**************@b******.com
Preparer Telephone
361-792-3083
Prepared Date
2017-07-21 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On 10/02/2016 at 19:03 the bth facility was recirculating a 250 series tank in order to blend the tank as per design. This recirculation process is completed utilizing in-plant facility piping, pumps, and recirculation equipment. When the recirculation process was complete and the process was shutdown, local operating personnel noticed crude oil leaking from the pump used for the transfer. All crude oil was contained within the concrete pump containment and immediate area. An estimated .5 barrels of product was released and all free product was recovered. No further remediation is necessary. 07/19/2017 the root cause of this release has been attributed to the incorrect installation of the seal by the manufacturer.
Report Received Date 2016-10-31 00:00:00
Iyear 2016
Report Number 20160358
Supplemental Number 22491
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2016-10-02 19:03:00
Location Latitude 27.832444 Google Maps OpenStreetMap
Location Longitude -97.501889 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-10-02 19:03:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Incident Was Discovered After Shutdown
On Site Datetime 2016-10-02 19:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Buckeye Texas Hub
Onshore State Abbreviation Tx
Onshore Postal Code 78409
Onshore City Name Corpus Christi
Onshore County Name Nueces
Designated Location Milepost/valve Station
Designated Name Ln Plant
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 2016
Material Involved Material Other Than Carbon Steel
Material Details Pump Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 25
Est Cost Prop Damage 2500
Est Cost Emergency 1000
Est Cost Environmental 0
Est Cost Other 0
Prpty 3525
Accident Psig 40
Mop Psig 225
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Additional Defect Ind Yes
Additional Installation Ind Yes
Preparer Name V****** G**************
Preparer Title District Compliance Specialist
Preparer Email V**************@b******.com
Preparer Telephone 361-792-3083
Prepared Date 2017-07-21 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On 10/02/2016 at 19:03 the bth facility was recirculating a 250 series tank in order to blend the tank as per design. This recirculation process is completed utilizing in-plant facility piping, pumps, and recirculation equipment. When the recirculation process was complete and the process was shutdown, local operating personnel noticed crude oil leaking from the pump used for the transfer. All crude oil was contained within the concrete pump containment and immediate area. An estimated .5 barrels of product was released and all free product was recovered. No further remediation is necessary. 07/19/2017 the root cause of this release has been attributed to the incorrect installation of the seal by the manufacturer.

All rights reserved. Copyright © by ClearPHMSA