HL incident on 2016-09-19 — IL

Operator
Bp Pipeline (North America) Inc.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$181,000
Incident datetime
2016-09-19 06:45
Report number
Location
IL
Narrative
At approximately 06:45 on monday september 19th, a magellan pipeline operator at drumright station contacted bp's local technician notifying him that there may be a possible release from the bp pipeline facilities. Drumright station is a manned magellan pipeline facility through which bp's #1 crude system traverses and has several pumps. The local bp technician contacted bp's tulsa control center and the pipeline was shut down immediately. The bp technician arrived onsite at approximately at 07:30 and confirmed the release. An estimated 22 barrels of crude oil was released. The released crude was removed and the sub-grade source identified via hydro-vacuuming. The source of the release was determined to be a block valve flange. The valve was installed in the 1950's. The valve incorporated ring joint flanges while the connecting piping flanges were raised face. The gasket connecting the valve to the pipe was found to not be of a currently approved design for joining the two flange types . Additionally, some of the bolts on the leaking flange were found to be loose. The flange surfaces and gasket were inspected, the gasket replaced with one suitable for the installation, the assembly appropriately torqued, and the line restarted. The other valves in the area were excavated and their flanged connections checked for to ensure they were appropriately torqued. Please note due to PHMSA website error a draft was submitted as an original on 10/18/16 this report should serve as the original.
Detailed record list
Report Received Date
2016-10-19 00:00:00
Iyear
2016
Report Number
20160333
Supplemental Number
22756
Report Type
Supplemental Final
Operator Id
Name
Bp Pipeline (North America) Inc.
Operator Street Address
30 S. Wacker Drive
Operator City Name
Chicago
Operator State Abbreviation
IL
Operator Postal Code
60606
Local Datetime
2016-09-19 06:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
22
Recovered Bbls
22
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-09-19 06:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-09-19 06:45:00
Restart Datetime
2016-09-21 12:19:00
On Site Datetime
2016-09-19 07:30:00
Nrc Rpt Datetime
2016-09-19 10:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
#1 Crude System / Drumright Station
Segment Name
Cushing / Freeman
Onshore State Abbreviation
Ok
Onshore Postal Code
74030
Onshore City Name
Drumright
Onshore County Name
Creek County
Designated Location
Milepost/valve Station
Designated Name
Scraper Trap
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
26
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1950
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
181000
Est Cost Emergency
34000
Est Cost Environmental
101000
Est Cost Other
0
Prpty
317000
Accident Psig
736
Mop Psig
807
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was a slow release it was not detected by leak detection. Once the controller received the call of a possible release the pipeline was shut down immediately.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Preparer Name
S**** F*********
Preparer Title
Dot Compliance Advisor
Preparer Email
F*****@b*.com
Preparer Telephone
281-217-3703
Prepared Date
2017-10-25 00:00:00
Authorizer Name
M****** S******
Authorizer Telephone
331-702-3226
Authorizer Title
Dot Team Leader Affiliates Uspl
Authorizer Email
M**************@b*.com
Narrative
At approximately 06:45 on monday september 19th, a magellan pipeline operator at drumright station contacted bp's local technician notifying him that there may be a possible release from the bp pipeline facilities. Drumright station is a manned magellan pipeline facility through which bp's #1 crude system traverses and has several pumps. The local bp technician contacted bp's tulsa control center and the pipeline was shut down immediately. The bp technician arrived onsite at approximately at 07:30 and confirmed the release. An estimated 22 barrels of crude oil was released. The released crude was removed and the sub-grade source identified via hydro-vacuuming. The source of the release was determined to be a block valve flange. The valve was installed in the 1950's. The valve incorporated ring joint flanges while the connecting piping flanges were raised face. The gasket connecting the valve to the pipe was found to not be of a currently approved design for joining the two flange types . Additionally, some of the bolts on the leaking flange were found to be loose. The flange surfaces and gasket were inspected, the gasket replaced with one suitable for the installation, the assembly appropriately torqued, and the line restarted. The other valves in the area were excavated and their flanged connections checked for to ensure they were appropriately torqued. Please note due to PHMSA website error a draft was submitted as an original on 10/18/16 this report should serve as the original.
Report Received Date 2016-10-19 00:00:00
Iyear 2016
Report Number 20160333
Supplemental Number 22756
Report Type Supplemental Final
Operator Id 31189 PHMSA Enforcement
Name Bp Pipeline (North America) Inc.
Operator Street Address 30 S. Wacker Drive
Operator City Name Chicago
Operator State Abbreviation IL
Operator Postal Code 60606
Local Datetime 2016-09-19 06:45:00
Location Latitude 35.989585 Google Maps OpenStreetMap
Location Longitude -96.5786369 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 22
Recovered Bbls 22
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-09-19 06:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-09-19 06:45:00
Restart Datetime 2016-09-21 12:19:00
On Site Datetime 2016-09-19 07:30:00
Nrc Rpt Datetime 2016-09-19 10:15:00
Nrc Rpt Num 1159338 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name #1 Crude System / Drumright Station
Segment Name Cushing / Freeman
Onshore State Abbreviation Ok
Onshore Postal Code 74030
Onshore City Name Drumright
Onshore County Name Creek County
Designated Location Milepost/valve Station
Designated Name Scraper Trap
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 26
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1950
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 181000
Est Cost Emergency 34000
Est Cost Environmental 101000
Est Cost Other 0
Prpty 317000
Accident Psig 736
Mop Psig 807
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was a slow release it was not detected by leak detection. Once the controller received the call of a possible release the pipeline was shut down immediately.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Installation Ind Yes
Preparer Name S**** F*********
Preparer Title Dot Compliance Advisor
Preparer Email F*****@b*.com
Preparer Telephone 281-217-3703
Prepared Date 2017-10-25 00:00:00
Authorizer Name M****** S******
Authorizer Telephone 331-702-3226
Authorizer Title Dot Team Leader Affiliates Uspl
Authorizer Email M**************@b*.com
Narrative At approximately 06:45 on monday september 19th, a magellan pipeline operator at drumright station contacted bp's local technician notifying him that there may be a possible release from the bp pipeline facilities. Drumright station is a manned magellan pipeline facility through which bp's #1 crude system traverses and has several pumps. The local bp technician contacted bp's tulsa control center and the pipeline was shut down immediately. The bp technician arrived onsite at approximately at 07:30 and confirmed the release. An estimated 22 barrels of crude oil was released. The released crude was removed and the sub-grade source identified via hydro-vacuuming. The source of the release was determined to be a block valve flange. The valve was installed in the 1950's. The valve incorporated ring joint flanges while the connecting piping flanges were raised face. The gasket connecting the valve to the pipe was found to not be of a currently approved design for joining the two flange types . Additionally, some of the bolts on the leaking flange were found to be loose. The flange surfaces and gasket were inspected, the gasket replaced with one suitable for the installation, the assembly appropriately torqued, and the line restarted. The other valves in the area were excavated and their flanged connections checked for to ensure they were appropriately torqued. Please note due to PHMSA website error a draft was submitted as an original on 10/18/16 this report should serve as the original.

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