HL incident on 2016-09-11 — TX

Operator
Texstar Midstream Logistics, Lp
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$16,960
Incident datetime
2016-09-11 19:42
Report number
Location
TX
Narrative
Delivering crude oil to 3rd party storage facility via lact meter skid. Gas controller received high pressure alarm on lact meter skid and notified pipeline operations personnel. Operations personnel had responded by shutting down pumps and investigating cause of high pressure. While operator was enroute to lact meter skid location, 3rd party storage facility operator called and reported a leak on the meter skid. Upon arrival, pipeline operations personnel shutdown valve upstream of lact meter skid to isolate leak. Upon investigation, it was determined downstream blockage had created the high pressure event resulting in the meter skid relief valve operation releasing oil to the soil. Cause of downstream blockage was on 3rd party system, which they reported to have been the possible result of a check valve failure; the check valve in question was replaced by the 3rd party customer. In addition, the lact meter skid high pressure shutdown valve was discovered to have been placed in local mode by an unknown 3rd party which disabled the valve from operating upon high pressure. The valve was placed back in service with a guard installed over the local/remote switch to prevent future tampering. Repairs were made to the lact skid, equipment was tested and returned to service 4 days after the incident. The following corrective actions have been implemented as a result of the root cause investigation: 1) 3rd party customer reported they replaced check valve on their downstream piping; 2) esd valve was returned to service, cover added over local/remote switch to prevent tampering and added point in scada to alert gas control center when valve is placed in local position in the field; 3) added high pressure alarm on lact skid; 4) added flow alarm on psv discharge to indicate if psv has activated; and, 5) added sop requiring physical verification in the field prior to resuming operations after high pressure alarm and shutdown.
Detailed record list
Report Received Date
2016-10-06 00:00:00
Iyear
2016
Report Number
20160323
Supplemental Number
21941
Report Type
Supplemental Final
Operator Id
Name
Texstar Midstream Logistics, Lp
Operator Street Address
1 Bda Crossing Ste 100
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78235
Local Datetime
2016-09-11 19:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
168
Recovered Bbls
18
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Customer
Incident Identified Datetime
2016-09-11 19:42:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-09-11 19:45:00
Restart Datetime
2016-09-15 07:30:00
On Site Datetime
2016-09-11 19:45:00
Nrc Rpt Datetime
2016-09-15 09:20:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Calumet Elmendorf Storage Facility
Segment Name
Karnes North 8"
Onshore State Abbreviation
Tx
Onshore Postal Code
78112
Onshore City Name
Not Within A Municipality
Onshore County Name
Bexar
Designated Location
Survey Station No.
Designated Name
2700+57
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Lact Meter Skid Psv
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Relief Valve
Installation Year
2014
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Relief Valve Release To Atmosphere
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
7560
Est Cost Prop Damage
16960
Est Cost Emergency
8735
Est Cost Environmental
78615
Est Cost Other
375
Est Cost Other Details
Incident Reporting
Prpty
112245
Accident Psig
693
Mop Psig
280
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind
Yes
Invest No Schedule Ind Details
Fatigue Was Not An Issue And Controllers Were Working Normal Shift. Controllers Received Alarms And Responded Appropriately.
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Esd System Failure Ind
Yes
Additional Overpressure Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Esd Shutdown Valve Disabled By Unknown 3rd Party
Preparer Name
T** L****
Preparer Title
Director Of Compliance Services
Preparer Email
T********@f*************.net
Preparer Telephone
405-423-8159
Prepared Date
2016-12-08 00:00:00
Authorizer Name
J***** G*****
Authorizer Telephone
210-569-6729
Authorizer Title
Vice President Of Operations And Engineering
Authorizer Email
J************@t***************.com
Narrative
Delivering crude oil to 3rd party storage facility via lact meter skid. Gas controller received high pressure alarm on lact meter skid and notified pipeline operations personnel. Operations personnel had responded by shutting down pumps and investigating cause of high pressure. While operator was enroute to lact meter skid location, 3rd party storage facility operator called and reported a leak on the meter skid. Upon arrival, pipeline operations personnel shutdown valve upstream of lact meter skid to isolate leak. Upon investigation, it was determined downstream blockage had created the high pressure event resulting in the meter skid relief valve operation releasing oil to the soil. Cause of downstream blockage was on 3rd party system, which they reported to have been the possible result of a check valve failure; the check valve in question was replaced by the 3rd party customer. In addition, the lact meter skid high pressure shutdown valve was discovered to have been placed in local mode by an unknown 3rd party which disabled the valve from operating upon high pressure. The valve was placed back in service with a guard installed over the local/remote switch to prevent future tampering. Repairs were made to the lact skid, equipment was tested and returned to service 4 days after the incident. The following corrective actions have been implemented as a result of the root cause investigation: 1) 3rd party customer reported they replaced check valve on their downstream piping; 2) esd valve was returned to service, cover added over local/remote switch to prevent tampering and added point in scada to alert gas control center when valve is placed in local position in the field; 3) added high pressure alarm on lact skid; 4) added flow alarm on psv discharge to indicate if psv has activated; and, 5) added sop requiring physical verification in the field prior to resuming operations after high pressure alarm and shutdown.
