Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2016-09-22 — TX
Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$5,000
Incident datetime
2016-09-22 09:00
Report number
Location
TX
Narrative
During a routine station inspection on 9/22/2016 operation personnel discovered a small release around the mixer on tank 300 at goodrich station. Investigation revealed the mixer shaft seal was leaking. Approximately ten gallons were released. The tank was pumped down and the manway blinded. The mixer was removed, the shaft seal was replaced and the mixer has been returned to service in tank 300. The contaminated soil was excavated and remediated onsite.
Detailed record list
Report Received Date
2016-10-20 00:00:00
Iyear
2016
Report Number
20160337
Supplemental Number
22536
Report Type
Supplemental Final
Operator Id
18718
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-09-22 09:00:00
Location Latitude
30.61829
Location Longitude
-94.97073
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.24
Recovered Bbls
0.24
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-09-22 09:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Isolated From Mainline.
On Site Datetime
2016-09-22 09:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Goodrich Station-Tank 300 Mixer
Segment Name
21004-10" Kilgore To Oti
Onshore State Abbreviation
Tx
Onshore Postal Code
77335
Onshore City Name
Goodrich
Onshore County Name
Polk
Designated Location
Survey Station No.
Designated Name
6729+76
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
5000
Est Cost Emergency
14000
Est Cost Environmental
0
Est Cost Other
0
Prpty
19000
Accident Psig
25
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
None-Mixer Seal Failure
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2017-08-10 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
During a routine station inspection on 9/22/2016 operation personnel discovered a small release around the mixer on tank 300 at goodrich station. Investigation revealed the mixer shaft seal was leaking. Approximately ten gallons were released. The tank was pumped down and the manway blinded. The mixer was removed, the shaft seal was replaced and the mixer has been returned to service in tank 300. The contaminated soil was excavated and remediated onsite.
| Report Received Date | 2016-10-20 00:00:00 |
|---|---|
| Iyear | 2016 |
| Report Number | 20160337 |
| Supplemental Number | 22536 |
| Report Type | Supplemental Final |
| Operator Id | 18718 PHMSA Enforcement |
| Name | Sunoco Pipeline L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2016-09-22 09:00:00 |
| Location Latitude | 30.61829 Google Maps OpenStreetMap |
| Location Longitude | -94.97073 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.24 |
| Recovered Bbls | 0.24 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2016-09-22 09:00:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Tank Was Isolated From Mainline. |
| On Site Datetime | 2016-09-22 09:00:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Goodrich Station-Tank 300 Mixer |
| Segment Name | 21004-10" Kilgore To Oti |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77335 |
| Onshore City Name | Goodrich |
| Onshore County Name | Polk |
| Designated Location | Survey Station No. |
| Designated Name | 6729+76 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Tank/vessel |
| Tank Vessel Subtype | Mixer |
| Tank Type | Atmospheric |
| Installation Year | 2012 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 5000 |
| Est Cost Emergency | 14000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 19000 |
| Accident Psig | 25 |
| Mop Psig | 285 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | A review of the accident determined that there were no control room actions that contributed to the event. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Seal (Not Pump Seal) Or Packing |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | None-Mixer Seal Failure |
| Preparer Name | T*** G* N******* |
| Preparer Title | Dot Compliance Manager |
| Preparer Email | T*********@s**************.com |
| Preparer Telephone | 281-637-6576 |
| Preparer Fax | 877-917-0448 |
| Prepared Date | 2017-08-10 00:00:00 |
| Authorizer Name | T*** G* N******* |
| Authorizer Telephone | 281-637-6576 |
| Authorizer Title | Dot Compliance Manager |
| Authorizer Email | T*********@s**************.com |
| Narrative | During a routine station inspection on 9/22/2016 operation personnel discovered a small release around the mixer on tank 300 at goodrich station. Investigation revealed the mixer shaft seal was leaking. Approximately ten gallons were released. The tank was pumped down and the manway blinded. The mixer was removed, the shaft seal was replaced and the mixer has been returned to service in tank 300. The contaminated soil was excavated and remediated onsite. |
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