HL incident on 2016-09-24 — TX

Operator
Plains Pipeline, L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$14,415
Incident datetime
2016-09-24 09:15
Report number
Location
TX
Narrative
Approximately 5 bbls of crude oil were released from an underground tank fill line as a result of internal corrosion. This piping has been removed and replaced. Modifications will be conducted in january to bring this piping aboveground. The national response center (nrc) was contacted as a precaution but it was later deemed unnecessary.
Detailed record list
Report Received Date
2016-10-24 00:00:00
Iyear
2016
Report Number
20160342
Supplemental Number
21785
Report Type
Original Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-09-24 09:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-09-24 09:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-09-24 09:16:00
Restart Datetime
2016-09-29 15:56:00
On Site Datetime
2016-09-24 09:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Mccamey Terminal
Segment Name
Tank 361 Manifold Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
79752
Onshore City Name
Mccamey
Onshore County Name
Upton
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
40
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
16
Pipe Wall Thickness
0.375
Pipe Smys
42000
Pipe Specification
X42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
14415
Est Cost Emergency
7590
Est Cost Environmental
0
Est Cost Other
0
Prpty
22005
Accident Psig
40
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C******* C*****
Preparer Title
Compliance Specialist
Preparer Email
C*******@p****.com
Preparer Telephone
713-993-5080
Preparer Fax
713-646-4310
Prepared Date
2016-10-24 00:00:00
Authorizer Name
T***** M*****
Authorizer Telephone
713-646-4109
Authorizer Title
Sr Dir Of Environmental And Regulatory Compliance
Authorizer Email
T*******@p****.com
Narrative
Approximately 5 bbls of crude oil were released from an underground tank fill line as a result of internal corrosion. This piping has been removed and replaced. Modifications will be conducted in january to bring this piping aboveground. The national response center (nrc) was contacted as a precaution but it was later deemed unnecessary.
Report Received Date 2016-10-24 00:00:00
Iyear 2016
Report Number 20160342
Supplemental Number 21785
Report Type Original Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-09-24 09:15:00
Location Latitude 31.13488 Google Maps OpenStreetMap
Location Longitude -102.188698 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 5
Recovered Bbls 5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-09-24 09:15:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-09-24 09:16:00
Restart Datetime 2016-09-29 15:56:00
On Site Datetime 2016-09-24 09:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Mccamey Terminal
Segment Name Tank 361 Manifold Piping
Onshore State Abbreviation Tx
Onshore Postal Code 79752
Onshore City Name Mccamey
Onshore County Name Upton
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 40
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 16
Pipe Wall Thickness 0.375
Pipe Smys 42000
Pipe Specification X42
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 14415
Est Cost Emergency 7590
Est Cost Environmental 0
Est Cost Other 0
Prpty 22005
Accident Psig 40
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C******* C*****
Preparer Title Compliance Specialist
Preparer Email C*******@p****.com
Preparer Telephone 713-993-5080
Preparer Fax 713-646-4310
Prepared Date 2016-10-24 00:00:00
Authorizer Name T***** M*****
Authorizer Telephone 713-646-4109
Authorizer Title Sr Dir Of Environmental And Regulatory Compliance
Authorizer Email T*******@p****.com
Narrative Approximately 5 bbls of crude oil were released from an underground tank fill line as a result of internal corrosion. This piping has been removed and replaced. Modifications will be conducted in january to bring this piping aboveground. The national response center (nrc) was contacted as a precaution but it was later deemed unnecessary.

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