Report Received Date 2016-10-06 00:00:00
Iyear 2016
Report Number 20160323
Supplemental Number 21941
Report Type Supplemental Final
Operator Id 39098 PHMSA Enforcement
Name Texstar Midstream Logistics, Lp
Operator Street Address 1 Bda Crossing Ste 100
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78235
Local Datetime 2016-09-11 19:30:00
Location Latitude 29.21194 Google Maps OpenStreetMap
Location Longitude -98.40472 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 168
Recovered Bbls 18
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Customer
Incident Identified Datetime 2016-09-11 19:42:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-09-11 19:45:00
Restart Datetime 2016-09-15 07:30:00
On Site Datetime 2016-09-11 19:45:00
Nrc Rpt Datetime 2016-09-15 09:20:00
Nrc Rpt Num 1159037 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Calumet Elmendorf Storage Facility
Segment Name Karnes North 8"
Onshore State Abbreviation Tx
Onshore Postal Code 78112
Onshore City Name Not Within A Municipality
Onshore County Name Bexar
Designated Location Survey Station No.
Designated Name 2700+57
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Lact Meter Skid Psv
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Relief Valve
Installation Year 2014
Material Involved Carbon Steel
Release Type Other
Release Type Details Relief Valve Release To Atmosphere
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 7560
Est Cost Prop Damage 16960
Est Cost Emergency 8735
Est Cost Environmental 78615
Est Cost Other 375
Est Cost Other Details Incident Reporting
Prpty 112245
Accident Psig 693
Mop Psig 280
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind Yes
Invest No Schedule Ind Details Fatigue Was Not An Issue And Controllers Were Working Normal Shift. Controllers Received Alarms And Responded Appropriately.
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Check Valve Ind Yes
Esd System Failure Ind Yes
Additional Overpressure Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Esd Shutdown Valve Disabled By Unknown 3rd Party
Preparer Name T** L****
Preparer Title Director Of Compliance Services
Preparer Email T********@f*************.net
Preparer Telephone 405-423-8159
Prepared Date 2016-12-08 00:00:00
Authorizer Name J***** G*****
Authorizer Telephone 210-569-6729
Authorizer Title Vice President Of Operations And Engineering
Authorizer Email J************@t***************.com
Narrative Delivering crude oil to 3rd party storage facility via lact meter skid. Gas controller received high pressure alarm on lact meter skid and notified pipeline operations personnel. Operations personnel had responded by shutting down pumps and investigating cause of high pressure. While operator was enroute to lact meter skid location, 3rd party storage facility operator called and reported a leak on the meter skid. Upon arrival, pipeline operations personnel shutdown valve upstream of lact meter skid to isolate leak. Upon investigation, it was determined downstream blockage had created the high pressure event resulting in the meter skid relief valve operation releasing oil to the soil. Cause of downstream blockage was on 3rd party system, which they reported to have been the possible result of a check valve failure; the check valve in question was replaced by the 3rd party customer. In addition, the lact meter skid high pressure shutdown valve was discovered to have been placed in local mode by an unknown 3rd party which disabled the valve from operating upon high pressure. The valve was placed back in service with a guard installed over the local/remote switch to prevent future tampering. Repairs were made to the lact skid, equipment was tested and returned to service 4 days after the incident. The following corrective actions have been implemented as a result of the root cause investigation: 1) 3rd party customer reported they replaced check valve on their downstream piping; 2) esd valve was returned to service, cover added over local/remote switch to prevent tampering and added point in scada to alert gas control center when valve is placed in local position in the field; 3) added high pressure alarm on lact skid; 4) added flow alarm on psv discharge to indicate if psv has activated; and, 5) added sop requiring physical verification in the field prior to resuming operations after high pressure alarm and shutdown.

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