HL incident on 2015-07-09 — TX

Operator
Wyoming Pipeline Company
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2015-07-09 09:30
Report number
Location
TX
Narrative
This spill was located approximately 24 miles south of newcastle, wyoming on the property of tim & sonya tysdal ranch; the area known as "bobcat creek." the creek is a dry wash and was dry at the time of the incident. Air patrol called in the leak to mush creek control center. Mccc notified the maintenance supervisor and the vac truck and backhoe were dispatched to the site. The oil was sucked up and returned to tankage; contaminated soil was picked up; hauled to remediation site. New soil was deposited in the excavated area.
Detailed record list
Report Received Date
2016-10-26 00:00:00
Iyear
2015
Report Number
20160346
Supplemental Number
22890
Report Type
Supplemental Final
Operator Id
Name
Wyoming Pipeline Company
Operator Street Address
825 Town & Country Lane
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2015-07-09 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
30
Recovered Bbls
30
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-07-09 09:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Buck Creek Line Not In Operation.
On Site Datetime
2015-07-09 11:00:00
Nrc Rpt Datetime
2015-07-10 08:22:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wyoming Pipeline Company
Segment Name
Buck Creek/morrissey Main Line
Onshore State Abbreviation
Wy
Onshore Postal Code
82701
Onshore City Name
Not Within A Municipality
Onshore County Name
Niobrara County
Designated Location
Milepost/valve Station
Designated Name
Buck Crk Line
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.365
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1949
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1200
Est Cost Prop Damage
5000
Est Cost Emergency
7185
Est Cost Environmental
3460
Est Cost Other
0
Prpty
16845
Accident Psig
0
Mop Psig
326
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This line has been inactive and the leak was discovered by air patrol.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Microbiological Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
No
Externally Coated
Yes
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
W****** M********
Preparer Title
Compliance Consultant
Preparer Email
W*****@c**.net
Preparer Telephone
4058201304
Prepared Date
2017-12-06 00:00:00
Authorizer Name
N***** H******
Authorizer Telephone
307-746-2379
Authorizer Title
Environmental Engineer
Authorizer Email
N*******@w****.com
Narrative
This spill was located approximately 24 miles south of newcastle, wyoming on the property of tim & sonya tysdal ranch; the area known as "bobcat creek." the creek is a dry wash and was dry at the time of the incident. Air patrol called in the leak to mush creek control center. Mccc notified the maintenance supervisor and the vac truck and backhoe were dispatched to the site. The oil was sucked up and returned to tankage; contaminated soil was picked up; hauled to remediation site. New soil was deposited in the excavated area.
Report Received Date 2016-10-26 00:00:00
Iyear 2015
Report Number 20160346
Supplemental Number 22890
Report Type Supplemental Final
Operator Id 32537 PHMSA Enforcement
Name Wyoming Pipeline Company
Operator Street Address 825 Town & Country Lane
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77024
Local Datetime 2015-07-09 09:30:00
Location Latitude 43.4625 Google Maps OpenStreetMap
Location Longitude -104.226944 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 30
Recovered Bbls 30
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-07-09 09:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Buck Creek Line Not In Operation.
On Site Datetime 2015-07-09 11:00:00
Nrc Rpt Datetime 2015-07-10 08:22:00
Nrc Rpt Num 1122359 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wyoming Pipeline Company
Segment Name Buck Creek/morrissey Main Line
Onshore State Abbreviation Wy
Onshore Postal Code 82701
Onshore City Name Not Within A Municipality
Onshore County Name Niobrara County
Designated Location Milepost/valve Station
Designated Name Buck Crk Line
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.365
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1949
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1200
Est Cost Prop Damage 5000
Est Cost Emergency 7185
Est Cost Environmental 3460
Est Cost Other 0
Prpty 16845
Accident Psig 0
Mop Psig 326
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This line has been inactive and the leak was discovered by air patrol.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Microbiological Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location No
Externally Coated Yes
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name W****** M********
Preparer Title Compliance Consultant
Preparer Email W*****@c**.net
Preparer Telephone 4058201304
Prepared Date 2017-12-06 00:00:00
Authorizer Name N***** H******
Authorizer Telephone 307-746-2379
Authorizer Title Environmental Engineer
Authorizer Email N*******@w****.com
Narrative This spill was located approximately 24 miles south of newcastle, wyoming on the property of tim & sonya tysdal ranch; the area known as "bobcat creek." the creek is a dry wash and was dry at the time of the incident. Air patrol called in the leak to mush creek control center. Mccc notified the maintenance supervisor and the vac truck and backhoe were dispatched to the site. The oil was sucked up and returned to tankage; contaminated soil was picked up; hauled to remediation site. New soil was deposited in the excavated area.

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