Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2016-10-16 — TX
Operator
Wyoming Pipeline Company
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$300
Incident datetime
2016-10-16 15:10
Report number
Location
TX
Narrative
Operator found leak while on rounds; the maintenance supervisor was called in; equipment, backhoe and vacuum truck were used in the clean-up process. The line has been replaced; the contaminated soil has been removed and replaced with new soil, reseeding completed.
Detailed record list
Report Received Date
2016-10-26 00:00:00
Iyear
2016
Report Number
20160351
Supplemental Number
22878
Report Type
Supplemental Final
Operator Id
32537
Name
Wyoming Pipeline Company
Operator Street Address
825 Town & Country Lane
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2016-10-16 15:10:00
Location Latitude
43.78813056
Location Longitude
-104.414856
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2016-10-16 15:10:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Leak Had A Clamp Installed With The Line In Operation
On Site Datetime
2016-10-16 15:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wyoming Pipeline Company
Segment Name
Station Piping
Onshore State Abbreviation
Wy
Onshore Postal Code
82701
Onshore City Name
Not Within A Municipality
Onshore County Name
Weston County
Designated Location
Milepost/valve Station
Designated Name
Mush Crk Sta
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.375
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
80
Est Cost Prop Damage
300
Est Cost Emergency
7185
Est Cost Environmental
1730
Est Cost Other
0
Prpty
9295
Accident Psig
20
Mop Psig
100
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pinhole leak was created by external corrosion that was found while repairs were being made.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Microbiological Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
Unknown
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Other Cp Survey Ind
Yes
Cp Annual Survey Year
2015
Close Interval Survey Year
2014
Other Cp Survey Year
2014
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D**** P****
Preparer Title
Aministrative Asst.
Preparer Email
D*****@w****.com
Preparer Telephone
307-746-9479
Preparer Fax
307-746-3606
Prepared Date
2017-12-06 00:00:00
Authorizer Name
N***** H******
Authorizer Telephone
307-746-9479
Authorizer Title
Environmental Engineer
Authorizer Email
N*******@w****.com
Narrative
Operator found leak while on rounds; the maintenance supervisor was called in; equipment, backhoe and vacuum truck were used in the clean-up process. The line has been replaced; the contaminated soil has been removed and replaced with new soil, reseeding completed.
| Report Received Date | 2016-10-26 00:00:00 |
|---|---|
| Iyear | 2016 |
| Report Number | 20160351 |
| Supplemental Number | 22878 |
| Report Type | Supplemental Final |
| Operator Id | 32537 PHMSA Enforcement |
| Name | Wyoming Pipeline Company |
| Operator Street Address | 825 Town & Country Lane |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77024 |
| Local Datetime | 2016-10-16 15:10:00 |
| Location Latitude | 43.78813056 Google Maps OpenStreetMap |
| Location Longitude | -104.414856 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 2 |
| Recovered Bbls | 2 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Ground Patrol By Operator Or Its Contractor |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2016-10-16 15:10:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | The Pipeline Leak Had A Clamp Installed With The Line In Operation |
| On Site Datetime | 2016-10-16 15:15:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Wyoming Pipeline Company |
| Segment Name | Station Piping |
| Onshore State Abbreviation | Wy |
| Onshore Postal Code | 82701 |
| Onshore City Name | Not Within A Municipality |
| Onshore County Name | Weston County |
| Designated Location | Milepost/valve Station |
| Designated Name | Mush Crk Sta |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 36 |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 12 |
| Pipe Wall Thickness | 0.375 |
| Pipe Smys | 24000 |
| Pipe Specification | Unknown |
| Pipe Seam Type | Erw - Low Frequency |
| Pipe Manufacturer | Unknown |
| Pipe Coating Type | Coal Tar |
| Installation Year | Unknown |
| Manufactured Year | Unknown |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 80 |
| Est Cost Prop Damage | 300 |
| Est Cost Emergency | 7185 |
| Est Cost Environmental | 1730 |
| Est Cost Other | 0 |
| Prpty | 9295 |
| Accident Psig | 20 |
| Mop Psig | 100 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The pinhole leak was created by external corrosion that was found while repairs were being made. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | External Corrosion |
| Internal External | External Corrosion |
| Visual Exam Results | General Corrosion |
| Microbiological Corrosion Ind | Yes |
| Field Exam Basis Ind | Yes |
| Underground Location | Yes |
| Under Cathodic Protection Ind | Yes |
| Cathodic Pro Start Year | Unknown |
| Shielding Evident | Unknown |
| Cathodic Survey Type | Yes |
| Cp Annual Survey Ind | Yes |
| Close Interval Survey Ind | Yes |
| Other Cp Survey Ind | Yes |
| Cp Annual Survey Year | 2015 |
| Close Interval Survey Year | 2014 |
| Other Cp Survey Year | 2014 |
| Prior Damage | No |
| Collected Data Ind | No |
| Has Hydrtst Conduc Before Ind | No |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | D**** P**** |
| Preparer Title | Aministrative Asst. |
| Preparer Email | D*****@w****.com |
| Preparer Telephone | 307-746-9479 |
| Preparer Fax | 307-746-3606 |
| Prepared Date | 2017-12-06 00:00:00 |
| Authorizer Name | N***** H****** |
| Authorizer Telephone | 307-746-9479 |
| Authorizer Title | Environmental Engineer |
| Authorizer Email | N*******@w****.com |
| Narrative | Operator found leak while on rounds; the maintenance supervisor was called in; equipment, backhoe and vacuum truck were used in the clean-up process. The line has been replaced; the contaminated soil has been removed and replaced with new soil, reseeding completed. |
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