HL incident on 2016-09-29 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-09-29 06:45
Report number
Location
OK
Narrative
At approximately 6:45 a.M. An operator found that a valve on the hydrometer in the change shack had been left open and gasoline flowed out of the change shack building and into the containment ditch surrounding it. The valve to the hydrometer was closed, stopping the leak, air monitoring was established, an exclusionary area was designated, and all work done in the area was done by personnel utilizing a half mask respirator with continued air monitoring. Potholes were dug in the impacted area, diapers placed in potholes, a vacuum truck which was onsite recovered free product, and roll off boxes were utilized to store recovered soil. Environmental contractors assisted in delineation and sampling. Approximately 2.5 bbl of product was recovered via vacuum truck and 1.6 bbl of product was recovered in 20 cubic yards of impacted soil which was excavated. Approximately 0.7 barrels was determined to have volatized following the release. Soil samples confirmed that soil conditions were within the oklahoma corporation commission (occ) cleanup standards, no further soil remediation actions required. The individual involved was disqualified following the incident and re-qualified on november 17, 2016. Supplemental update: part a #11 volume recovered and part h narrative
Detailed record list
Report Received Date
2016-10-24 00:00:00
Iyear
2016
Report Number
20160341
Supplemental Number
22422
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
One Williams Center, Md 28 P.o. Box 22186
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2016-09-29 06:45:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
5
Recovered Bbls
4.8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-09-29 06:45:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Operation Had Been Completed By The Time Of Discovery
On Site Datetime
2016-09-29 06:45:00
Nrc Rpt Datetime
2016-09-30 13:27:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Glenpool West Station
Segment Name
Station 585
Onshore State Abbreviation
Ok
Onshore Postal Code
74033
Onshore City Name
Glenpool
Onshore County Name
Tulsa
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1978
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
A Valve Was Opened And Left Unattended Which Overfilled A Hydrometer Tube And Released Product.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
0
Est Cost Emergency
52000
Est Cost Environmental
0
Est Cost Other
0
Prpty
52050
Accident Psig
0
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The change shack where the release occurred is not monitored by operations control. Operations control did not cause or contribute to the release.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2017-06-16 00:00:00
Authorizer Name
S****** L******
Authorizer Telephone
918-574-7327
Authorizer Title
Ai Analyst
Authorizer Email
S**************@m*********.com
Narrative
At approximately 6:45 a.M. An operator found that a valve on the hydrometer in the change shack had been left open and gasoline flowed out of the change shack building and into the containment ditch surrounding it. The valve to the hydrometer was closed, stopping the leak, air monitoring was established, an exclusionary area was designated, and all work done in the area was done by personnel utilizing a half mask respirator with continued air monitoring. Potholes were dug in the impacted area, diapers placed in potholes, a vacuum truck which was onsite recovered free product, and roll off boxes were utilized to store recovered soil. Environmental contractors assisted in delineation and sampling. Approximately 2.5 bbl of product was recovered via vacuum truck and 1.6 bbl of product was recovered in 20 cubic yards of impacted soil which was excavated. Approximately 0.7 barrels was determined to have volatized following the release. Soil samples confirmed that soil conditions were within the oklahoma corporation commission (occ) cleanup standards, no further soil remediation actions required. The individual involved was disqualified following the incident and re-qualified on november 17, 2016. Supplemental update: part a #11 volume recovered and part h narrative
Report Received Date 2016-10-24 00:00:00
Iyear 2016
Report Number 20160341
Supplemental Number 22422
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address One Williams Center, Md 28 P.o. Box 22186
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2016-09-29 06:45:00
Location Latitude 35.96953 Google Maps OpenStreetMap
Location Longitude -96.01372 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 5
Recovered Bbls 4.8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-09-29 06:45:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Operation Had Been Completed By The Time Of Discovery
On Site Datetime 2016-09-29 06:45:00
Nrc Rpt Datetime 2016-09-30 13:27:00
Nrc Rpt Num 1160434 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Glenpool West Station
Segment Name Station 585
Onshore State Abbreviation Ok
Onshore Postal Code 74033
Onshore City Name Glenpool
Onshore County Name Tulsa
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1978
Material Involved Carbon Steel
Release Type Other
Release Type Details A Valve Was Opened And Left Unattended Which Overfilled A Hydrometer Tube And Released Product.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 0
Est Cost Emergency 52000
Est Cost Environmental 0
Est Cost Other 0
Prpty 52050
Accident Psig 0
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The change shack where the release occurred is not monitored by operations control. Operations control did not cause or contribute to the release.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2017-06-16 00:00:00
Authorizer Name S****** L******
Authorizer Telephone 918-574-7327
Authorizer Title Ai Analyst
Authorizer Email S**************@m*********.com
Narrative At approximately 6:45 a.M. An operator found that a valve on the hydrometer in the change shack had been left open and gasoline flowed out of the change shack building and into the containment ditch surrounding it. The valve to the hydrometer was closed, stopping the leak, air monitoring was established, an exclusionary area was designated, and all work done in the area was done by personnel utilizing a half mask respirator with continued air monitoring. Potholes were dug in the impacted area, diapers placed in potholes, a vacuum truck which was onsite recovered free product, and roll off boxes were utilized to store recovered soil. Environmental contractors assisted in delineation and sampling. Approximately 2.5 bbl of product was recovered via vacuum truck and 1.6 bbl of product was recovered in 20 cubic yards of impacted soil which was excavated. Approximately 0.7 barrels was determined to have volatized following the release. Soil samples confirmed that soil conditions were within the oklahoma corporation commission (occ) cleanup standards, no further soil remediation actions required. The individual involved was disqualified following the incident and re-qualified on november 17, 2016. Supplemental update: part a #11 volume recovered and part h narrative

All rights reserved. Copyright © by ClearPHMSA